HL incident on 2019-09-16 — TX

Operator
Sinclair Transportation Company
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,500
Incident datetime
2019-09-16 15:45
Report number
Location
TX
Narrative
On 9/16/2019, at 13:50 the control center received a call from resident reporting dead spots in the grass, with dark spots in the soil and an odor of diesel. The resident described his location as south of bb highway in clark county. The control center contacted local operations personnel as a precaution, before personnel could reach the site, the control center initiated a line shut down at 14:02. The three intermediate motor operated remote valves were blocked in between gibbs station and montrose terminal. The maintenance crew was dispatched to the site. A crew with a mini excavator was at the scene within 2 hours (15:45). The pipe was exposed and gasoline saturated soil was observed near the pipe. Excavation continued until the leak location was found. A small corrosion pit was found at the 5 o'clock position. Initially observed as just a seeping leak, when the rust scale was removed from the pipe so that a repair clamp could be installed, the leak rate increased. A clamp was successfully installed at 16:45 and the emergency phase of the incident was over. There were no personal injuries or fires related to the release or response. Only soil impact was observed. No surface water was impacted. No free standing liquid was observed ' only saturated soil. The site is being excavated of all contaminated soil. Once all contaminated soil is removed, the pipe will be cut out and sent to a laboratory off site to determine pipe grade and seam type.
Detailed record list
Report Received Date
2019-09-26 00:00:00
Iyear
2019
Report Number
20190301
Supplemental Number
33360
Report Type
Supplemental Final
Operator Id
Name
Sinclair Transportation Company
Operator Street Address
2323 Victory Ave. Suite 1400
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75219
Local Datetime
2019-09-16 15:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2019-09-16 15:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Shutdown Following Landowner Notification
On Site Datetime
2019-09-16 15:45:00
Nrc Rpt Datetime
2019-09-16 16:05:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Mid Continent Pipeline
Segment Name
Gibbs To Montrose
Onshore State Abbreviation
Mo
Onshore Postal Code
63445
Onshore City Name
Not Within A Municipality
Onshore County Name
Clark
Designated Location
Milepost/valve Station
Designated Name
Mp 42.16
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
30
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.322
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Other
Pipe Seam Details
Not Known At This Time
Pipe Manufacturer
Unknown
Pipe Coating Type
None
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
10000
Est Cost Gas Released
1050
Est Cost Prop Damage
3500
Est Cost Emergency
2000
Est Cost Environmental
610000
Est Cost Other
0
Prpty
626550
Accident Psig
41
Mop Psig
485
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
68640
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind
Yes
Invest No Schedule Ind Details
Investigation Identified No Control Room Or Controller Issues
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Invest Other Ind
Yes
Invest Other Ind Details
Investigation Identified That During Shutdowns Some Sections Of Line Have Less Than 15 Psi On Line. The Cpm Leak Detection Is Ineffective When Static Line Pressures Are Less Than 15 Psi
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
Unknown
Cathodic Survey Type
No
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2017
Hydrtst Most Rcnt Pressure
800
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J******* B****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
J*****@s**********.com
Preparer Telephone
3073283643
Prepared Date
2020-02-21 00:00:00
Authorizer Name
M*** P*******
Authorizer Telephone
8015242852
Authorizer Title
President Sinclair Transportation Company
Authorizer Email
M*********@s**********.com
Narrative
On 9/16/2019, at 13:50 the control center received a call from resident reporting dead spots in the grass, with dark spots in the soil and an odor of diesel. The resident described his location as south of bb highway in clark county. The control center contacted local operations personnel as a precaution, before personnel could reach the site, the control center initiated a line shut down at 14:02. The three intermediate motor operated remote valves were blocked in between gibbs station and montrose terminal. The maintenance crew was dispatched to the site. A crew with a mini excavator was at the scene within 2 hours (15:45). The pipe was exposed and gasoline saturated soil was observed near the pipe. Excavation continued until the leak location was found. A small corrosion pit was found at the 5 o'clock position. Initially observed as just a seeping leak, when the rust scale was removed from the pipe so that a repair clamp could be installed, the leak rate increased. A clamp was successfully installed at 16:45 and the emergency phase of the incident was over. There were no personal injuries or fires related to the release or response. Only soil impact was observed. No surface water was impacted. No free standing liquid was observed ' only saturated soil. The site is being excavated of all contaminated soil. Once all contaminated soil is removed, the pipe will be cut out and sent to a laboratory off site to determine pipe grade and seam type.
Report Received Date 2019-09-26 00:00:00
Iyear 2019
Report Number 20190301
Supplemental Number 33360
Report Type Supplemental Final
Operator Id 15156 PHMSA Enforcement
Name Sinclair Transportation Company
Operator Street Address 2323 Victory Ave. Suite 1400
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75219
Local Datetime 2019-09-16 15:45:00
Location Latitude 40.409028 Google Maps OpenStreetMap
Location Longitude -91.838939 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 10
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2019-09-16 15:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Shutdown Following Landowner Notification
On Site Datetime 2019-09-16 15:45:00
Nrc Rpt Datetime 2019-09-16 16:05:00
Nrc Rpt Num 1258413 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Mid Continent Pipeline
Segment Name Gibbs To Montrose
Onshore State Abbreviation Mo
Onshore Postal Code 63445
Onshore City Name Not Within A Municipality
Onshore County Name Clark
Designated Location Milepost/valve Station
Designated Name Mp 42.16
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 30
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.322
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Other
Pipe Seam Details Not Known At This Time
Pipe Manufacturer Unknown
Pipe Coating Type None
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 10000
Est Cost Gas Released 1050
Est Cost Prop Damage 3500
Est Cost Emergency 2000
Est Cost Environmental 610000
Est Cost Other 0
Prpty 626550
Accident Psig 41
Mop Psig 485
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 68640
Internal Inspection Ind No
Other Restrictions Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind Yes
Invest No Schedule Ind Details Investigation Identified No Control Room Or Controller Issues
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Invest Other Ind Yes
Invest Other Ind Details Investigation Identified That During Shutdowns Some Sections Of Line Have Less Than 15 Psi On Line. The Cpm Leak Detection Is Ineffective When Static Line Pressures Are Less Than 15 Psi
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident Unknown
Cathodic Survey Type No
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2017
Hydrtst Most Rcnt Pressure 800
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J******* B****
Preparer Title Regulatory Compliance Coordinator
Preparer Email J*****@s**********.com
Preparer Telephone 3073283643
Prepared Date 2020-02-21 00:00:00
Authorizer Name M*** P*******
Authorizer Telephone 8015242852
Authorizer Title President Sinclair Transportation Company
Authorizer Email M*********@s**********.com
Narrative On 9/16/2019, at 13:50 the control center received a call from resident reporting dead spots in the grass, with dark spots in the soil and an odor of diesel. The resident described his location as south of bb highway in clark county. The control center contacted local operations personnel as a precaution, before personnel could reach the site, the control center initiated a line shut down at 14:02. The three intermediate motor operated remote valves were blocked in between gibbs station and montrose terminal. The maintenance crew was dispatched to the site. A crew with a mini excavator was at the scene within 2 hours (15:45). The pipe was exposed and gasoline saturated soil was observed near the pipe. Excavation continued until the leak location was found. A small corrosion pit was found at the 5 o'clock position. Initially observed as just a seeping leak, when the rust scale was removed from the pipe so that a repair clamp could be installed, the leak rate increased. A clamp was successfully installed at 16:45 and the emergency phase of the incident was over. There were no personal injuries or fires related to the release or response. Only soil impact was observed. No surface water was impacted. No free standing liquid was observed ' only saturated soil. The site is being excavated of all contaminated soil. Once all contaminated soil is removed, the pipe will be cut out and sent to a laboratory off site to determine pipe grade and seam type.

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