HL incident on 2019-08-02 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$54,000
Incident datetime
2019-08-02 13:20
Report number
Location
TX
Narrative
On 8/2/2019 at 13:20, km operations responded to a hydrocarbon detector alarm at the 3900 manifold. A pinhole leak was found on the outbound tank line for tank 150-116. The area was isolated and stripped and the section of pipe was removed. The pipe was sent for metallurgical analysis, which determined the cause to be oxygen at a vapor-liquid interface.
Detailed record list
Report Received Date
2019-08-30 00:00:00
Iyear
2019
Report Number
20190278
Supplemental Number
33488
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-08-02 13:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2019-08-02 13:20:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Did Not Affect Operations
On Site Datetime
2019-08-02 13:20:00
Nrc Rpt Datetime
2019-08-29 11:26:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park
Segment Name
Tank 150-116 Tankline
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Industrial Piping Specialist
Pipe Coating Type
Paint
Installation Year
2012
Manufactured Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
800
Est Cost Prop Damage
54000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
54800
Accident Psig
40
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Line not operational at time of incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Vapor-Liquid Interface Caused Oxygen Deposits On The Metal
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Middle Of Tee
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D******* S*******
Preparer Title
Director Of Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
7134206496
Prepared Date
2020-03-19 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
7134206496
Authorizer Title
Director Of Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On 8/2/2019 at 13:20, km operations responded to a hydrocarbon detector alarm at the 3900 manifold. A pinhole leak was found on the outbound tank line for tank 150-116. The area was isolated and stripped and the section of pipe was removed. The pipe was sent for metallurgical analysis, which determined the cause to be oxygen at a vapor-liquid interface.
Report Received Date 2019-08-30 00:00:00
Iyear 2019
Report Number 20190278
Supplemental Number 33488
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-08-02 13:20:00
Location Latitude 29.72708 Google Maps OpenStreetMap
Location Longitude -95.21915 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2019-08-02 13:20:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Did Not Affect Operations
On Site Datetime 2019-08-02 13:20:00
Nrc Rpt Datetime 2019-08-29 11:26:00
Nrc Rpt Num 1256742 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Galena Park
Segment Name Tank 150-116 Tankline
Onshore State Abbreviation Tx
Onshore Postal Code 77547
Onshore City Name Galena Park
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 20
Pipe Wall Thickness 0.375
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Industrial Piping Specialist
Pipe Coating Type Paint
Installation Year 2012
Manufactured Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 800
Est Cost Prop Damage 54000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 54800
Accident Psig 40
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Line not operational at time of incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details Vapor-Liquid Interface Caused Oxygen Deposits On The Metal
Int Metallurgical Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Middle Of Tee
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name D******* S*******
Preparer Title Director Of Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 7134206496
Prepared Date 2020-03-19 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 7134206496
Authorizer Title Director Of Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On 8/2/2019 at 13:20, km operations responded to a hydrocarbon detector alarm at the 3900 manifold. A pinhole leak was found on the outbound tank line for tank 150-116. The area was isolated and stripped and the section of pipe was removed. The pipe was sent for metallurgical analysis, which determined the cause to be oxygen at a vapor-liquid interface.

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