HL incident on 2019-07-31 — TX

Operator
Buckeye Development & Logistics, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-07-31 10:42
Report number
Location
TX
Narrative
On 7/31/2019 at approximately 10:42 am, local operations employees were cleaning up from a previous maintenance activity they were performing on the sasol-na1-tx-6" ethane line at the lone star ngl facility when they heard a leak coming from the door of the pig trap. Local operations immediately called the lone star outside operator who immediately turned on local fire monitors around the area of the pig trap to suppress the ethane vapors, and the emergency response procedures were initiated. All internal and external notifications were made. The pig trap was removed, blinded, and shipped to dnv to further investigate the cause of the release on the threaded pig trap door. The root cause of the incident was determined to be equipment failure. The results of the analysis indicate that the leak occurred due to the failure of an o-ring. The o-ring failed as a result of mechanical damage in the form of pinching that occurred during installation.
Detailed record list
Report Received Date
2019-08-30 00:00:00
Iyear
2019
Report Number
20190277
Supplemental Number
33628
Report Type
Supplemental Final
Operator Id
Name
Buckeye Development & Logistics, Llc
Operator Street Address
4200 Westheimer Road # 975
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77027
Local Datetime
2019-07-31 10:42:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
5
Intentional Release Bbls
1343
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-31 10:42:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-07-31 10:48:00
Restart Datetime
2019-08-03 09:54:00
On Site Datetime
2019-07-31 10:42:00
Nrc Rpt Datetime
2019-07-31 11:47:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Lone Star Ngl Facility
Segment Name
Sasol Na1 - Tx
Onshore State Abbreviation
Tx
Onshore Postal Code
77580
Onshore City Name
Mont Belvieu
Onshore County Name
Chambers
Designated Location
Milepost/valve Station
Designated Name
Station 0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
1979
Material Involved
Material Other Than Carbon Steel
Material Details
Viton
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
10000
Est Cost Prop Damage
0
Est Cost Emergency
50000
Est Cost Environmental
0
Est Cost Other
300000
Est Cost Other Details
Cost Associated With The De-Commissioning And Re-Commissioning Line.
Prpty
360000
Accident Psig
1730
Mop Psig
2132
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
26400
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
Pig Trap Door (Threaded Fitting) O-Ring Failure
Preparer Name
M*** C*******
Preparer Title
Sr. Compliance Specialist
Preparer Email
M********@b******.com
Preparer Telephone
936-641-5261
Preparer Fax
713-204-9799
Prepared Date
2020-04-22 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On 7/31/2019 at approximately 10:42 am, local operations employees were cleaning up from a previous maintenance activity they were performing on the sasol-na1-tx-6" ethane line at the lone star ngl facility when they heard a leak coming from the door of the pig trap. Local operations immediately called the lone star outside operator who immediately turned on local fire monitors around the area of the pig trap to suppress the ethane vapors, and the emergency response procedures were initiated. All internal and external notifications were made. The pig trap was removed, blinded, and shipped to dnv to further investigate the cause of the release on the threaded pig trap door. The root cause of the incident was determined to be equipment failure. The results of the analysis indicate that the leak occurred due to the failure of an o-ring. The o-ring failed as a result of mechanical damage in the form of pinching that occurred during installation.
Report Received Date 2019-08-30 00:00:00
Iyear 2019
Report Number 20190277
Supplemental Number 33628
Report Type Supplemental Final
Operator Id 31371 PHMSA Enforcement
Name Buckeye Development & Logistics, Llc
Operator Street Address 4200 Westheimer Road # 975
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77027
Local Datetime 2019-07-31 10:42:00
Location Latitude 29.8561111 Google Maps OpenStreetMap
Location Longitude -94.9019444 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 5
Intentional Release Bbls 1343
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-07-31 10:42:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-07-31 10:48:00
Restart Datetime 2019-08-03 09:54:00
On Site Datetime 2019-07-31 10:42:00
Nrc Rpt Datetime 2019-07-31 11:47:00
Nrc Rpt Num 1253764 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Lone Star Ngl Facility
Segment Name Sasol Na1 - Tx
Onshore State Abbreviation Tx
Onshore Postal Code 77580
Onshore City Name Mont Belvieu
Onshore County Name Chambers
Designated Location Milepost/valve Station
Designated Name Station 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 1979
Material Involved Material Other Than Carbon Steel
Material Details Viton
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 10000
Est Cost Prop Damage 0
Est Cost Emergency 50000
Est Cost Environmental 0
Est Cost Other 300000
Est Cost Other Details Cost Associated With The De-Commissioning And Re-Commissioning Line.
Prpty 360000
Accident Psig 1730
Mop Psig 2132
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 26400
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details Pig Trap Door (Threaded Fitting) O-Ring Failure
Preparer Name M*** C*******
Preparer Title Sr. Compliance Specialist
Preparer Email M********@b******.com
Preparer Telephone 936-641-5261
Preparer Fax 713-204-9799
Prepared Date 2020-04-22 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On 7/31/2019 at approximately 10:42 am, local operations employees were cleaning up from a previous maintenance activity they were performing on the sasol-na1-tx-6" ethane line at the lone star ngl facility when they heard a leak coming from the door of the pig trap. Local operations immediately called the lone star outside operator who immediately turned on local fire monitors around the area of the pig trap to suppress the ethane vapors, and the emergency response procedures were initiated. All internal and external notifications were made. The pig trap was removed, blinded, and shipped to dnv to further investigate the cause of the release on the threaded pig trap door. The root cause of the incident was determined to be equipment failure. The results of the analysis indicate that the leak occurred due to the failure of an o-ring. The o-ring failed as a result of mechanical damage in the form of pinching that occurred during installation.

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