HL incident on 2019-08-01 — TX

Operator
Centurion Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2019-08-01 11:07
Report number
Location
TX
Narrative
On august 1, 2019, at approximately 11:07 am, a centurion pipeline company l.P. (cpl) employee reported a release at the midland tank farm near midland, texas, in midland county, texas. The release was from a failed pressure gauge downstream of the 2-12 blend pump. Approximately 0.5 barrels of crude oil was released. All oil was recovered with 0.5 barrel in soil remediation. The pressure gauge was replaced on august 2, 2019. No injuries, fatalities, or fires were associated with this accident.
Detailed record list
Report Received Date
2019-08-29 00:00:00
Iyear
2019
Report Number
20190273
Supplemental Number
32629
Report Type
Original Final
Operator Id
Name
Centurion Pipeline L.p.
Operator Street Address
5 Greenway Plaza, Suite 1600
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046-7570
Local Datetime
2019-08-01 11:07:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-08-01 11:07:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Local Pump Was Shut Down To Replace Pressure Gauge Then Restarted.
On Site Datetime
2019-08-01 11:07:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Midland Station
Segment Name
Midland Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Midland
Onshore County Name
Midland
Designated Location
Milepost/valve Station
Designated Name
3-12 Pump
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Instrumentation
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Other
Release Type Details
Pressure Gauge Internal Component Leak.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
35
Est Cost Prop Damage
500
Est Cost Emergency
2500
Est Cost Environmental
0
Est Cost Other
0
Prpty
3035
Accident Psig
100
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No abnormal operating conditions existed at the time of incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Pressure Gauge Internal Component Failure.
Eq Additional Other Ind
Yes
Eq Additional Other Details
End Of Pressure Gauge Life Cycle.
Preparer Name
D**** N*****
Preparer Title
Risk Engineer
Preparer Email
D***********@c**********.com
Preparer Telephone
346-803-2688
Prepared Date
2019-08-29 00:00:00
Authorizer Name
D**** M****
Authorizer Telephone
346-803-2680
Authorizer Title
Senior Pipeline Compliance Consultant
Authorizer Email
D**********@c**********.com
Narrative
On august 1, 2019, at approximately 11:07 am, a centurion pipeline company l.P. (cpl) employee reported a release at the midland tank farm near midland, texas, in midland county, texas. The release was from a failed pressure gauge downstream of the 2-12 blend pump. Approximately 0.5 barrels of crude oil was released. All oil was recovered with 0.5 barrel in soil remediation. The pressure gauge was replaced on august 2, 2019. No injuries, fatalities, or fires were associated with this accident.
Report Received Date 2019-08-29 00:00:00
Iyear 2019
Report Number 20190273
Supplemental Number 32629
Report Type Original Final
Operator Id 31888 PHMSA Enforcement
Name Centurion Pipeline L.p.
Operator Street Address 5 Greenway Plaza, Suite 1600
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046-7570
Local Datetime 2019-08-01 11:07:00
Location Latitude 32.00482 Google Maps OpenStreetMap
Location Longitude -102.04012 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-08-01 11:07:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Local Pump Was Shut Down To Replace Pressure Gauge Then Restarted.
On Site Datetime 2019-08-01 11:07:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Midland Station
Segment Name Midland Station
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Midland
Onshore County Name Midland
Designated Location Milepost/valve Station
Designated Name 3-12 Pump
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Instrumentation
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Other
Release Type Details Pressure Gauge Internal Component Leak.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 35
Est Cost Prop Damage 500
Est Cost Emergency 2500
Est Cost Environmental 0
Est Cost Other 0
Prpty 3035
Accident Psig 100
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No abnormal operating conditions existed at the time of incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Pressure Gauge Internal Component Failure.
Eq Additional Other Ind Yes
Eq Additional Other Details End Of Pressure Gauge Life Cycle.
Preparer Name D**** N*****
Preparer Title Risk Engineer
Preparer Email D***********@c**********.com
Preparer Telephone 346-803-2688
Prepared Date 2019-08-29 00:00:00
Authorizer Name D**** M****
Authorizer Telephone 346-803-2680
Authorizer Title Senior Pipeline Compliance Consultant
Authorizer Email D**********@c**********.com
Narrative On august 1, 2019, at approximately 11:07 am, a centurion pipeline company l.P. (cpl) employee reported a release at the midland tank farm near midland, texas, in midland county, texas. The release was from a failed pressure gauge downstream of the 2-12 blend pump. Approximately 0.5 barrels of crude oil was released. All oil was recovered with 0.5 barrel in soil remediation. The pressure gauge was replaced on august 2, 2019. No injuries, fatalities, or fires were associated with this accident.

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