HL incident on 2019-07-30 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2019-07-30 15:00
Report number
Location
TX
Narrative
On 7/30/2019, a km operator found a leak on the tcr can stripping pump. Approximately 12 gallons of gasoline leaked through the threated connection on the internal flush line of the pump. Remediation began immediately, the asset was stripped and isolated. The pump was pulled from the can and sent out for repairs. The cause of the leak was determined to be corrosion on the threads of the fitting caused by collection of water in the pump head. Plan to prevent reoccurrence - to prevent the accumulation of water from occurring in the pump head, km now has a mousehole, for water draining, be added to the pump head during servicing and inspection of the pumps.
Detailed record list
Report Received Date
2019-08-29 00:00:00
Iyear
2019
Report Number
20190271
Supplemental Number
32624
Report Type
Original Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-07-30 15:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.28
Recovered Bbls
0.28
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-30 15:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Did Not Affect Operations
On Site Datetime
2019-07-30 15:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pasadena Terminal
Segment Name
Tcr Gas D/b Stripper Pump
Onshore State Abbreviation
Tx
Onshore Postal Code
77506
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
36
Est Cost Prop Damage
5000
Est Cost Emergency
0
Est Cost Environmental
1000
Est Cost Other
0
Prpty
6036
Accident Psig
30
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Review of pressure trends did not reveal any high pressure events, therefore controllers actions are not related to release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
Corroded Threads
Preparer Name
D******* S*******
Preparer Title
Director Of Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
7134206496
Prepared Date
2019-08-29 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
7134206496
Authorizer Title
Director Of Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On 7/30/2019, a km operator found a leak on the tcr can stripping pump. Approximately 12 gallons of gasoline leaked through the threated connection on the internal flush line of the pump. Remediation began immediately, the asset was stripped and isolated. The pump was pulled from the can and sent out for repairs. The cause of the leak was determined to be corrosion on the threads of the fitting caused by collection of water in the pump head. Plan to prevent reoccurrence - to prevent the accumulation of water from occurring in the pump head, km now has a mousehole, for water draining, be added to the pump head during servicing and inspection of the pumps.
Report Received Date 2019-08-29 00:00:00
Iyear 2019
Report Number 20190271
Supplemental Number 32624
Report Type Original Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-07-30 15:00:00
Location Latitude 29.728549 Google Maps OpenStreetMap
Location Longitude -95.202147 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.28
Recovered Bbls 0.28
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-07-30 15:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Did Not Affect Operations
On Site Datetime 2019-07-30 15:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Pasadena Terminal
Segment Name Tcr Gas D/b Stripper Pump
Onshore State Abbreviation Tx
Onshore Postal Code 77506
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 36
Est Cost Prop Damage 5000
Est Cost Emergency 0
Est Cost Environmental 1000
Est Cost Other 0
Prpty 6036
Accident Psig 30
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Review of pressure trends did not reveal any high pressure events, therefore controllers actions are not related to release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details Corroded Threads
Preparer Name D******* S*******
Preparer Title Director Of Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 7134206496
Prepared Date 2019-08-29 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 7134206496
Authorizer Title Director Of Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On 7/30/2019, a km operator found a leak on the tcr can stripping pump. Approximately 12 gallons of gasoline leaked through the threated connection on the internal flush line of the pump. Remediation began immediately, the asset was stripped and isolated. The pump was pulled from the can and sent out for repairs. The cause of the leak was determined to be corrosion on the threads of the fitting caused by collection of water in the pump head. Plan to prevent reoccurrence - to prevent the accumulation of water from occurring in the pump head, km now has a mousehole, for water draining, be added to the pump head during servicing and inspection of the pumps.

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