HL incident on 2019-07-26 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2019-07-26 15:00
Report number
Location
GA
Narrative
At approximately 15:00 cst, a senior operator performing a yardcheck noticed stained gravel around and product dripping from the cupola area of the ln02 station discharge valve. The operator contacted a technician, who contacted the control center. The operator began containing the leak source - ln02 was shut down at this time due to an origination out of baton rouge. With assistance from the control center, the technician and operator on-site attempted to stop the leak by closing station valves. Technicians and contract personnel and equipment arrived on-site at approximately 16:45 and evacuated the line to relieve pressure, which, stopped the leak. The valve was repaired at23.55. Mainline operations resumed on 7/27/19 at 00:37. O-ring damage/failure was determined to be the source of the release. Product recovery and soil excavation were completed and the estimated volume of released kerosene is approximately 15 gallons.
Detailed record list
Report Received Date
2019-08-27 00:00:00
Iyear
2019
Report Number
20190268
Supplemental Number
32658
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2019-07-26 15:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.4
Recovered Bbls
0.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-26 15:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Ln02 Was Shut Down At The Time Of Discovery Due To An Origination Down Stream
On Site Datetime
2019-07-26 15:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Krotz Springs Station
Segment Name
Krotz Springs
Onshore State Abbreviation
La
Onshore Postal Code
70750
Onshore City Name
Krotz Springs
Onshore County Name
St. Landry
Designated Location
Milepost/valve Station
Designated Name
Krotz Springs
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1965
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
1000
Est Cost Emergency
6000
Est Cost Environmental
35000
Est Cost Other
0
Prpty
42040
Accident Psig
75
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
All systems were operating normally within acceptable ranges and the source of the leak was associated to an equipment failure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Ief Addl Misalignment Ind
Yes
Preparer Name
R***** D*****
Preparer Title
Compliance Coordinator
Preparer Email
R******@c******.com
Preparer Telephone
4097904288
Prepared Date
2019-09-04 00:00:00
Authorizer Name
R***** D*****
Authorizer Telephone
4097904288
Authorizer Title
Compliance Coordinator
Authorizer Email
R******@c******.com
Narrative
At approximately 15:00 cst, a senior operator performing a yardcheck noticed stained gravel around and product dripping from the cupola area of the ln02 station discharge valve. The operator contacted a technician, who contacted the control center. The operator began containing the leak source - ln02 was shut down at this time due to an origination out of baton rouge. With assistance from the control center, the technician and operator on-site attempted to stop the leak by closing station valves. Technicians and contract personnel and equipment arrived on-site at approximately 16:45 and evacuated the line to relieve pressure, which, stopped the leak. The valve was repaired at23.55. Mainline operations resumed on 7/27/19 at 00:37. O-ring damage/failure was determined to be the source of the release. Product recovery and soil excavation were completed and the estimated volume of released kerosene is approximately 15 gallons.
Report Received Date 2019-08-27 00:00:00
Iyear 2019
Report Number 20190268
Supplemental Number 32658
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2019-07-26 15:00:00
Location Latitude 30.528829 Google Maps OpenStreetMap
Location Longitude -91.746864 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.4
Recovered Bbls 0.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-07-26 15:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Ln02 Was Shut Down At The Time Of Discovery Due To An Origination Down Stream
On Site Datetime 2019-07-26 15:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Krotz Springs Station
Segment Name Krotz Springs
Onshore State Abbreviation La
Onshore Postal Code 70750
Onshore City Name Krotz Springs
Onshore County Name St. Landry
Designated Location Milepost/valve Station
Designated Name Krotz Springs
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1965
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 40
Est Cost Prop Damage 1000
Est Cost Emergency 6000
Est Cost Environmental 35000
Est Cost Other 0
Prpty 42040
Accident Psig 75
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details All systems were operating normally within acceptable ranges and the source of the leak was associated to an equipment failure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Ief Addl Misalignment Ind Yes
Preparer Name R***** D*****
Preparer Title Compliance Coordinator
Preparer Email R******@c******.com
Preparer Telephone 4097904288
Prepared Date 2019-09-04 00:00:00
Authorizer Name R***** D*****
Authorizer Telephone 4097904288
Authorizer Title Compliance Coordinator
Authorizer Email R******@c******.com
Narrative At approximately 15:00 cst, a senior operator performing a yardcheck noticed stained gravel around and product dripping from the cupola area of the ln02 station discharge valve. The operator contacted a technician, who contacted the control center. The operator began containing the leak source - ln02 was shut down at this time due to an origination out of baton rouge. With assistance from the control center, the technician and operator on-site attempted to stop the leak by closing station valves. Technicians and contract personnel and equipment arrived on-site at approximately 16:45 and evacuated the line to relieve pressure, which, stopped the leak. The valve was repaired at23.55. Mainline operations resumed on 7/27/19 at 00:37. O-ring damage/failure was determined to be the source of the release. Product recovery and soil excavation were completed and the estimated volume of released kerosene is approximately 15 gallons.

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