HL incident on 2019-07-24 — TX

Operator
Plains Pipeline, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200
Incident datetime
2019-07-24 08:28
Report number
Location
TX
Narrative
Approximately 14 barrels of crude oil were released within facility boundaries. The date and time of the release (07/23/2019 at 16:30) is indicative of the earliest possible time the release could have started, as it was the last time the location had been visited and confirmed that no crude oil was being released. The release was caused by the double block and bleed valve (body needle valve) not properly seating, and its secondary release control (the plug at the end of the tubing from the body bleed) failing because the ferrule, which would have engaged the compression of the fitting, was not installed during new construction. Additionally, station repairs were completed before restart was required under normal operating procedures. Plains has since replaced the valve and tubing associated to prevent future releases. Supplemental narrative: update was made to part b, q5-county or parish.
Detailed record list
Report Received Date
2019-08-23 00:00:00
Iyear
2019
Report Number
20190263
Supplemental Number
33421
Report Type
Supplemental Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-07-23 16:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
14
Recovered Bbls
12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-24 08:28:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Station Was Shut-Down Prior To The Release Under Normal Operating Procedures.
On Site Datetime
2019-07-24 08:28:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Porterville Station
Segment Name
Meter And Sampling System
Onshore State Abbreviation
Tx
Onshore Postal Code
79754
Onshore City Name
Mentone
Onshore County Name
Loving
Designated Location
Milepost/valve Station
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Meter/prover
Installation Year
2019
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
560
Est Cost Prop Damage
200
Est Cost Emergency
20000
Est Cost Environmental
0
Est Cost Other
0
Prpty
20760
Accident Psig
40
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Porterville station was not operating at the time of the release being discovered by field personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Other
Other Stripped Details
Compression Fitting
Additional Installation Ind
Yes
Preparer Name
N****** G*******
Preparer Title
Erc Compliance Specialist
Preparer Email
N*********@p****.com
Preparer Telephone
7136464376
Prepared Date
2020-03-06 00:00:00
Authorizer Name
N***** G*****
Authorizer Telephone
7136464336
Authorizer Title
Erc Mgr Director
Authorizer Email
N******@p****.com
Narrative
Approximately 14 barrels of crude oil were released within facility boundaries. The date and time of the release (07/23/2019 at 16:30) is indicative of the earliest possible time the release could have started, as it was the last time the location had been visited and confirmed that no crude oil was being released. The release was caused by the double block and bleed valve (body needle valve) not properly seating, and its secondary release control (the plug at the end of the tubing from the body bleed) failing because the ferrule, which would have engaged the compression of the fitting, was not installed during new construction. Additionally, station repairs were completed before restart was required under normal operating procedures. Plains has since replaced the valve and tubing associated to prevent future releases. Supplemental narrative: update was made to part b, q5-county or parish.
Report Received Date 2019-08-23 00:00:00
Iyear 2019
Report Number 20190263
Supplemental Number 33421
Report Type Supplemental Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-07-23 16:30:00
Location Latitude 31.71764 Google Maps OpenStreetMap
Location Longitude -103.5923 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 14
Recovered Bbls 12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-07-24 08:28:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Station Was Shut-Down Prior To The Release Under Normal Operating Procedures.
On Site Datetime 2019-07-24 08:28:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Porterville Station
Segment Name Meter And Sampling System
Onshore State Abbreviation Tx
Onshore Postal Code 79754
Onshore City Name Mentone
Onshore County Name Loving
Designated Location Milepost/valve Station
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Meter/prover
Installation Year 2019
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 560
Est Cost Prop Damage 200
Est Cost Emergency 20000
Est Cost Environmental 0
Est Cost Other 0
Prpty 20760
Accident Psig 40
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Porterville station was not operating at the time of the release being discovered by field personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Other
Other Stripped Details Compression Fitting
Additional Installation Ind Yes
Preparer Name N****** G*******
Preparer Title Erc Compliance Specialist
Preparer Email N*********@p****.com
Preparer Telephone 7136464376
Prepared Date 2020-03-06 00:00:00
Authorizer Name N***** G*****
Authorizer Telephone 7136464336
Authorizer Title Erc Mgr Director
Authorizer Email N******@p****.com
Narrative Approximately 14 barrels of crude oil were released within facility boundaries. The date and time of the release (07/23/2019 at 16:30) is indicative of the earliest possible time the release could have started, as it was the last time the location had been visited and confirmed that no crude oil was being released. The release was caused by the double block and bleed valve (body needle valve) not properly seating, and its secondary release control (the plug at the end of the tubing from the body bleed) failing because the ferrule, which would have engaged the compression of the fitting, was not installed during new construction. Additionally, station repairs were completed before restart was required under normal operating procedures. Plains has since replaced the valve and tubing associated to prevent future releases. Supplemental narrative: update was made to part b, q5-county or parish.

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