HL incident on 2019-07-16 — PA

Operator
Mipc Llc
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300,000
Incident datetime
2019-07-16 10:30
Report number
Location
PA
Narrative
On 7/16/19 at 1030 hours, employees and contractors at mipc were walking down the work scope for a project involving the aboveground storage tanks at mipc's chelsea tank farm. During the walk down an employee observed an odor around the base of tank 711. There was no product visible on the ground. Tank 711 was safely emptied and taken out of service in preparation for an API std 653 out-of-service inspection on august 28, 2019. The API inspection report received on september 17, 2019, found that tank 711 had four (4) product stains from the bottom welds. Those four (4) stains were vacuum box leak tested and only one (1) stain leaked and was at the bottom to shell weld. Tank 711 remains out of service until a permanent repair is made. Updated the report to include a cost estimate for repairing tank 711 that's budgeted for 2022. The accident report will be updated after final costs are determined.
Detailed record list
Report Received Date
2019-08-15 00:00:00
Iyear
2019
Report Number
20190256
Supplemental Number
35953
Report Type
Supplemental Final
Operator Id
Name
Mipc Llc
Operator Street Address
920 Cherry Tree Road
Operator City Name
Aston
Operator State Abbreviation
PA
Operator Postal Code
19014
Local Datetime
2019-07-16 10:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.4
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-16 10:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Remaining Product In Tank 711 Was Safely Transferred To Other Tanks.
On Site Datetime
2019-07-16 10:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Chelsea Tank Farm
Segment Name
Tank 711
Onshore State Abbreviation
Pa
Onshore Postal Code
19014
Onshore City Name
Aston
Onshore County Name
Delaware
Designated Location
Milepost/valve Station
Designated Name
Chelsea
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Api Std Out Of Service Year
2004
Api Std In Service Year
2018
Installation Year
1955
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
300000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
300000
Accident Psig
0
Mop Psig
0.25
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control room's actions did not cause or contribute to this accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Other Corrosion Ind
Yes
Corrosion Type Details
Soilside Corrosion
Field Exam Basis Ind
Yes
Other Basis Ind
Yes
Corrosion Basis Details
Vacuum Box Testing And Magnetic Flux Leakage (Mfl) Scanning Was Conducted.
Underground Location
No
Externally Coated
No
Prior Damage
No
Preparer Name
J*** B****
Preparer Title
Pipeline Safety Lead
Preparer Email
J*********@m************.com
Preparer Telephone
484-816-3303
Prepared Date
2021-11-03 00:00:00
Authorizer Name
C******** S*******
Authorizer Telephone
610-364-8187
Authorizer Title
Vice President And General Manager
Authorizer Email
C*************@m************.com
Narrative
On 7/16/19 at 1030 hours, employees and contractors at mipc were walking down the work scope for a project involving the aboveground storage tanks at mipc's chelsea tank farm. During the walk down an employee observed an odor around the base of tank 711. There was no product visible on the ground. Tank 711 was safely emptied and taken out of service in preparation for an API std 653 out-of-service inspection on august 28, 2019. The API inspection report received on september 17, 2019, found that tank 711 had four (4) product stains from the bottom welds. Those four (4) stains were vacuum box leak tested and only one (1) stain leaked and was at the bottom to shell weld. Tank 711 remains out of service until a permanent repair is made. Updated the report to include a cost estimate for repairing tank 711 that's budgeted for 2022. The accident report will be updated after final costs are determined.
Report Received Date 2019-08-15 00:00:00
Iyear 2019
Report Number 20190256
Supplemental Number 35953
Report Type Supplemental Final
Operator Id 38922 PHMSA Enforcement
Name Mipc Llc
Operator Street Address 920 Cherry Tree Road
Operator City Name Aston
Operator State Abbreviation PA
Operator Postal Code 19014
Local Datetime 2019-07-16 10:30:00
Location Latitude 39.86388889 Google Maps OpenStreetMap
Location Longitude -75.455 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.4
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-07-16 10:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Remaining Product In Tank 711 Was Safely Transferred To Other Tanks.
On Site Datetime 2019-07-16 10:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Chelsea Tank Farm
Segment Name Tank 711
Onshore State Abbreviation Pa
Onshore Postal Code 19014
Onshore City Name Aston
Onshore County Name Delaware
Designated Location Milepost/valve Station
Designated Name Chelsea
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Single Bottom System
Tank Type Atmospheric
Api Std Out Of Service Year 2004
Api Std In Service Year 2018
Installation Year 1955
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 300000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 300000
Accident Psig 0
Mop Psig 0.25
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control room's actions did not cause or contribute to this accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Microbiological Corrosion Ind Yes
Other Corrosion Ind Yes
Corrosion Type Details Soilside Corrosion
Field Exam Basis Ind Yes
Other Basis Ind Yes
Corrosion Basis Details Vacuum Box Testing And Magnetic Flux Leakage (Mfl) Scanning Was Conducted.
Underground Location No
Externally Coated No
Prior Damage No
Preparer Name J*** B****
Preparer Title Pipeline Safety Lead
Preparer Email J*********@m************.com
Preparer Telephone 484-816-3303
Prepared Date 2021-11-03 00:00:00
Authorizer Name C******** S*******
Authorizer Telephone 610-364-8187
Authorizer Title Vice President And General Manager
Authorizer Email C*************@m************.com
Narrative On 7/16/19 at 1030 hours, employees and contractors at mipc were walking down the work scope for a project involving the aboveground storage tanks at mipc's chelsea tank farm. During the walk down an employee observed an odor around the base of tank 711. There was no product visible on the ground. Tank 711 was safely emptied and taken out of service in preparation for an API std 653 out-of-service inspection on august 28, 2019. The API inspection report received on september 17, 2019, found that tank 711 had four (4) product stains from the bottom welds. Those four (4) stains were vacuum box leak tested and only one (1) stain leaked and was at the bottom to shell weld. Tank 711 remains out of service until a permanent repair is made. Updated the report to include a cost estimate for repairing tank 711 that's budgeted for 2022. The accident report will be updated after final costs are determined.

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