HL incident on 2019-07-16 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$150,000
Incident datetime
2019-07-16 13:14
Report number
Location
TX
Narrative
On 07/16/2019 at 13:14 local time during a routine station inspection an enterprise technician discovered 10 bbls of crude oil on the ground near manifold a at the cushing west terminal. Based on field investigation, the leak was determined to be associated with tank #41122 transfer line and caused by internal corrosion. The line has now been abandoned. Initial call to nrc was made on 7/16/2019 at 13:50 local time (nrc#1252155). The call was made based on repair cost estimates exceeding $50,000. 48 hour update call to nrc was made on 7/18/2019 at 12:12 local time (nrc#1252373).
Detailed record list
Report Received Date
2019-08-13 00:00:00
Iyear
2019
Report Number
20190254
Supplemental Number
36134
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-07-16 13:14:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-16 13:14:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Asset Was Already Out Of Operation.
On Site Datetime
2019-07-16 13:14:00
Nrc Rpt Datetime
2019-07-16 13:50:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing West Station
Segment Name
Tank #41122 Transfer Line
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Okxx0738
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.177
Pipe Smys
Unknown
Pipe Specification
Api 5l
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2011
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
150000
Est Cost Emergency
35000
Est Cost Environmental
40000
Est Cost Other
0
Prpty
225000
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R*** T********
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2021-12-15 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Compliance Manager
Authorizer Email
S******@e****.com
Narrative
On 07/16/2019 at 13:14 local time during a routine station inspection an enterprise technician discovered 10 bbls of crude oil on the ground near manifold a at the cushing west terminal. Based on field investigation, the leak was determined to be associated with tank #41122 transfer line and caused by internal corrosion. The line has now been abandoned. Initial call to nrc was made on 7/16/2019 at 13:50 local time (nrc#1252155). The call was made based on repair cost estimates exceeding $50,000. 48 hour update call to nrc was made on 7/18/2019 at 12:12 local time (nrc#1252373).
Report Received Date 2019-08-13 00:00:00
Iyear 2019
Report Number 20190254
Supplemental Number 36134
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-07-16 13:14:00
Location Latitude 35.9515 Google Maps OpenStreetMap
Location Longitude -96.7597 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 10
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-07-16 13:14:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Asset Was Already Out Of Operation.
On Site Datetime 2019-07-16 13:14:00
Nrc Rpt Datetime 2019-07-16 13:50:00
Nrc Rpt Num 1252155 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing West Station
Segment Name Tank #41122 Transfer Line
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Okxx0738
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness 0.177
Pipe Smys Unknown
Pipe Specification Api 5l
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2011
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 150000
Est Cost Emergency 35000
Est Cost Environmental 40000
Est Cost Other 0
Prpty 225000
Accident Psig 15
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R*** T********
Preparer Title Pipeline Compliance Engineer
Preparer Email R*********@e****.com
Preparer Telephone 713-381-4659
Prepared Date 2021-12-15 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Compliance Manager
Authorizer Email S******@e****.com
Narrative On 07/16/2019 at 13:14 local time during a routine station inspection an enterprise technician discovered 10 bbls of crude oil on the ground near manifold a at the cushing west terminal. Based on field investigation, the leak was determined to be associated with tank #41122 transfer line and caused by internal corrosion. The line has now been abandoned. Initial call to nrc was made on 7/16/2019 at 13:50 local time (nrc#1252155). The call was made based on repair cost estimates exceeding $50,000. 48 hour update call to nrc was made on 7/18/2019 at 12:12 local time (nrc#1252373).

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