HL incident on 2019-07-17 — TX

Operator
Centurion Pipeline L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-07-17 11:52
Report number
Location
TX
Narrative
On july 17, 2019, at centurion pipeline (cpl) wasson station in yoakum county, texas, at 11:52 am, a station sump overflowed following a normal operations activity. Following an accident investigation it was determined that the sump, when approaching the fill level, unexpectedly released an air pocket. This release pushed oil out of the sump through the aboveground fill pot with some oil reaching the ground. The investigation concluded that installing a check valve between the sump and the fill pot will prevent future flow from the sump to the fill pot, hence preventing future overflows. Following the investigation a check valve was installed. Sumps across cpl's system are monitored for fill levels so any future events will be contained within the respective sump. High sump levels will shut stations down, hence preventing future similar events. One half barrel of oil reached the ground, all of which was recovered. No employees were injured and no other damages occurred.
Detailed record list
Report Received Date
2019-08-13 00:00:00
Iyear
2019
Report Number
20190253
Supplemental Number
32696
Report Type
Supplemental Final
Operator Id
Name
Centurion Pipeline L.p.
Operator Street Address
5 Greenway Plaza, Suite 1600
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046-7570
Local Datetime
2019-07-19 11:52:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-17 11:52:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-07-17 11:52:00
Restart Datetime
2019-07-17 14:41:00
On Site Datetime
2019-07-17 11:52:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wasson Station
Segment Name
Wasson Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79072
Onshore City Name
Wasson
Onshore County Name
Yoakum
Designated Location
Milepost/valve Station
Designated Name
Sump Piping
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
0
Est Cost Emergency
500
Est Cost Environmental
2500
Est Cost Other
0
Prpty
3030
Accident Psig
96
Mop Psig
385
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No abnormal operating conditions existed at the time of the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Inadequate Monitoring
Related Other Ind
Yes
Operation Related Details
No High Level Alarm To Shut Down Fill Of Sump.
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
D**** N*****
Preparer Title
Risk Engineer
Preparer Email
D***********@c**********.com
Preparer Telephone
346-803-2688
Prepared Date
2019-09-12 00:00:00
Authorizer Name
D**** M****
Authorizer Telephone
346-803-2680
Authorizer Title
Senior Pipeline Compliance Consultant
Authorizer Email
D**********@c**********.com
Narrative
On july 17, 2019, at centurion pipeline (cpl) wasson station in yoakum county, texas, at 11:52 am, a station sump overflowed following a normal operations activity. Following an accident investigation it was determined that the sump, when approaching the fill level, unexpectedly released an air pocket. This release pushed oil out of the sump through the aboveground fill pot with some oil reaching the ground. The investigation concluded that installing a check valve between the sump and the fill pot will prevent future flow from the sump to the fill pot, hence preventing future overflows. Following the investigation a check valve was installed. Sumps across cpl's system are monitored for fill levels so any future events will be contained within the respective sump. High sump levels will shut stations down, hence preventing future similar events. One half barrel of oil reached the ground, all of which was recovered. No employees were injured and no other damages occurred.
Report Received Date 2019-08-13 00:00:00
Iyear 2019
Report Number 20190253
Supplemental Number 32696
Report Type Supplemental Final
Operator Id 31888 PHMSA Enforcement
Name Centurion Pipeline L.p.
Operator Street Address 5 Greenway Plaza, Suite 1600
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046-7570
Local Datetime 2019-07-19 11:52:00
Location Latitude 32.987609 Google Maps OpenStreetMap
Location Longitude -102.77071 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-07-17 11:52:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-07-17 11:52:00
Restart Datetime 2019-07-17 14:41:00
On Site Datetime 2019-07-17 11:52:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wasson Station
Segment Name Wasson Station
Onshore State Abbreviation Tx
Onshore Postal Code 79072
Onshore City Name Wasson
Onshore County Name Yoakum
Designated Location Milepost/valve Station
Designated Name Sump Piping
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 0
Est Cost Emergency 500
Est Cost Environmental 2500
Est Cost Other 0
Prpty 3030
Accident Psig 96
Mop Psig 385
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No abnormal operating conditions existed at the time of the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Inadequate Monitoring
Related Other Ind Yes
Operation Related Details No High Level Alarm To Shut Down Fill Of Sump.
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name D**** N*****
Preparer Title Risk Engineer
Preparer Email D***********@c**********.com
Preparer Telephone 346-803-2688
Prepared Date 2019-09-12 00:00:00
Authorizer Name D**** M****
Authorizer Telephone 346-803-2680
Authorizer Title Senior Pipeline Compliance Consultant
Authorizer Email D**********@c**********.com
Narrative On july 17, 2019, at centurion pipeline (cpl) wasson station in yoakum county, texas, at 11:52 am, a station sump overflowed following a normal operations activity. Following an accident investigation it was determined that the sump, when approaching the fill level, unexpectedly released an air pocket. This release pushed oil out of the sump through the aboveground fill pot with some oil reaching the ground. The investigation concluded that installing a check valve between the sump and the fill pot will prevent future flow from the sump to the fill pot, hence preventing future overflows. Following the investigation a check valve was installed. Sumps across cpl's system are monitored for fill levels so any future events will be contained within the respective sump. High sump levels will shut stations down, hence preventing future similar events. One half barrel of oil reached the ground, all of which was recovered. No employees were injured and no other damages occurred.

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