HL incident on 2019-07-15 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-07-15 20:10
Report number
Location
TX
Narrative
Enterprise employee was making rounds and discovered approximately 15 gallons of crude oil on the ground that had leaked from a 3/8 inch body bleed on a fill line valve. The bleed valve had not been operated since installation. The body bleed showed no signs of damage and no additional leaks after it was closed.An investigation found no determinable cause. All body bleeds within tank farm were inspected. All remediation was completed.
Detailed record list
Report Received Date
2019-08-13 00:00:00
Iyear
2019
Report Number
20190252
Supplemental Number
33200
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-07-15 20:10:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Recovered Bbls
0.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-15 20:10:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Closed
On Site Datetime
2019-07-15 20:10:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Midland Tank Farm
Segment Name
M2s Manifold
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Midland
Onshore County Name
Midland
Designated Location
Milepost/valve Station
Designated Name
M2s Manifold
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2019
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Valve Opened Slightly
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
0
Est Cost Emergency
800
Est Cost Environmental
0
Est Cost Other
0
Prpty
820
Accident Psig
30
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room played no role in accident cause or discovery
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Unable To Determine If Debris Or Manufacturing Issue
Eq Additional Other Ind
Yes
Eq Additional Other Details
Unable To Determine If Debris Or Manufacturing Issue
Preparer Name
D**** B*****
Preparer Title
Compliance Engineer
Preparer Email
D*******@e****.com
Preparer Telephone
713-381-5647
Prepared Date
2020-01-17 00:00:00
Authorizer Name
D**** B*****
Authorizer Telephone
713-381-5647
Authorizer Title
Compliance Engineer
Authorizer Email
D*******@e****.com
Narrative
Enterprise employee was making rounds and discovered approximately 15 gallons of crude oil on the ground that had leaked from a 3/8 inch body bleed on a fill line valve. The bleed valve had not been operated since installation. The body bleed showed no signs of damage and no additional leaks after it was closed.An investigation found no determinable cause. All body bleeds within tank farm were inspected. All remediation was completed.
Report Received Date 2019-08-13 00:00:00
Iyear 2019
Report Number 20190252
Supplemental Number 33200
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-07-15 20:10:00
Location Latitude 32.021 Google Maps OpenStreetMap
Location Longitude -102.0157 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.36
Recovered Bbls 0.36
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2019-07-15 20:10:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Valve Was Closed
On Site Datetime 2019-07-15 20:10:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Midland Tank Farm
Segment Name M2s Manifold
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Midland
Onshore County Name Midland
Designated Location Milepost/valve Station
Designated Name M2s Manifold
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2019
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Other
Leak Type Other Valve Opened Slightly
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 0
Est Cost Emergency 800
Est Cost Environmental 0
Est Cost Other 0
Prpty 820
Accident Psig 30
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room played no role in accident cause or discovery
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Unable To Determine If Debris Or Manufacturing Issue
Eq Additional Other Ind Yes
Eq Additional Other Details Unable To Determine If Debris Or Manufacturing Issue
Preparer Name D**** B*****
Preparer Title Compliance Engineer
Preparer Email D*******@e****.com
Preparer Telephone 713-381-5647
Prepared Date 2020-01-17 00:00:00
Authorizer Name D**** B*****
Authorizer Telephone 713-381-5647
Authorizer Title Compliance Engineer
Authorizer Email D*******@e****.com
Narrative Enterprise employee was making rounds and discovered approximately 15 gallons of crude oil on the ground that had leaked from a 3/8 inch body bleed on a fill line valve. The bleed valve had not been operated since installation. The body bleed showed no signs of damage and no additional leaks after it was closed.An investigation found no determinable cause. All body bleeds within tank farm were inspected. All remediation was completed.

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