HL incident on 2019-07-11 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-07-11 05:30
Report number
Location
TX
Narrative
On 07/11/19 at 5:30 am terminal operator found a leak had been identified on the pressure relief valve piping on tank 65 at the carteret terminal. Tank 65 contained gasoline at the time of the incident. Quantity released was 25 barrels of gas. Kinder morgan's terminal maintenance team and remediation contractors worked together to repair the tank and remediate the dike area. The failed pressure relief line has been replaced and tank 65 is back in service. 48 hour nrc #: 1251776. Due to the long term assessment for soil remediation, the costs are an estimate. If, after the assessment is completed the costs are significantly different to the estimate a supplemental report shall be submitted. 04/09/2025 - updated by PHMSA per operator approval.
Detailed record list
Report Received Date
2019-08-09 00:00:00
Iyear
2019
Report Number
20190246
Supplemental Number
32849
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-07-11 05:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
25
Recovered Bbls
25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2019-07-11 05:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Not Being Used At The Time Of The Incident.
On Site Datetime
2019-07-11 05:35:00
Nrc Rpt Datetime
2019-07-11 14:03:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Carteret Terminal
Segment Name
Tank 65
Onshore State Abbreviation
Nj
Onshore Postal Code
07008
Onshore City Name
Carteret
Onshore County Name
Middlesex
Designated Location
Milepost/valve Station
Designated Name
In Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Relief Valve
Tank Type
Atmospheric
Installation Year
1942
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0.01
Rel Water Name
Groundwater
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
19651
Est Cost Environmental
206936
Est Cost Other
0
Prpty
226587
Accident Psig
16.7
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The tank was not being operated by the control room at the time of the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Vibration Ind
Yes
Preparer Name
D******* S*******
Preparer Title
Director Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
7137250147
Prepared Date
2019-10-18 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
7137250147
Authorizer Title
Director Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On 07/11/19 at 5:30 am terminal operator found a leak had been identified on the pressure relief valve piping on tank 65 at the carteret terminal. Tank 65 contained gasoline at the time of the incident. Quantity released was 25 barrels of gas. Kinder morgan's terminal maintenance team and remediation contractors worked together to repair the tank and remediate the dike area. The failed pressure relief line has been replaced and tank 65 is back in service. 48 hour nrc #: 1251776. Due to the long term assessment for soil remediation, the costs are an estimate. If, after the assessment is completed the costs are significantly different to the estimate a supplemental report shall be submitted. 04/09/2025 - updated by PHMSA per operator approval.
Report Received Date 2019-08-09 00:00:00
Iyear 2019
Report Number 20190246
Supplemental Number 32849
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-07-11 05:30:00
Location Latitude 40.583972 Google Maps OpenStreetMap
Location Longitude -74.211946 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 25
Recovered Bbls 25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2019-07-11 05:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Was Not Being Used At The Time Of The Incident.
On Site Datetime 2019-07-11 05:35:00
Nrc Rpt Datetime 2019-07-11 14:03:00
Nrc Rpt Num 1251636 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Carteret Terminal
Segment Name Tank 65
Onshore State Abbreviation Nj
Onshore Postal Code 07008
Onshore City Name Carteret
Onshore County Name Middlesex
Designated Location Milepost/valve Station
Designated Name In Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Relief Valve
Tank Type Atmospheric
Installation Year 1942
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0.01
Rel Water Name Groundwater
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 19651
Est Cost Environmental 206936
Est Cost Other 0
Prpty 226587
Accident Psig 16.7
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The tank was not being operated by the control room at the time of the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Vibration Ind Yes
Preparer Name D******* S*******
Preparer Title Director Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 7137250147
Prepared Date 2019-10-18 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 7137250147
Authorizer Title Director Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On 07/11/19 at 5:30 am terminal operator found a leak had been identified on the pressure relief valve piping on tank 65 at the carteret terminal. Tank 65 contained gasoline at the time of the incident. Quantity released was 25 barrels of gas. Kinder morgan's terminal maintenance team and remediation contractors worked together to repair the tank and remediate the dike area. The failed pressure relief line has been replaced and tank 65 is back in service. 48 hour nrc #: 1251776. Due to the long term assessment for soil remediation, the costs are an estimate. If, after the assessment is completed the costs are significantly different to the estimate a supplemental report shall be submitted. 04/09/2025 - updated by PHMSA per operator approval.

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