HL incident on 2019-07-08 — WY

Operator
Bridger Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,962
Incident datetime
2019-07-08 12:45
Report number
Location
WY
Narrative
On august 8, 2019 a gasket failure on the downstream flange of regulated rural gathering 8" line from marmarth station to baker station occurred. A third party truck driver notified the company of the incident. Operator personnel and controllers worked together to get the pipeline shut in and isolated. The gasket was investigated for cause and no defects or misalignments were noted. A small piece of the gasket was missing between the five and six o'clock positions. The worn gasket was removed and then replaced with a new gasket.
Detailed record list
Report Received Date
2019-08-07 00:00:00
Iyear
2019
Report Number
20190245
Supplemental Number
32593
Report Type
Supplemental Final
Operator Id
Name
Bridger Pipeline Llc
Operator Street Address
455 N. Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82602
Local Datetime
2019-07-08 12:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Truck Driver
Incident Identified Datetime
2019-07-08 12:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-07-08 01:30:00
Restart Datetime
2019-07-08 19:00:00
On Site Datetime
2019-07-08 12:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Marmarth Station
Segment Name
Bowman Gathering
Onshore State Abbreviation
Nd
Onshore Postal Code
58643
Onshore City Name
Not Within A Municipality
Onshore County Name
Bowman
Designated Location
Milepost/valve Station
Designated Name
Marmarth
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Gasket
Installation Year
2012
Material Involved
Material Other Than Carbon Steel
Material Details
Paper Gasket Failure
Release Type
Other
Release Type Details
Gasket Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
10962
Est Cost Emergency
8296
Est Cost Environmental
5000
Est Cost Other
0
Prpty
24758
Accident Psig
1053
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
After trending the pipeline pressures it was determined that an over-pressure did not occur. Due to the small volume and the location of the leak the controller would not have reasonably been expected to see the leak. The controller did an excellent job getting things shut in/shutdown and working with field personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Eq Additional Other Ind
Yes
Eq Additional Other Details
Worn Gasket
Preparer Name
J**** R*********
Preparer Title
Compliance Coordinator
Preparer Email
J***************@t******.com
Preparer Telephone
3072660250
Prepared Date
2019-08-22 00:00:00
Authorizer Name
J**** R*********
Authorizer Telephone
3072660250
Authorizer Title
Compliance Coordinator
Authorizer Email
J***************@t******.com
Narrative
On august 8, 2019 a gasket failure on the downstream flange of regulated rural gathering 8" line from marmarth station to baker station occurred. A third party truck driver notified the company of the incident. Operator personnel and controllers worked together to get the pipeline shut in and isolated. The gasket was investigated for cause and no defects or misalignments were noted. A small piece of the gasket was missing between the five and six o'clock positions. The worn gasket was removed and then replaced with a new gasket.
Report Received Date 2019-08-07 00:00:00
Iyear 2019
Report Number 20190245
Supplemental Number 32593
Report Type Supplemental Final
Operator Id 31878 PHMSA Enforcement
Name Bridger Pipeline Llc
Operator Street Address 455 N. Poplar St.
Operator City Name Casper
Operator State Abbreviation WY
Operator Postal Code 82602
Local Datetime 2019-07-08 12:45:00
Location Latitude 46.191125 Google Maps OpenStreetMap
Location Longitude -103.952295 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Recovered Bbls 3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Truck Driver
Incident Identified Datetime 2019-07-08 12:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-07-08 01:30:00
Restart Datetime 2019-07-08 19:00:00
On Site Datetime 2019-07-08 12:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Marmarth Station
Segment Name Bowman Gathering
Onshore State Abbreviation Nd
Onshore Postal Code 58643
Onshore City Name Not Within A Municipality
Onshore County Name Bowman
Designated Location Milepost/valve Station
Designated Name Marmarth
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Gasket
Installation Year 2012
Material Involved Material Other Than Carbon Steel
Material Details Paper Gasket Failure
Release Type Other
Release Type Details Gasket Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 10962
Est Cost Emergency 8296
Est Cost Environmental 5000
Est Cost Other 0
Prpty 24758
Accident Psig 1053
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details After trending the pipeline pressures it was determined that an over-pressure did not occur. Due to the small volume and the location of the leak the controller would not have reasonably been expected to see the leak. The controller did an excellent job getting things shut in/shutdown and working with field personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Eq Additional Other Ind Yes
Eq Additional Other Details Worn Gasket
Preparer Name J**** R*********
Preparer Title Compliance Coordinator
Preparer Email J***************@t******.com
Preparer Telephone 3072660250
Prepared Date 2019-08-22 00:00:00
Authorizer Name J**** R*********
Authorizer Telephone 3072660250
Authorizer Title Compliance Coordinator
Authorizer Email J***************@t******.com
Narrative On august 8, 2019 a gasket failure on the downstream flange of regulated rural gathering 8" line from marmarth station to baker station occurred. A third party truck driver notified the company of the incident. Operator personnel and controllers worked together to get the pipeline shut in and isolated. The gasket was investigated for cause and no defects or misalignments were noted. A small piece of the gasket was missing between the five and six o'clock positions. The worn gasket was removed and then replaced with a new gasket.

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