HL incident on 2019-07-04 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100,790
Incident datetime
2019-07-04 22:30
Report number
Location
TX
Narrative
On july 4, 2019 at 9:50 pm cdt, the on call technician was dispatched by the edmonton control center to the floodwood line 4 station due to a gas alarm. While the technician was en route to the station, the control center received another gas alarm, initiating the line 4 shut down at 10:03 pm cdt. Upon arriving at the station at 10:30 pm cdt, the technician confirmed oil on the pump room floor and the interior walls of the building. Additional personnel were dispatched to assist with clean up. It was discovered that the source of the crude oil was a pinhole leak on the 1/2" tubing on the line 4 unit 2 pump. The nrc was notified on july 5, 2019 at 2:13 pm cdt (#1251072) after the unit 2 motor was found to have oil inside the housing unit and the costs were estimated to exceed the nrc reporting threshold to clean and repair the motor. A 48-hour update was made to the nrc on july 7, 2019 at 8:23 am cdt (#1251215). The pump is currently locked out until the motor is cleaned and the piping replaced. Approximately three cubic yards of contaminated soil has been properly disposed of. A third-party metallurgical analysis determined that the failure was due to mechanical damage to the 1/2" tubing, at an unknown previous time, causing a protrusion into the tube. Eventually the tubing failed at the protrusion. The motor was sent in for an overall cleaning and the pump is in the process of being rebuilt. The unit will be placed back into service once all parts have been prepared for assembly.
Detailed record list
Report Received Date
2019-08-02 00:00:00
Iyear
2019
Report Number
20190242
Supplemental Number
33242
Report Type
Supplemental Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2019-07-04 21:50:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6.7
Recovered Bbls
6.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2019-07-04 22:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-07-04 22:03:00
Restart Datetime
2019-07-05 04:17:00
On Site Datetime
2019-07-04 22:30:00
Nrc Rpt Datetime
2019-07-05 14:13:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Floodwood Station
Segment Name
Line 4 Unit 2
Onshore State Abbreviation
Mn
Onshore Postal Code
55736
Onshore City Name
Floodwood
Onshore County Name
St. Louis
Designated Location
Milepost/valve Station
Designated Name
1044
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
1970
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
382
Est Cost Prop Damage
100790
Est Cost Emergency
124
Est Cost Environmental
2500
Est Cost Other
0
Prpty
103796
Accident Psig
727
Mop Psig
879
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Actions from the operator would not have had an impact on the event
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
Mechanical Damage
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2020-01-28 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On july 4, 2019 at 9:50 pm cdt, the on call technician was dispatched by the edmonton control center to the floodwood line 4 station due to a gas alarm. While the technician was en route to the station, the control center received another gas alarm, initiating the line 4 shut down at 10:03 pm cdt. Upon arriving at the station at 10:30 pm cdt, the technician confirmed oil on the pump room floor and the interior walls of the building. Additional personnel were dispatched to assist with clean up. It was discovered that the source of the crude oil was a pinhole leak on the 1/2" tubing on the line 4 unit 2 pump. The nrc was notified on july 5, 2019 at 2:13 pm cdt (#1251072) after the unit 2 motor was found to have oil inside the housing unit and the costs were estimated to exceed the nrc reporting threshold to clean and repair the motor. A 48-hour update was made to the nrc on july 7, 2019 at 8:23 am cdt (#1251215). The pump is currently locked out until the motor is cleaned and the piping replaced. Approximately three cubic yards of contaminated soil has been properly disposed of. A third-party metallurgical analysis determined that the failure was due to mechanical damage to the 1/2" tubing, at an unknown previous time, causing a protrusion into the tube. Eventually the tubing failed at the protrusion. The motor was sent in for an overall cleaning and the pump is in the process of being rebuilt. The unit will be placed back into service once all parts have been prepared for assembly.
Report Received Date 2019-08-02 00:00:00
Iyear 2019
Report Number 20190242
Supplemental Number 33242
Report Type Supplemental Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2019-07-04 21:50:00
Location Latitude 46.93887 Google Maps OpenStreetMap
Location Longitude -92.938287 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6.7
Recovered Bbls 6.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2019-07-04 22:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-07-04 22:03:00
Restart Datetime 2019-07-05 04:17:00
On Site Datetime 2019-07-04 22:30:00
Nrc Rpt Datetime 2019-07-05 14:13:00
Nrc Rpt Num 1251072 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Floodwood Station
Segment Name Line 4 Unit 2
Onshore State Abbreviation Mn
Onshore Postal Code 55736
Onshore City Name Floodwood
Onshore County Name St. Louis
Designated Location Milepost/valve Station
Designated Name 1044
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year 1970
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 382
Est Cost Prop Damage 100790
Est Cost Emergency 124
Est Cost Environmental 2500
Est Cost Other 0
Prpty 103796
Accident Psig 727
Mop Psig 879
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Actions from the operator would not have had an impact on the event
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details Mechanical Damage
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2020-01-28 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On july 4, 2019 at 9:50 pm cdt, the on call technician was dispatched by the edmonton control center to the floodwood line 4 station due to a gas alarm. While the technician was en route to the station, the control center received another gas alarm, initiating the line 4 shut down at 10:03 pm cdt. Upon arriving at the station at 10:30 pm cdt, the technician confirmed oil on the pump room floor and the interior walls of the building. Additional personnel were dispatched to assist with clean up. It was discovered that the source of the crude oil was a pinhole leak on the 1/2" tubing on the line 4 unit 2 pump. The nrc was notified on july 5, 2019 at 2:13 pm cdt (#1251072) after the unit 2 motor was found to have oil inside the housing unit and the costs were estimated to exceed the nrc reporting threshold to clean and repair the motor. A 48-hour update was made to the nrc on july 7, 2019 at 8:23 am cdt (#1251215). The pump is currently locked out until the motor is cleaned and the piping replaced. Approximately three cubic yards of contaminated soil has been properly disposed of. A third-party metallurgical analysis determined that the failure was due to mechanical damage to the 1/2" tubing, at an unknown previous time, causing a protrusion into the tube. Eventually the tubing failed at the protrusion. The motor was sent in for an overall cleaning and the pump is in the process of being rebuilt. The unit will be placed back into service once all parts have been prepared for assembly.

All rights reserved. Copyright © by ClearPHMSA