HL incident on 2019-07-02 — TX

Operator
Oryx Delaware Oil Transport Llc
Cause
Locating Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2019-07-02 12:40
Report number
Location
TX
Narrative
On july 2nd, 2019 at 12:40pm, excavator was contracted to drill a 30" diameter hole for a pipeline support pier for a 30" line tie in. The proposed drill depth was 6'. At 4' the excavator felt resistance in the drill, stopped drilling and pulled out of the hole. The excavator witnessed oil collecting in the hole and notified construction inspector of the incident. The pipe was then isolated and soil remediation contractor was then dispatched to the location. The contributing factor to the incident was an improper response to the subsequent one call tickets and the resultant failure to mark the lines within the facility. Corrective action: oryx damage prevention department held a safety stand down with all 3rd party line locators that work for oryx midstream to discuss the incident, proper response to one call tickets and to improve communication with excavators or construction project managers.
Detailed record list
Report Received Date
2019-07-31 00:00:00
Iyear
2019
Report Number
20190237
Supplemental Number
32489
Report Type
Original Final
Operator Id
Name
Oryx Delaware Oil Transport Llc
Operator Street Address
333 Clay St. Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-07-02 13:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.24
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2019-07-02 12:40:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The In Station Meter Prover Was Not In Operation During The Release.
On Site Datetime
2019-07-02 12:40:00
Nrc Rpt Datetime
2019-07-02 16:02:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Crane Ii Breakout Facility
Segment Name
Meter Prover Bypass
Onshore State Abbreviation
Tx
Onshore Postal Code
79731
Onshore City Name
Not Within A Municipality
Onshore County Name
Crane
Designated Location
Milepost/valve Station
Designated Name
Prover Bypass
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
1.2
Puncture Circum
1.2
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
15
Est Cost Prop Damage
10000
Est Cost Emergency
0
Est Cost Environmental
3500
Est Cost Other
0
Prpty
13515
Accident Psig
15
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
Yes
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Auger
Work Performed
Building Construction
One Call Notified Ind
Yes
One Call Ticket Num
1966104210
One Call Center Name
Texas 811
Locator Type
Contract Locator
Visible Marks
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Marked Inaccurately Due To Locator Error
Preparer Name
G****** H****
Preparer Title
Sr. Regulatory Compliance Specialist
Preparer Email
G******@o************.com
Preparer Telephone
4322542238
Prepared Date
2019-07-31 00:00:00
Authorizer Name
M***** M*****
Authorizer Telephone
4322537774
Authorizer Title
Cheif Operating Officer
Authorizer Email
M*****@o************.com
Narrative
On july 2nd, 2019 at 12:40pm, excavator was contracted to drill a 30" diameter hole for a pipeline support pier for a 30" line tie in. The proposed drill depth was 6'. At 4' the excavator felt resistance in the drill, stopped drilling and pulled out of the hole. The excavator witnessed oil collecting in the hole and notified construction inspector of the incident. The pipe was then isolated and soil remediation contractor was then dispatched to the location. The contributing factor to the incident was an improper response to the subsequent one call tickets and the resultant failure to mark the lines within the facility. Corrective action: oryx damage prevention department held a safety stand down with all 3rd party line locators that work for oryx midstream to discuss the incident, proper response to one call tickets and to improve communication with excavators or construction project managers.
Report Received Date 2019-07-31 00:00:00
Iyear 2019
Report Number 20190237
Supplemental Number 32489
Report Type Original Final
Operator Id 39654 PHMSA Enforcement
Name Oryx Delaware Oil Transport Llc
Operator Street Address 333 Clay St. Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-07-02 13:00:00
Location Latitude 31.426311 Google Maps OpenStreetMap
Location Longitude -102.449186 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.24
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2019-07-02 12:40:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The In Station Meter Prover Was Not In Operation During The Release.
On Site Datetime 2019-07-02 12:40:00
Nrc Rpt Datetime 2019-07-02 16:02:00
Nrc Rpt Num 1250867 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Crane Ii Breakout Facility
Segment Name Meter Prover Bypass
Onshore State Abbreviation Tx
Onshore Postal Code 79731
Onshore City Name Not Within A Municipality
Onshore County Name Crane
Designated Location Milepost/valve Station
Designated Name Prover Bypass
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year 2018
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 1.2
Puncture Circum 1.2
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 15
Est Cost Prop Damage 10000
Est Cost Emergency 0
Est Cost Environmental 3500
Est Cost Other 0
Prpty 13515
Accident Psig 15
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 1
Num Employees Failed 0
Num Contractors Tested 1
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt Yes
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Auger
Work Performed Building Construction
One Call Notified Ind Yes
One Call Ticket Num 1966104210
One Call Center Name Texas 811
Locator Type Contract Locator
Visible Marks No
Root Cause Category Locating Issue
Root Cause Type Facility Marked Inaccurately Due To Locator Error
Preparer Name G****** H****
Preparer Title Sr. Regulatory Compliance Specialist
Preparer Email G******@o************.com
Preparer Telephone 4322542238
Prepared Date 2019-07-31 00:00:00
Authorizer Name M***** M*****
Authorizer Telephone 4322537774
Authorizer Title Cheif Operating Officer
Authorizer Email M*****@o************.com
Narrative On july 2nd, 2019 at 12:40pm, excavator was contracted to drill a 30" diameter hole for a pipeline support pier for a 30" line tie in. The proposed drill depth was 6'. At 4' the excavator felt resistance in the drill, stopped drilling and pulled out of the hole. The excavator witnessed oil collecting in the hole and notified construction inspector of the incident. The pipe was then isolated and soil remediation contractor was then dispatched to the location. The contributing factor to the incident was an improper response to the subsequent one call tickets and the resultant failure to mark the lines within the facility. Corrective action: oryx damage prevention department held a safety stand down with all 3rd party line locators that work for oryx midstream to discuss the incident, proper response to one call tickets and to improve communication with excavators or construction project managers.

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