HL incident on 2019-06-21 — TX

Operator
Centurion Pipeline L.p.
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2019-06-21 21:30
Report number
Location
TX
Narrative
On june 21, 2019, at approximately 9:30 pm, a third party trucking reported a release at post station near post, texas, in garza county, texas to centurion pipeline company l.P. (cpl) . The release was from a quarter inch nipple failure. All oil was recovered with 1 barrel being recovered in liquid form while the remaining barrel was recovered through soil remediation. The nipple was replaced on june 21, 2019. No injuries, fatalities, or fires were associated with this accident. The root cause analysis of the failure has determined that high wind led to a utility cabinet falling onto the quarter inch nipple. The utility cabinet has been relocated away from the process and secured to prevent damage to the system during a high wind event.
Detailed record list
Report Received Date
2019-07-18 00:00:00
Iyear
2019
Report Number
20190225
Supplemental Number
32435
Report Type
Original Final
Operator Id
Name
Centurion Pipeline L.p.
Operator Street Address
5 Greenway Plaza, Suite 1600
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046-7570
Local Datetime
2019-06-21 21:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Trucking
Incident Identified Datetime
2019-06-21 21:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-06-21 21:30:00
Restart Datetime
2019-06-21 23:30:00
On Site Datetime
2019-06-21 22:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Post Station
Segment Name
Post Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Post
Onshore County Name
Garza
Designated Location
Milepost/valve Station
Designated Name
Piping
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
120
Est Cost Prop Damage
500
Est Cost Emergency
2000
Est Cost Environmental
6075
Est Cost Other
0
Prpty
8695
Accident Psig
38
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No abnormal operating conditions existed at the time of the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
High Winds
Natural Force Type
High Winds
Nf Other Details
,,,
Nf Extreme Weather Ind
No
Preparer Name
D**** N*****
Preparer Title
Risk Engineer
Preparer Email
D***********@c**********.com
Preparer Telephone
346-803-2688
Prepared Date
2019-07-18 00:00:00
Authorizer Name
D**** M****
Authorizer Telephone
346-803-2680
Authorizer Title
Senior Pipeline Compliance Consultant
Authorizer Email
D**********@c**********.com
Narrative
On june 21, 2019, at approximately 9:30 pm, a third party trucking reported a release at post station near post, texas, in garza county, texas to centurion pipeline company l.P. (cpl) . The release was from a quarter inch nipple failure. All oil was recovered with 1 barrel being recovered in liquid form while the remaining barrel was recovered through soil remediation. The nipple was replaced on june 21, 2019. No injuries, fatalities, or fires were associated with this accident. The root cause analysis of the failure has determined that high wind led to a utility cabinet falling onto the quarter inch nipple. The utility cabinet has been relocated away from the process and secured to prevent damage to the system during a high wind event.
Report Received Date 2019-07-18 00:00:00
Iyear 2019
Report Number 20190225
Supplemental Number 32435
Report Type Original Final
Operator Id 31888 PHMSA Enforcement
Name Centurion Pipeline L.p.
Operator Street Address 5 Greenway Plaza, Suite 1600
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046-7570
Local Datetime 2019-06-21 21:30:00
Location Latitude 33.152138 Google Maps OpenStreetMap
Location Longitude -101.37279 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Trucking
Incident Identified Datetime 2019-06-21 21:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-06-21 21:30:00
Restart Datetime 2019-06-21 23:30:00
On Site Datetime 2019-06-21 22:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Post Station
Segment Name Post Station
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Post
Onshore County Name Garza
Designated Location Milepost/valve Station
Designated Name Piping
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 120
Est Cost Prop Damage 500
Est Cost Emergency 2000
Est Cost Environmental 6075
Est Cost Other 0
Prpty 8695
Accident Psig 38
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No abnormal operating conditions existed at the time of the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details High Winds
Natural Force Type High Winds
Nf Other Details ,,,
Nf Extreme Weather Ind No
Preparer Name D**** N*****
Preparer Title Risk Engineer
Preparer Email D***********@c**********.com
Preparer Telephone 346-803-2688
Prepared Date 2019-07-18 00:00:00
Authorizer Name D**** M****
Authorizer Telephone 346-803-2680
Authorizer Title Senior Pipeline Compliance Consultant
Authorizer Email D**********@c**********.com
Narrative On june 21, 2019, at approximately 9:30 pm, a third party trucking reported a release at post station near post, texas, in garza county, texas to centurion pipeline company l.P. (cpl) . The release was from a quarter inch nipple failure. All oil was recovered with 1 barrel being recovered in liquid form while the remaining barrel was recovered through soil remediation. The nipple was replaced on june 21, 2019. No injuries, fatalities, or fires were associated with this accident. The root cause analysis of the failure has determined that high wind led to a utility cabinet falling onto the quarter inch nipple. The utility cabinet has been relocated away from the process and secured to prevent damage to the system during a high wind event.

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