HL incident on 2019-06-14 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$123,674
Incident datetime
2019-06-14 07:15
Report number
Location
TX
Narrative
On june 14, 2019 at 7:15 am cdt, an electrical technician completing morning rounds discovered approximately 3 gallons of crude oil near the line 65 unit 3 pump at the donaldson station. The unit 3 pump was not running at the time the release was discovered. The edmonton control center was contacted and the pump was isolated and locked out. Additional operations personnel were dispatched to investigate the source of the release and begin cleanup of the oil from the concrete pump room floor. Small diameter piping that was welded to the underside of the pump was found to be the source of the release. Once the repair plan was finalized on june 18, 2019 it was determined that the costs would exceed the nrc reporting threshold and an external notification to the nrc was made at 9:52 am cdt (#1249253). A 48-hour update was made to the nrc on june 20. 2019 at 8:10 am cdt (#1249485). In order to repair the small diameter piping and determine the cause of the failure, the entire pump was removed from the station and sent to sulzer for repair, cleaning, and analysis. Once the pump was disassembled and inspected, it was discovered that the cause of the release was due to internal corrosion/erosion within the pump case and balance line. When the cleaning of the pump is completed, the pump will be sent back to the donaldson station for installation. It is anticipated that the pump will be operational by the end of 2019.
Detailed record list
Report Received Date
2019-07-12 00:00:00
Iyear
2019
Report Number
20190223
Supplemental Number
32880
Report Type
Supplemental Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2019-06-14 07:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-06-14 07:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Unit 3 Pump Was Not Running At The Time Of The Release And Was Locked Out
On Site Datetime
2019-06-14 07:15:00
Nrc Rpt Datetime
2019-06-18 09:52:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Donaldson Station
Segment Name
Line 65 Unit 3
Onshore State Abbreviation
Mn
Onshore Postal Code
56720
Onshore City Name
Donaldson
Onshore County Name
Kittson
Designated Location
Milepost/valve Station
Designated Name
814
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1997
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
4
Est Cost Prop Damage
123674
Est Cost Emergency
124
Est Cost Environmental
0
Est Cost Other
0
Prpty
123802
Accident Psig
657
Mop Psig
1430
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement. Field identified release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Other
Int Visual Exam Details
Erosion By Fluid Wash
Int Erosion Ind
Yes
Int Field Exam Basis Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Elbow Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2019-10-30 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On june 14, 2019 at 7:15 am cdt, an electrical technician completing morning rounds discovered approximately 3 gallons of crude oil near the line 65 unit 3 pump at the donaldson station. The unit 3 pump was not running at the time the release was discovered. The edmonton control center was contacted and the pump was isolated and locked out. Additional operations personnel were dispatched to investigate the source of the release and begin cleanup of the oil from the concrete pump room floor. Small diameter piping that was welded to the underside of the pump was found to be the source of the release. Once the repair plan was finalized on june 18, 2019 it was determined that the costs would exceed the nrc reporting threshold and an external notification to the nrc was made at 9:52 am cdt (#1249253). A 48-hour update was made to the nrc on june 20. 2019 at 8:10 am cdt (#1249485). In order to repair the small diameter piping and determine the cause of the failure, the entire pump was removed from the station and sent to sulzer for repair, cleaning, and analysis. Once the pump was disassembled and inspected, it was discovered that the cause of the release was due to internal corrosion/erosion within the pump case and balance line. When the cleaning of the pump is completed, the pump will be sent back to the donaldson station for installation. It is anticipated that the pump will be operational by the end of 2019.
Report Received Date 2019-07-12 00:00:00
Iyear 2019
Report Number 20190223
Supplemental Number 32880
Report Type Supplemental Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2019-06-14 07:15:00
Location Latitude 48.573929 Google Maps OpenStreetMap
Location Longitude -96.935187 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-06-14 07:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Unit 3 Pump Was Not Running At The Time Of The Release And Was Locked Out
On Site Datetime 2019-06-14 07:15:00
Nrc Rpt Datetime 2019-06-18 09:52:00
Nrc Rpt Num 1249253 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Donaldson Station
Segment Name Line 65 Unit 3
Onshore State Abbreviation Mn
Onshore Postal Code 56720
Onshore City Name Donaldson
Onshore County Name Kittson
Designated Location Milepost/valve Station
Designated Name 814
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 1997
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 4
Est Cost Prop Damage 123674
Est Cost Emergency 124
Est Cost Environmental 0
Est Cost Other 0
Prpty 123802
Accident Psig 657
Mop Psig 1430
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement. Field identified release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Other
Int Visual Exam Details Erosion By Fluid Wash
Int Erosion Ind Yes
Int Field Exam Basis Ind Yes
Int Metallurgical Basis Ind Yes
Int Elbow Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2019-10-30 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On june 14, 2019 at 7:15 am cdt, an electrical technician completing morning rounds discovered approximately 3 gallons of crude oil near the line 65 unit 3 pump at the donaldson station. The unit 3 pump was not running at the time the release was discovered. The edmonton control center was contacted and the pump was isolated and locked out. Additional operations personnel were dispatched to investigate the source of the release and begin cleanup of the oil from the concrete pump room floor. Small diameter piping that was welded to the underside of the pump was found to be the source of the release. Once the repair plan was finalized on june 18, 2019 it was determined that the costs would exceed the nrc reporting threshold and an external notification to the nrc was made at 9:52 am cdt (#1249253). A 48-hour update was made to the nrc on june 20. 2019 at 8:10 am cdt (#1249485). In order to repair the small diameter piping and determine the cause of the failure, the entire pump was removed from the station and sent to sulzer for repair, cleaning, and analysis. Once the pump was disassembled and inspected, it was discovered that the cause of the release was due to internal corrosion/erosion within the pump case and balance line. When the cleaning of the pump is completed, the pump will be sent back to the donaldson station for installation. It is anticipated that the pump will be operational by the end of 2019.

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