Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2019-06-10 — TX
Operator
Centurion Pipeline L.p.
Cause
Notification Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$289,500
Incident datetime
2019-06-10 09:30
Report number
Location
TX
Narrative
On june 10, 2019, at approximately 9:30 am, a member of the public reported a release to centurion pipeline company l.P. (cpl) on a right of way near blair, oklahoma, in jackson county, oklahoma. Cpl shut down the pipeline at 9:39 am after confirming the release. Approximately 4201 barrels of crude oil were released. 1897 barrels of oil were recovered with 1741 barrels being recovered in liquid form while 156 barrels in soil have been moved to an offsite location for remediation. No injuries, fatalities, or fires were associated with this accident. The initial national response center (nrc) report number concerning this accident is 1248387. The 48 hour follow up call made to the nrc on june 12, 2019 has a reference number of 1248615. The root cause analysis of the failure has determined that a third party road grader struck the line leading to loss of containment. The pipeline has been repaired with a plidco split + sleeve, a commercially available bolt on split sleeve repair, and restarted the pipeline at 8:20 am on june 12, 2019. Environmental remediation is still underway and a supplemental report will be completed once remediation costs have been determined. Supplemental final report submitted october 10, 2019 permanent repairs to the pipeline were completed july 24, 2019. Approximately 20 feet of pipe was replaced with new API 5l, ps2l, x52 specification pipe. Remediation efforts were completed september 23, 2019. Part d, item 8 has been updated to include the final remediation estimate as well as the cost of the permanent repair.
Detailed record list
Report Received Date
2019-07-10 00:00:00
Iyear
2019
Report Number
20190221
Supplemental Number
32793
Report Type
Supplemental Final
Operator Id
31888
Name
Centurion Pipeline L.p.
Operator Street Address
5 Greenway Plaza, Suite 1600
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046-7570
Local Datetime
2019-06-10 09:20:00
Location Latitude
34.765475
Location Longitude
-99.32194444
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4201
Recovered Bbls
1897
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2019-06-10 09:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-06-10 09:39:00
Restart Datetime
2019-06-12 08:20:00
On Site Datetime
2019-06-10 10:15:00
Nrc Rpt Datetime
2019-06-10 10:20:00
Nrc Rpt Num
1248615
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Slaughter To Cushing System #1
Segment Name
Slaughter To Cushing System #1
Onshore State Abbreviation
Ok
Onshore Postal Code
73009
Onshore City Name
Blair
Onshore County Name
Jackson
Designated Location
Milepost/valve Station
Designated Name
179
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
14
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
16
Pipe Wall Thickness
0.25
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Other
Pipe Seam Details
Electric Fusion Welding (Efw)
Pipe Manufacturer
A.o. Smith
Pipe Coating Type
Composite
Installation Year
1944
Manufactured Year
1942
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
8
Puncture Circum
1
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
200000
Est Cost Gas Released
135300
Est Cost Prop Damage
289500
Est Cost Emergency
81000
Est Cost Environmental
884000
Est Cost Other
0
Prpty
1589800
Accident Psig
400
Mop Psig
715
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
84480
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Third party damage was the cause.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Easement
Excavator Type
Farmer
Excavator Equipment
Grader/scraper
Work Performed
Drainage
One Call Notified Ind
No
Service Interruption
Yes
Service Interruption Hours
44
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2017
Geometry Recent Year
2017
Other Recent Year
2017
Insp Compl Before Damage Ind
Yes
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2009
Hydrtst Most Rcnt Pressure
1010
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D**** N*****
Preparer Title
Risk Engineer
Preparer Email
D***********@c**********.com
Preparer Telephone
346-803-2688
Prepared Date
2019-10-09 00:00:00
Authorizer Name
D**** M****
Authorizer Telephone
346-803-2680
Authorizer Title
Senior Pipeline Compliance Consultant
Authorizer Email
D**********@c**********.com
Narrative
On june 10, 2019, at approximately 9:30 am, a member of the public reported a release to centurion pipeline company l.P. (cpl) on a right of way near blair, oklahoma, in jackson county, oklahoma. Cpl shut down the pipeline at 9:39 am after confirming the release. Approximately 4201 barrels of crude oil were released. 1897 barrels of oil were recovered with 1741 barrels being recovered in liquid form while 156 barrels in soil have been moved to an offsite location for remediation. No injuries, fatalities, or fires were associated with this accident. The initial national response center (nrc) report number concerning this accident is 1248387. The 48 hour follow up call made to the nrc on june 12, 2019 has a reference number of 1248615. The root cause analysis of the failure has determined that a third party road grader struck the line leading to loss of containment. The pipeline has been repaired with a plidco split + sleeve, a commercially available bolt on split sleeve repair, and restarted the pipeline at 8:20 am on june 12, 2019. Environmental remediation is still underway and a supplemental report will be completed once remediation costs have been determined. Supplemental final report submitted october 10, 2019 permanent repairs to the pipeline were completed july 24, 2019. Approximately 20 feet of pipe was replaced with new API 5l, ps2l, x52 specification pipe. Remediation efforts were completed september 23, 2019. Part d, item 8 has been updated to include the final remediation estimate as well as the cost of the permanent repair.
| Report Received Date | 2019-07-10 00:00:00 |
|---|---|
| Iyear | 2019 |
| Report Number | 20190221 |
| Supplemental Number | 32793 |
| Report Type | Supplemental Final |
| Operator Id | 31888 PHMSA Enforcement |
| Name | Centurion Pipeline L.p. |
| Operator Street Address | 5 Greenway Plaza, Suite 1600 |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77046-7570 |
| Local Datetime | 2019-06-10 09:20:00 |
| Location Latitude | 34.765475 Google Maps OpenStreetMap |
| Location Longitude | -99.32194444 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 4201 |
| Recovered Bbls | 1897 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Notification From Public |
| Incident Identified Datetime | 2019-06-10 09:30:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2019-06-10 09:39:00 |
| Restart Datetime | 2019-06-12 08:20:00 |
| On Site Datetime | 2019-06-10 10:15:00 |
| Nrc Rpt Datetime | 2019-06-10 10:20:00 |
| Nrc Rpt Num | 1248615 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Upstream Valve Type Ind | Remotely Controlled |
| Downstream Valve Type Ind | Remotely Controlled |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Slaughter To Cushing System #1 |
| Segment Name | Slaughter To Cushing System #1 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 73009 |
| Onshore City Name | Blair |
| Onshore County Name | Jackson |
| Designated Location | Milepost/valve Station |
| Designated Name | 179 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 14 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 16 |
| Pipe Wall Thickness | 0.25 |
| Pipe Smys | 35000 |
| Pipe Specification | Grade B |
| Pipe Seam Type | Other |
| Pipe Seam Details | Electric Fusion Welding (Efw) |
| Pipe Manufacturer | A.o. Smith |
| Pipe Coating Type | Composite |
| Installation Year | 1944 |
| Manufactured Year | 1942 |
| Material Involved | Carbon Steel |
| Release Type | Mechanical Puncture |
| Puncture Axial | 8 |
| Puncture Circum | 1 |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 200000 |
| Est Cost Gas Released | 135300 |
| Est Cost Prop Damage | 289500 |
| Est Cost Emergency | 81000 |
| Est Cost Environmental | 884000 |
| Est Cost Other | 0 |
| Prpty | 1589800 |
| Accident Psig | 400 |
| Mop Psig | 715 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Length Segment Isolated | 84480 |
| Internal Inspection Ind | Yes |
| Operation Complications Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | Yes |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | Yes |
| Cpm Conf Ind | Yes |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Third party damage was the cause. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Excavation Damage |
| Cause Details | Excavation Damage By Third Party |
| Ex Party Type | Excavation Damage By Third Party |
| Prior Notification Ind | No |
| Notify Cga Dirt | Yes |
| Private Row Ind | Yes |
| Private Subtype | Private Easement |
| Excavator Type | Farmer |
| Excavator Equipment | Grader/scraper |
| Work Performed | Drainage |
| One Call Notified Ind | No |
| Service Interruption | Yes |
| Service Interruption Hours | 44 |
| Root Cause Category | Notification Issue |
| Root Cause Type | No Notification Made To The One-Call Center/811 |
| Collected Data Ind | Yes |
| Axial Magnetic Flx Lkg Ind | Yes |
| Geometry Deformation Ind | Yes |
| Axial Recent Year | 2017 |
| Geometry Recent Year | 2017 |
| Other Recent Year | 2017 |
| Insp Compl Before Damage Ind | Yes |
| Has Hydrtst Conduc Before Ind | Yes |
| Hydrtst Most Rcnt Year | 2009 |
| Hydrtst Most Rcnt Pressure | 1010 |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | D**** N***** |
| Preparer Title | Risk Engineer |
| Preparer Email | D***********@c**********.com |
| Preparer Telephone | 346-803-2688 |
| Prepared Date | 2019-10-09 00:00:00 |
| Authorizer Name | D**** M**** |
| Authorizer Telephone | 346-803-2680 |
| Authorizer Title | Senior Pipeline Compliance Consultant |
| Authorizer Email | D**********@c**********.com |
| Narrative | On june 10, 2019, at approximately 9:30 am, a member of the public reported a release to centurion pipeline company l.P. (cpl) on a right of way near blair, oklahoma, in jackson county, oklahoma. Cpl shut down the pipeline at 9:39 am after confirming the release. Approximately 4201 barrels of crude oil were released. 1897 barrels of oil were recovered with 1741 barrels being recovered in liquid form while 156 barrels in soil have been moved to an offsite location for remediation. No injuries, fatalities, or fires were associated with this accident. The initial national response center (nrc) report number concerning this accident is 1248387. The 48 hour follow up call made to the nrc on june 12, 2019 has a reference number of 1248615. The root cause analysis of the failure has determined that a third party road grader struck the line leading to loss of containment. The pipeline has been repaired with a plidco split + sleeve, a commercially available bolt on split sleeve repair, and restarted the pipeline at 8:20 am on june 12, 2019. Environmental remediation is still underway and a supplemental report will be completed once remediation costs have been determined. Supplemental final report submitted october 10, 2019 permanent repairs to the pipeline were completed july 24, 2019. Approximately 20 feet of pipe was replaced with new API 5l, ps2l, x52 specification pipe. Remediation efforts were completed september 23, 2019. Part d, item 8 has been updated to include the final remediation estimate as well as the cost of the permanent repair. |
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