HL incident on 2019-06-25 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$13,451
Incident datetime
2019-06-25 04:30
Report number
Location
TX
Narrative
On 5/30/19 at 4:30 pm terminal manager received call from a terminal operator stating a pinhole leak had been identified on the pressure relief valve piping on tank 96 at the carteret truck rack terminal. Tank 96 contained heavy naptha. Quantity released into secondary containment was 7.9 gallons of naptha. Kinder morgan's terminal project management team, mechanical contractors, environmental health and safety, and remediation contractors worked together to drain the tank, repair the tank and remediate the secondary containment area. Verification of finalized remediation is pending. The failed pressure relief line has been replaced with thicker wall piping and additional bracing. Tank 96 is back in service. 04/09/2025 - updated by PHMSA per operator approval.
Detailed record list
Report Received Date
2019-06-28 00:00:00
Iyear
2019
Report Number
20190207
Supplemental Number
33263
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-05-30 04:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.19
Recovered Bbls
0.19
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-06-25 04:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
This Did Not Occur During A Pipeline Move.
On Site Datetime
2019-06-25 04:35:00
Nrc Rpt Datetime
2019-06-25 05:20:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Carteret Truck Rack Terminal
Segment Name
Tank 96
Onshore State Abbreviation
Nj
Onshore Postal Code
07008
Onshore City Name
Carteret
Onshore County Name
Middlesex
Designated Location
Milepost/valve Station
Designated Name
In Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Relief Valve
Tank Type
Atmospheric
Installation Year
2005
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
13451
Est Cost Emergency
5426
Est Cost Environmental
21073
Est Cost Other
0
Prpty
39950
Accident Psig
16.7
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The tank was idle at the time of the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Other
Other Non Threaded Details
Welded Pipe Nipple.
Additional Vibration Ind
Yes
Preparer Name
D******* S*******
Preparer Title
Director Of Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
713-725-0147
Preparer Fax
303-984-3048
Prepared Date
2020-02-03 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
713-725-0147
Authorizer Title
Director Of Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On 5/30/19 at 4:30 pm terminal manager received call from a terminal operator stating a pinhole leak had been identified on the pressure relief valve piping on tank 96 at the carteret truck rack terminal. Tank 96 contained heavy naptha. Quantity released into secondary containment was 7.9 gallons of naptha. Kinder morgan's terminal project management team, mechanical contractors, environmental health and safety, and remediation contractors worked together to drain the tank, repair the tank and remediate the secondary containment area. Verification of finalized remediation is pending. The failed pressure relief line has been replaced with thicker wall piping and additional bracing. Tank 96 is back in service. 04/09/2025 - updated by PHMSA per operator approval.
Report Received Date 2019-06-28 00:00:00
Iyear 2019
Report Number 20190207
Supplemental Number 33263
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-05-30 04:30:00
Location Latitude 40.58953 Google Maps OpenStreetMap
Location Longitude -74.225518 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.19
Recovered Bbls 0.19
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-06-25 04:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain This Did Not Occur During A Pipeline Move.
On Site Datetime 2019-06-25 04:35:00
Nrc Rpt Datetime 2019-06-25 05:20:00
Nrc Rpt Num 1247328 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Carteret Truck Rack Terminal
Segment Name Tank 96
Onshore State Abbreviation Nj
Onshore Postal Code 07008
Onshore City Name Carteret
Onshore County Name Middlesex
Designated Location Milepost/valve Station
Designated Name In Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Relief Valve
Tank Type Atmospheric
Installation Year 2005
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 13451
Est Cost Emergency 5426
Est Cost Environmental 21073
Est Cost Other 0
Prpty 39950
Accident Psig 16.7
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The tank was idle at the time of the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Other
Other Non Threaded Details Welded Pipe Nipple.
Additional Vibration Ind Yes
Preparer Name D******* S*******
Preparer Title Director Of Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 713-725-0147
Preparer Fax 303-984-3048
Prepared Date 2020-02-03 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 713-725-0147
Authorizer Title Director Of Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On 5/30/19 at 4:30 pm terminal manager received call from a terminal operator stating a pinhole leak had been identified on the pressure relief valve piping on tank 96 at the carteret truck rack terminal. Tank 96 contained heavy naptha. Quantity released into secondary containment was 7.9 gallons of naptha. Kinder morgan's terminal project management team, mechanical contractors, environmental health and safety, and remediation contractors worked together to drain the tank, repair the tank and remediate the secondary containment area. Verification of finalized remediation is pending. The failed pressure relief line has been replaced with thicker wall piping and additional bracing. Tank 96 is back in service. 04/09/2025 - updated by PHMSA per operator approval.

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