HL incident on 2019-05-29 — TX

Operator
Holly Energy Partners - Operating, L.p.
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40
Incident datetime
2019-05-29 01:22
Report number
Location
TX
Narrative
During normal operations, the holly energy partners control center received an lel vapor monitor alarm at hawley station at 00:22 mt via the scada system. The pipeline was immediately shut down and blocked in at 00:22 mt. A technician was dispatched to the location to investigate further. Once holly energy partners personnel arrived on-site at 01:05 mt, they were able to confirm that a piece of steel tubing had failed on hawley stations pumping unit #2. Holly energy partners personnel on location also reported that there was a release of product from the failed tubing. During a root cause investigation, it was determined that the failure was a result of high-frequency vibration.
Detailed record list
Report Received Date
2019-06-26 00:00:00
Iyear
2019
Report Number
20190201
Supplemental Number
33955
Report Type
Supplemental Final
Operator Id
Name
Holly Energy Partners - Operating, L.p.
Operator Street Address
2323 Victory Ave. Suite 1400
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75219
Local Datetime
2019-05-29 01:22:00
Location Latitude
Location Longitude
-99.78808901
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.4
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2019-05-29 01:22:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-05-29 01:22:00
Restart Datetime
2019-05-29 11:34:00
On Site Datetime
2019-05-29 02:05:00
Nrc Rpt Datetime
2019-05-29 03:07:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Trust 6/8 Hawley Station
Segment Name
Hawley Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79525
Onshore City Name
Not Within A Municipality
Onshore County Name
Jones
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tubing
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
40
Est Cost Emergency
0
Est Cost Environmental
20000
Est Cost Other
0
Prpty
20065
Accident Psig
385
Mop Psig
1150
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Actions of the control room personnel did not contribute to the failure of the tubing. Control room personnel were operating the pipeline well below mop and the line was in a steady-state.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Vibration Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
High Frequency Vibration
Preparer Name
C****** C***
Preparer Title
Manager Pipeline Regulatory
Preparer Email
C***********@h**********.com
Preparer Telephone
2148713574
Prepared Date
2020-06-26 00:00:00
Authorizer Name
C****** C***
Authorizer Telephone
2148713574
Authorizer Title
Manager Pipeline Regulatory
Authorizer Email
C***********@h**********.com
Narrative
During normal operations, the holly energy partners control center received an lel vapor monitor alarm at hawley station at 00:22 mt via the scada system. The pipeline was immediately shut down and blocked in at 00:22 mt. A technician was dispatched to the location to investigate further. Once holly energy partners personnel arrived on-site at 01:05 mt, they were able to confirm that a piece of steel tubing had failed on hawley stations pumping unit #2. Holly energy partners personnel on location also reported that there was a release of product from the failed tubing. During a root cause investigation, it was determined that the failure was a result of high-frequency vibration.
Report Received Date 2019-06-26 00:00:00
Iyear 2019
Report Number 20190201
Supplemental Number 33955
Report Type Supplemental Final
Operator Id 32011 PHMSA Enforcement
Name Holly Energy Partners - Operating, L.p.
Operator Street Address 2323 Victory Ave. Suite 1400
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75219
Local Datetime 2019-05-29 01:22:00
Location Latitude 32.56314783 Google Maps OpenStreetMap
Location Longitude -99.78808901 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.4
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2019-05-29 01:22:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-05-29 01:22:00
Restart Datetime 2019-05-29 11:34:00
On Site Datetime 2019-05-29 02:05:00
Nrc Rpt Datetime 2019-05-29 03:07:00
Nrc Rpt Num 1247097 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Trust 6/8 Hawley Station
Segment Name Hawley Station
Onshore State Abbreviation Tx
Onshore Postal Code 79525
Onshore City Name Not Within A Municipality
Onshore County Name Jones
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tubing
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 25
Est Cost Prop Damage 40
Est Cost Emergency 0
Est Cost Environmental 20000
Est Cost Other 0
Prpty 20065
Accident Psig 385
Mop Psig 1150
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Actions of the control room personnel did not contribute to the failure of the tubing. Control room personnel were operating the pipeline well below mop and the line was in a steady-state.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Vibration Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details High Frequency Vibration
Preparer Name C****** C***
Preparer Title Manager Pipeline Regulatory
Preparer Email C***********@h**********.com
Preparer Telephone 2148713574
Prepared Date 2020-06-26 00:00:00
Authorizer Name C****** C***
Authorizer Telephone 2148713574
Authorizer Title Manager Pipeline Regulatory
Authorizer Email C***********@h**********.com
Narrative During normal operations, the holly energy partners control center received an lel vapor monitor alarm at hawley station at 00:22 mt via the scada system. The pipeline was immediately shut down and blocked in at 00:22 mt. A technician was dispatched to the location to investigate further. Once holly energy partners personnel arrived on-site at 01:05 mt, they were able to confirm that a piece of steel tubing had failed on hawley stations pumping unit #2. Holly energy partners personnel on location also reported that there was a release of product from the failed tubing. During a root cause investigation, it was determined that the failure was a result of high-frequency vibration.

All rights reserved. Copyright © by ClearPHMSA