HL incident on 2019-05-29 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$145,000
Incident datetime
2019-05-29 08:45
Report number
Location
TX
Narrative
On wednesday, may 29, 2019 at approximately 8:45 am during a routine anamoly dig, the crew was removing coating and wrap and heard a hissing noise coming from a pin hole leak near a stopple fitting on the pr-01 pipeline. The crew exited the ditch and made notifications. The line was immediately shut down and isolated and the leak area was monitored. To repair the leak, the pipeline was purged with nitrogen purge and the section of the pipeline with the leak was replaced. The pipeline restarted at approximately 6 pm on sunday, june 2, 2019. The total leak volume was estimated at 0.98 barrels. The section of pipe that was removed has been sent to a lab for metallurgical analysis to determine the cause of the pinhole. This report will be finalized following obtaining the results of the analysis. 02/26/2020 update received preliminary metallurgical analysis shows that the failure appears to have been caused by soil side selective seam corrosion. A mechanical test is in progress to verify the results. 3/30/2020 update. Updated depth of cover due to discrepancy in API reports--tf 6/3/2020 final analysis. Final analysis concluded that the pipe leaked due to selective erw seam weld corrosion. The corrosion was entirely external and highly localized in a small zone of apparent coating failure at the 6:00 o'clock position. The erw seam weld was of good quality with no hook cracks or excessive internal flash. Internal corrosion was minimal and the pipe met the chemistry and mechanical properties requirements for API 5l gr. X-42. 9-10-2020 update request from aid updated the unknown frequency, year and manufacture of pipe. Corrected g-5 to a yes because there was damaged coating. --tf 9-15-2020 update due to error in pipe manufacture reporting--tf
Detailed record list
Report Received Date
2019-06-20 00:00:00
Iyear
2019
Report Number
20190198
Supplemental Number
34272
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2019-05-29 08:45:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.98
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2019-05-29 08:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-05-29 08:50:00
Restart Datetime
2019-06-02 18:00:00
On Site Datetime
2019-05-29 08:45:00
Nrc Rpt Datetime
2019-05-29 09:56:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Pr-01
Segment Name
Pr-01 Denver Junction To Kiowa
Onshore State Abbreviation
Co
Onshore Postal Code
80013
Onshore City Name
Aurora
Onshore County Name
Arapahoe
Designated Location
Milepost/valve Station
Designated Name
Mp 343
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api-5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Coal Tar
Installation Year
1950
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
145000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
145060
Accident Psig
1155
Mop Psig
1350
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
31928
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pinhole leak discovered during an anomaly dig. Controller had no affect on the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Selective Seam Corrosion Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1979
Shielding Evident
Unknown
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2018
Other Cp Survey Year
2019
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Axial Recent Year
2018
Circ Wave Recent Year
2012
Geometry Recent Year
2018
Other Recent Year
2018
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1994
Hydrtst Most Rcnt Pressure
1916
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J*** R********
Preparer Title
Dot Coordinator
Preparer Email
J***************@p**.com
Preparer Telephone
806-318-9269
Prepared Date
2020-09-15 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
8327651632
Authorizer Title
Director Dot Compliance
Authorizer Email
T***********@p**.com
Narrative
On wednesday, may 29, 2019 at approximately 8:45 am during a routine anamoly dig, the crew was removing coating and wrap and heard a hissing noise coming from a pin hole leak near a stopple fitting on the pr-01 pipeline. The crew exited the ditch and made notifications. The line was immediately shut down and isolated and the leak area was monitored. To repair the leak, the pipeline was purged with nitrogen purge and the section of the pipeline with the leak was replaced. The pipeline restarted at approximately 6 pm on sunday, june 2, 2019. The total leak volume was estimated at 0.98 barrels. The section of pipe that was removed has been sent to a lab for metallurgical analysis to determine the cause of the pinhole. This report will be finalized following obtaining the results of the analysis. 02/26/2020 update received preliminary metallurgical analysis shows that the failure appears to have been caused by soil side selective seam corrosion. A mechanical test is in progress to verify the results. 3/30/2020 update. Updated depth of cover due to discrepancy in API reports--tf 6/3/2020 final analysis. Final analysis concluded that the pipe leaked due to selective erw seam weld corrosion. The corrosion was entirely external and highly localized in a small zone of apparent coating failure at the 6:00 o'clock position. The erw seam weld was of good quality with no hook cracks or excessive internal flash. Internal corrosion was minimal and the pipe met the chemistry and mechanical properties requirements for API 5l gr. X-42. 9-10-2020 update request from aid updated the unknown frequency, year and manufacture of pipe. Corrected g-5 to a yes because there was damaged coating. --tf 9-15-2020 update due to error in pipe manufacture reporting--tf
Report Received Date 2019-06-20 00:00:00
Iyear 2019
Report Number 20190198
Supplemental Number 34272
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2019-05-29 08:45:00
Location Latitude 39.68194 Google Maps OpenStreetMap
Location Longitude -104.78501 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.98
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2019-05-29 08:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-05-29 08:50:00
Restart Datetime 2019-06-02 18:00:00
On Site Datetime 2019-05-29 08:45:00
Nrc Rpt Datetime 2019-05-29 09:56:00
Nrc Rpt Num 1247141 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Pr-01
Segment Name Pr-01 Denver Junction To Kiowa
Onshore State Abbreviation Co
Onshore Postal Code 80013
Onshore City Name Aurora
Onshore County Name Arapahoe
Designated Location Milepost/valve Station
Designated Name Mp 343
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api-5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Republic Steel
Pipe Coating Type Coal Tar
Installation Year 1950
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 145000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 145060
Accident Psig 1155
Mop Psig 1350
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 31928
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pinhole leak discovered during an anomaly dig. Controller had no affect on the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Selective Seam Corrosion Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1979
Shielding Evident Unknown
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Other Cp Survey Ind Yes
Cp Annual Survey Year 2018
Other Cp Survey Year 2019
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Axial Recent Year 2018
Circ Wave Recent Year 2012
Geometry Recent Year 2018
Other Recent Year 2018
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1994
Hydrtst Most Rcnt Pressure 1916
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J*** R********
Preparer Title Dot Coordinator
Preparer Email J***************@p**.com
Preparer Telephone 806-318-9269
Prepared Date 2020-09-15 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 8327651632
Authorizer Title Director Dot Compliance
Authorizer Email T***********@p**.com
Narrative On wednesday, may 29, 2019 at approximately 8:45 am during a routine anamoly dig, the crew was removing coating and wrap and heard a hissing noise coming from a pin hole leak near a stopple fitting on the pr-01 pipeline. The crew exited the ditch and made notifications. The line was immediately shut down and isolated and the leak area was monitored. To repair the leak, the pipeline was purged with nitrogen purge and the section of the pipeline with the leak was replaced. The pipeline restarted at approximately 6 pm on sunday, june 2, 2019. The total leak volume was estimated at 0.98 barrels. The section of pipe that was removed has been sent to a lab for metallurgical analysis to determine the cause of the pinhole. This report will be finalized following obtaining the results of the analysis. 02/26/2020 update received preliminary metallurgical analysis shows that the failure appears to have been caused by soil side selective seam corrosion. A mechanical test is in progress to verify the results. 3/30/2020 update. Updated depth of cover due to discrepancy in API reports--tf 6/3/2020 final analysis. Final analysis concluded that the pipe leaked due to selective erw seam weld corrosion. The corrosion was entirely external and highly localized in a small zone of apparent coating failure at the 6:00 o'clock position. The erw seam weld was of good quality with no hook cracks or excessive internal flash. Internal corrosion was minimal and the pipe met the chemistry and mechanical properties requirements for API 5l gr. X-42. 9-10-2020 update request from aid updated the unknown frequency, year and manufacture of pipe. Corrected g-5 to a yes because there was damaged coating. --tf 9-15-2020 update due to error in pipe manufacture reporting--tf

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