HL incident on 2019-05-13 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$150
Incident datetime
2019-05-13 07:12
Report number
Location
TX
Narrative
Pipeline control received a haz-gas alarm from mclouth station at 07:12 on 5/13/19. Enterprise technician was dispatched and discovered that the .75 inch relief valve on facility pipe relieved open and did not close. Release was stopped approximately 08:45. The technician replaced the relief valve to prevent reoccurrence. Normal operations resumed at 10:45 the same day. The valve would not completely seat due to worn soft good material (o-rings). Approximately 3 bbls of ethane/propane mix was released with no environmental consequences.
Detailed record list
Report Received Date
2019-06-17 00:00:00
Iyear
2019
Report Number
20190192
Supplemental Number
32866
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-05-13 07:12:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane/propane Mix
Unintentional Release Bbls
3
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2019-05-13 07:12:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-05-13 07:12:00
Restart Datetime
2019-05-13 10:45:00
On Site Datetime
2019-05-13 08:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Mclouth Station
Segment Name
Lid 603
Onshore State Abbreviation
Ks
Onshore Postal Code
66054
Onshore City Name
Mclouth
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Am 156
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Relief Valve Relieved At Lower Pressure Than Set Point.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
150
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
350
Accident Psig
619
Mop Psig
1300
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room did not contribute to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Soft Goods Failure
Preparer Name
R*** T********
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2019-10-23 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Pipeline Compliance Manager
Authorizer Email
S******@e****.com
Narrative
Pipeline control received a haz-gas alarm from mclouth station at 07:12 on 5/13/19. Enterprise technician was dispatched and discovered that the .75 inch relief valve on facility pipe relieved open and did not close. Release was stopped approximately 08:45. The technician replaced the relief valve to prevent reoccurrence. Normal operations resumed at 10:45 the same day. The valve would not completely seat due to worn soft good material (o-rings). Approximately 3 bbls of ethane/propane mix was released with no environmental consequences.
Report Received Date 2019-06-17 00:00:00
Iyear 2019
Report Number 20190192
Supplemental Number 32866
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-05-13 07:12:00
Location Latitude 39.17354 Google Maps OpenStreetMap
Location Longitude -95.20931 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane/propane Mix
Unintentional Release Bbls 3
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2019-05-13 07:12:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-05-13 07:12:00
Restart Datetime 2019-05-13 10:45:00
On Site Datetime 2019-05-13 08:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Mclouth Station
Segment Name Lid 603
Onshore State Abbreviation Ks
Onshore Postal Code 66054
Onshore City Name Mclouth
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Am 156
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Relief Valve
Installation Year 2018
Material Involved Carbon Steel
Release Type Other
Release Type Details Relief Valve Relieved At Lower Pressure Than Set Point.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 150
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 350
Accident Psig 619
Mop Psig 1300
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room did not contribute to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Soft Goods Failure
Preparer Name R*** T********
Preparer Title Pipeline Compliance Engineer
Preparer Email R*********@e****.com
Preparer Telephone 713-381-4659
Prepared Date 2019-10-23 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Pipeline Compliance Manager
Authorizer Email S******@e****.com
Narrative Pipeline control received a haz-gas alarm from mclouth station at 07:12 on 5/13/19. Enterprise technician was dispatched and discovered that the .75 inch relief valve on facility pipe relieved open and did not close. Release was stopped approximately 08:45. The technician replaced the relief valve to prevent reoccurrence. Normal operations resumed at 10:45 the same day. The valve would not completely seat due to worn soft good material (o-rings). Approximately 3 bbls of ethane/propane mix was released with no environmental consequences.

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