HL incident on 2019-05-22 — OH

Operator
Marathon Pipe Line Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-05-22 22:00
Report number
Location
OH
Narrative
On 5/22/19 at 2200 hours, terminal operator discovered a small product release from a tank valve on transmix tank t-5. The leak was stopped by closing a small needle valve on the body relief. Initial clean-up was performed by the terminal personnel and totally contained on operator property. Total volume released has been determined to be 73.5 gallons. Root cause analysis has determined the cause to be a small needle valve attached to the valve body relief was left open and when pressure built up, the product released through the open path. 01/21/2025 - a small needle valve attached to the valve body relief was left open 01/21/2025 - updated by PHMSA per operator approval.
Detailed record list
Report Received Date
2019-06-17 00:00:00
Iyear
2019
Report Number
20190191
Supplemental Number
32532
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2019-05-22 22:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
1.8
Recovered Bbls
1.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-05-22 22:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Not In Use At Time Of Discovery
On Site Datetime
2019-05-22 22:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hammond Terminal
Segment Name
Facility Piping
Onshore State Abbreviation
In
Onshore Postal Code
46327
Onshore City Name
Hammond
Onshore County Name
Lake
Designated Location
Milepost/valve Station
Designated Name
Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Valve Type
Relief Valve
Tank Vessel Subtype
Appurtenance
Tank Type
Atmospheric
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Needle Valve Open
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
132
Est Cost Prop Damage
0
Est Cost Emergency
14000
Est Cost Environmental
0
Est Cost Other
0
Prpty
14132
Accident Psig
10
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Due to minimal release rate, the incident was non-detectable by cpm/scada
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
B*** H********
Preparer Title
Hes Professional
Preparer Email
B**********@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2019-08-09 00:00:00
Authorizer Name
R****** W* B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory And Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
On 5/22/19 at 2200 hours, terminal operator discovered a small product release from a tank valve on transmix tank t-5. The leak was stopped by closing a small needle valve on the body relief. Initial clean-up was performed by the terminal personnel and totally contained on operator property. Total volume released has been determined to be 73.5 gallons. Root cause analysis has determined the cause to be a small needle valve attached to the valve body relief was left open and when pressure built up, the product released through the open path. 01/21/2025 - a small needle valve attached to the valve body relief was left open 01/21/2025 - updated by PHMSA per operator approval.
Report Received Date 2019-06-17 00:00:00
Iyear 2019
Report Number 20190191
Supplemental Number 32532
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2019-05-22 22:00:00
Location Latitude 41.637437 Google Maps OpenStreetMap
Location Longitude -87.501584 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 1.8
Recovered Bbls 1.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-05-22 22:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Was Not In Use At Time Of Discovery
On Site Datetime 2019-05-22 22:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Hammond Terminal
Segment Name Facility Piping
Onshore State Abbreviation In
Onshore Postal Code 46327
Onshore City Name Hammond
Onshore County Name Lake
Designated Location Milepost/valve Station
Designated Name Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Valve Type Relief Valve
Tank Vessel Subtype Appurtenance
Tank Type Atmospheric
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Needle Valve Open
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 132
Est Cost Prop Damage 0
Est Cost Emergency 14000
Est Cost Environmental 0
Est Cost Other 0
Prpty 14132
Accident Psig 10
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Due to minimal release rate, the incident was non-detectable by cpm/scada
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name B*** H********
Preparer Title Hes Professional
Preparer Email B**********@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2019-08-09 00:00:00
Authorizer Name R****** W* B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory And Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative On 5/22/19 at 2200 hours, terminal operator discovered a small product release from a tank valve on transmix tank t-5. The leak was stopped by closing a small needle valve on the body relief. Initial clean-up was performed by the terminal personnel and totally contained on operator property. Total volume released has been determined to be 73.5 gallons. Root cause analysis has determined the cause to be a small needle valve attached to the valve body relief was left open and when pressure built up, the product released through the open path. 01/21/2025 - a small needle valve attached to the valve body relief was left open 01/21/2025 - updated by PHMSA per operator approval.

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