HL incident on 2019-05-17 — TX

Operator
Plantation Pipe Line Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2019-05-17 09:00
Report number
Location
TX
Narrative
On 5/16/2019 at 20:00, the explosive atmosphere detector alarm at the catchment basin (opposite side of delivery terminal) activated. Local personnel conducted an investigation of the site and were unable to determine cause of alarm. During a subsequent investigation the morning of 5/17/2019, local personnel discovered the presence of hydrocarbon product in a water-collection vault. Further investigation identified a failed insulating gasket (used for cathodic protection purposes) on a nearby flange as the source of the release. Supplemental/final note: the type of material used for the failed gasket installed at this location had no secondary sealing surface and was made of non-compressible material. This gasket was replaced with one suitable for this type of pipeline service. The national response center was notified on 6/3/19 when it was determined the cost of the release would likely exceed the $50,000 reporting criteria.
Detailed record list
Report Received Date
2019-06-14 00:00:00
Iyear
2019
Report Number
20190190
Supplemental Number
32450
Report Type
Supplemental Final
Operator Id
Name
Plantation Pipe Line Co
Operator Street Address
1001 Louisiana St Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-05-16 20:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.4
Recovered Bbls
0.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2019-05-17 09:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Facility Was Already Shut Down Due To Normal Scheduling
On Site Datetime
2019-05-17 09:00:00
Nrc Rpt Datetime
2019-06-03 11:33:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Charlotte Delivery Terminal
Segment Name
Delivery Manifold
Onshore State Abbreviation
Nc
Onshore Postal Code
28214
Onshore City Name
Charlotte
Onshore County Name
Mecklenburg
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1997
Material Involved
Material Other Than Carbon Steel
Material Details
Phenolic Gasket
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
33
Est Cost Prop Damage
500
Est Cost Emergency
45000
Est Cost Environmental
23000
Est Cost Other
0
Prpty
68533
Accident Psig
1
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Preparer Name
Q****** H F******
Preparer Title
Director-Compliance Codes And Standards
Preparer Email
Q**************@k***********.com
Preparer Telephone
770-751-4240
Prepared Date
2019-07-19 00:00:00
Authorizer Name
Q****** H F******
Authorizer Telephone
770-751-4240
Authorizer Title
Director-Compliance Codes And Standards
Authorizer Email
Q**************@k***********.com
Narrative
On 5/16/2019 at 20:00, the explosive atmosphere detector alarm at the catchment basin (opposite side of delivery terminal) activated. Local personnel conducted an investigation of the site and were unable to determine cause of alarm. During a subsequent investigation the morning of 5/17/2019, local personnel discovered the presence of hydrocarbon product in a water-collection vault. Further investigation identified a failed insulating gasket (used for cathodic protection purposes) on a nearby flange as the source of the release. Supplemental/final note: the type of material used for the failed gasket installed at this location had no secondary sealing surface and was made of non-compressible material. This gasket was replaced with one suitable for this type of pipeline service. The national response center was notified on 6/3/19 when it was determined the cost of the release would likely exceed the $50,000 reporting criteria.
Report Received Date 2019-06-14 00:00:00
Iyear 2019
Report Number 20190190
Supplemental Number 32450
Report Type Supplemental Final
Operator Id 15674 PHMSA Enforcement
Name Plantation Pipe Line Co
Operator Street Address 1001 Louisiana St Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-05-16 20:00:00
Location Latitude 35.28024 Google Maps OpenStreetMap
Location Longitude -80.93964 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.4
Recovered Bbls 0.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2019-05-17 09:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Facility Was Already Shut Down Due To Normal Scheduling
On Site Datetime 2019-05-17 09:00:00
Nrc Rpt Datetime 2019-06-03 11:33:00
Nrc Rpt Num 1247673 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Charlotte Delivery Terminal
Segment Name Delivery Manifold
Onshore State Abbreviation Nc
Onshore Postal Code 28214
Onshore City Name Charlotte
Onshore County Name Mecklenburg
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1997
Material Involved Material Other Than Carbon Steel
Material Details Phenolic Gasket
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 33
Est Cost Prop Damage 500
Est Cost Emergency 45000
Est Cost Environmental 23000
Est Cost Other 0
Prpty 68533
Accident Psig 1
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Installation Ind Yes
Preparer Name Q****** H F******
Preparer Title Director-Compliance Codes And Standards
Preparer Email Q**************@k***********.com
Preparer Telephone 770-751-4240
Prepared Date 2019-07-19 00:00:00
Authorizer Name Q****** H F******
Authorizer Telephone 770-751-4240
Authorizer Title Director-Compliance Codes And Standards
Authorizer Email Q**************@k***********.com
Narrative On 5/16/2019 at 20:00, the explosive atmosphere detector alarm at the catchment basin (opposite side of delivery terminal) activated. Local personnel conducted an investigation of the site and were unable to determine cause of alarm. During a subsequent investigation the morning of 5/17/2019, local personnel discovered the presence of hydrocarbon product in a water-collection vault. Further investigation identified a failed insulating gasket (used for cathodic protection purposes) on a nearby flange as the source of the release. Supplemental/final note: the type of material used for the failed gasket installed at this location had no secondary sealing surface and was made of non-compressible material. This gasket was replaced with one suitable for this type of pipeline service. The national response center was notified on 6/3/19 when it was determined the cost of the release would likely exceed the $50,000 reporting criteria.

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