HL incident on 2019-05-18 — TX

Operator
Ccps Transportation, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,975
Incident datetime
2019-05-18 06:50
Report number
Location
TX
Narrative
On may 18, 2019 at 06:24 cdt, the edmonton control center noticed that the sample cans for line 59 were not filling up and notified the cushing control center. An operations technician was sent out to investigate the sample can issue. At 06:50 cdt, the technician discovered the sample probe for line 59 released approximately 7 gallons of crude oil in the sample building located in the cushing south terminal. The technician immediately contacted the edmonton control center and line 59 was shut down to prevent any further release of product. All crude oil was contained within the sample building, which was cleaned up and properly disposed of. The probe cap was tightened and the line was restarted. The area was monitored and no further releases occurred. The investigation determined the release was due to the sample probe cap not being properly tightened prior to shipping.
Detailed record list
Report Received Date
2019-06-13 00:00:00
Iyear
2019
Report Number
20190185
Supplemental Number
32274
Report Type
Original Final
Operator Id
Name
Ccps Transportation, Llc
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2019-05-18 06:24:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.17
Recovered Bbls
0.17
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2019-05-18 06:50:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-05-18 06:52:00
Restart Datetime
2019-05-18 09:13:00
On Site Datetime
2019-05-18 06:50:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing South Terminal
Segment Name
Line 59
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Lincoln
Designated Location
Milepost/valve Station
Designated Name
Cushing
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Instrumentation
Installation Year
2019
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
7
Est Cost Prop Damage
1975
Est Cost Emergency
628
Est Cost Environmental
0
Est Cost Other
0
Prpty
2610
Accident Psig
64
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Sample Probe Cap
Eq Additional Other Ind
Yes
Eq Additional Other Details
Sample Probe Cap Was Not Properly Tightened Prior To Shipping
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2019-06-13 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On may 18, 2019 at 06:24 cdt, the edmonton control center noticed that the sample cans for line 59 were not filling up and notified the cushing control center. An operations technician was sent out to investigate the sample can issue. At 06:50 cdt, the technician discovered the sample probe for line 59 released approximately 7 gallons of crude oil in the sample building located in the cushing south terminal. The technician immediately contacted the edmonton control center and line 59 was shut down to prevent any further release of product. All crude oil was contained within the sample building, which was cleaned up and properly disposed of. The probe cap was tightened and the line was restarted. The area was monitored and no further releases occurred. The investigation determined the release was due to the sample probe cap not being properly tightened prior to shipping.
Report Received Date 2019-06-13 00:00:00
Iyear 2019
Report Number 20190185
Supplemental Number 32274
Report Type Original Final
Operator Id 32080 PHMSA Enforcement
Name Ccps Transportation, Llc
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2019-05-18 06:24:00
Location Latitude 35.937033 Google Maps OpenStreetMap
Location Longitude -96.752431 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.17
Recovered Bbls 0.17
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2019-05-18 06:50:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-05-18 06:52:00
Restart Datetime 2019-05-18 09:13:00
On Site Datetime 2019-05-18 06:50:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing South Terminal
Segment Name Line 59
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Lincoln
Designated Location Milepost/valve Station
Designated Name Cushing
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Instrumentation
Installation Year 2019
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 7
Est Cost Prop Damage 1975
Est Cost Emergency 628
Est Cost Environmental 0
Est Cost Other 0
Prpty 2610
Accident Psig 64
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Sample Probe Cap
Eq Additional Other Ind Yes
Eq Additional Other Details Sample Probe Cap Was Not Properly Tightened Prior To Shipping
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2019-06-13 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On may 18, 2019 at 06:24 cdt, the edmonton control center noticed that the sample cans for line 59 were not filling up and notified the cushing control center. An operations technician was sent out to investigate the sample can issue. At 06:50 cdt, the technician discovered the sample probe for line 59 released approximately 7 gallons of crude oil in the sample building located in the cushing south terminal. The technician immediately contacted the edmonton control center and line 59 was shut down to prevent any further release of product. All crude oil was contained within the sample building, which was cleaned up and properly disposed of. The probe cap was tightened and the line was restarted. The area was monitored and no further releases occurred. The investigation determined the release was due to the sample probe cap not being properly tightened prior to shipping.

All rights reserved. Copyright © by ClearPHMSA