HL incident on 2019-05-11 — TX

Operator
Permian Express Partners Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,000
Incident datetime
2019-05-11 09:49
Report number
Location
TX
Narrative
On 5/11/19 at approximately 9:49 am, field personnel found oil on the surface near the pe2 outbound/inbound meter. The control room was notified at 9:50 am and the pipeline was shutdown. The meter relief line was determined to be the source of the release. The line was isolated for repairs and remediation of surrounding soil. Upon excavation it was discovered that the failure was due to an internal corrosion pinhole at the 6 o'clock position. A plidco clamp was installed and on 5/12/18 at 3:35 am, the pipeline was returned to service. All free product was recovered and contaminated soil is being remediated on-site. Clean backfill and gravel was brought in. Failed section will be cut out and replaced at a later date.
Detailed record list
Report Received Date
2019-06-06 00:00:00
Iyear
2019
Report Number
20190178
Supplemental Number
32246
Report Type
Original Final
Operator Id
Name
Permian Express Partners Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-05-11 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
20
Recovered Bbls
20
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-05-11 09:49:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-05-11 09:50:00
Restart Datetime
2019-05-12 03:35:00
On Site Datetime
2019-05-11 09:49:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Colorado City Station
Segment Name
Pe2 Colorado City Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Hermleigh
Onshore County Name
Scurry
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
96
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Pipe Wall Thickness
0.375
Pipe Smys
65000
Pipe Specification
Api 5l
Pipe Seam Type
Dsaw
Pipe Manufacturer
Stupp
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2015
Manufactured Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1200
Est Cost Prop Damage
4000
Est Cost Emergency
20000
Est Cost Environmental
1000
Est Cost Other
0
Prpty
26200
Accident Psig
45
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** N*******
Preparer Title
Sr. Manager - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Preparer Fax
877-917-0448
Prepared Date
2019-05-31 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Sr. Manager - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 5/11/19 at approximately 9:49 am, field personnel found oil on the surface near the pe2 outbound/inbound meter. The control room was notified at 9:50 am and the pipeline was shutdown. The meter relief line was determined to be the source of the release. The line was isolated for repairs and remediation of surrounding soil. Upon excavation it was discovered that the failure was due to an internal corrosion pinhole at the 6 o'clock position. A plidco clamp was installed and on 5/12/18 at 3:35 am, the pipeline was returned to service. All free product was recovered and contaminated soil is being remediated on-site. Clean backfill and gravel was brought in. Failed section will be cut out and replaced at a later date.
Report Received Date 2019-06-06 00:00:00
Iyear 2019
Report Number 20190178
Supplemental Number 32246
Report Type Original Final
Operator Id 39596 PHMSA Enforcement
Name Permian Express Partners Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-05-11 09:30:00
Location Latitude 32.5303 Google Maps OpenStreetMap
Location Longitude -100.8297 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 20
Recovered Bbls 20
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-05-11 09:49:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-05-11 09:50:00
Restart Datetime 2019-05-12 03:35:00
On Site Datetime 2019-05-11 09:49:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Colorado City Station
Segment Name Pe2 Colorado City Station
Onshore State Abbreviation Tx
Onshore Postal Code 79526
Onshore City Name Hermleigh
Onshore County Name Scurry
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 96
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 20
Pipe Wall Thickness 0.375
Pipe Smys 65000
Pipe Specification Api 5l
Pipe Seam Type Dsaw
Pipe Manufacturer Stupp
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2015
Manufactured Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1200
Est Cost Prop Damage 4000
Est Cost Emergency 20000
Est Cost Environmental 1000
Est Cost Other 0
Prpty 26200
Accident Psig 45
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** N*******
Preparer Title Sr. Manager - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Preparer Fax 877-917-0448
Prepared Date 2019-05-31 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Sr. Manager - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 5/11/19 at approximately 9:49 am, field personnel found oil on the surface near the pe2 outbound/inbound meter. The control room was notified at 9:50 am and the pipeline was shutdown. The meter relief line was determined to be the source of the release. The line was isolated for repairs and remediation of surrounding soil. Upon excavation it was discovered that the failure was due to an internal corrosion pinhole at the 6 o'clock position. A plidco clamp was installed and on 5/12/18 at 3:35 am, the pipeline was returned to service. All free product was recovered and contaminated soil is being remediated on-site. Clean backfill and gravel was brought in. Failed section will be cut out and replaced at a later date.

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