HL incident on 2019-05-01 — TX

Operator
Exxonmobil Pipeline Co
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2019-05-01 17:59
Report number
Location
TX
Narrative
Exxonmobil pipeline company (empco) was notified at 5:46pm of a potential leak at the highway 225 surveillance site by a third party. Empco field operations arrived at 5:59pm and confirmed discovery of a valve packing release of chemical grade propylene. The pipeline segment was already isolated and shutdown due to planned recommissioning work from other pipeline maintenance. Field personnel addressed the issue by repacking the valve and stopping the leak at approximately 7:10pm. At the time of discovery, the initial release volume estimate was not determined to meet reportable thresholds. At approximately 8:39pm, engineering calculations produced an estimated total of 1,010 lbs for the chemical grade propylene release, which contained a combination of 939 lbs (5.12 bbls) of propylene and 71 lbs (.38 bbls) of propane. The release was reported to texas spill reporting hotline, reaching texas railroad commission and texas commission of environmental quality, at 8:44 p.M. And then the national response center at 8:53 p.M.
Detailed record list
Report Received Date
2019-05-31 00:00:00
Iyear
2019
Report Number
20190174
Supplemental Number
32225
Report Type
Original Final
Operator Id
Name
Exxonmobil Pipeline Co
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2019-05-01 17:46:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Chemical Grade Propylene
Unintentional Release Bbls
5.49
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third-Party Operator Notified Empco One Call Personnel
Incident Identified Datetime
2019-05-01 17:59:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Segment Was Already Shutdown And Isolated Prior To Event.
On Site Datetime
2019-05-01 17:59:00
Nrc Rpt Datetime
2019-05-01 20:53:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Highway 225 Surveillance Site
Segment Name
Tx-167c 8" Cgp Line
Onshore State Abbreviation
Tx
Onshore Postal Code
77571
Onshore City Name
La Porte
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Mov-Bc5 Valve
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
354
Est Cost Prop Damage
50
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
300
Est Cost Other Details
Labor Cost
Prpty
704
Accident Psig
825
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
49087
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline segment was already isolated and shutdown for recommissioning work.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Valve Packing Leak
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear
Preparer Name
D**** R* S*****
Preparer Title
Pipeline Safety Advisor
Preparer Email
D*************@e*********.com
Preparer Telephone
832-624-7531
Prepared Date
2019-05-31 00:00:00
Authorizer Name
C******* B* H********
Authorizer Telephone
832-624-7920
Authorizer Title
Exxonmobil Pipeline Company Sshe Manager
Authorizer Email
C*******************@e*********.com
Narrative
Exxonmobil pipeline company (empco) was notified at 5:46pm of a potential leak at the highway 225 surveillance site by a third party. Empco field operations arrived at 5:59pm and confirmed discovery of a valve packing release of chemical grade propylene. The pipeline segment was already isolated and shutdown due to planned recommissioning work from other pipeline maintenance. Field personnel addressed the issue by repacking the valve and stopping the leak at approximately 7:10pm. At the time of discovery, the initial release volume estimate was not determined to meet reportable thresholds. At approximately 8:39pm, engineering calculations produced an estimated total of 1,010 lbs for the chemical grade propylene release, which contained a combination of 939 lbs (5.12 bbls) of propylene and 71 lbs (.38 bbls) of propane. The release was reported to texas spill reporting hotline, reaching texas railroad commission and texas commission of environmental quality, at 8:44 p.M. And then the national response center at 8:53 p.M.
Report Received Date 2019-05-31 00:00:00
Iyear 2019
Report Number 20190174
Supplemental Number 32225
Report Type Original Final
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Co
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2019-05-01 17:46:00
Location Latitude 29.694536 Google Maps OpenStreetMap
Location Longitude -95.055497 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Chemical Grade Propylene
Unintentional Release Bbls 5.49
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third-Party Operator Notified Empco One Call Personnel
Incident Identified Datetime 2019-05-01 17:59:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Segment Was Already Shutdown And Isolated Prior To Event.
On Site Datetime 2019-05-01 17:59:00
Nrc Rpt Datetime 2019-05-01 20:53:00
Nrc Rpt Num 1244349 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Highway 225 Surveillance Site
Segment Name Tx-167c 8" Cgp Line
Onshore State Abbreviation Tx
Onshore Postal Code 77571
Onshore City Name La Porte
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Mov-Bc5 Valve
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 354
Est Cost Prop Damage 50
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 300
Est Cost Other Details Labor Cost
Prpty 704
Accident Psig 825
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 49087
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline segment was already isolated and shutdown for recommissioning work.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Valve Packing Leak
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear And Tear
Preparer Name D**** R* S*****
Preparer Title Pipeline Safety Advisor
Preparer Email D*************@e*********.com
Preparer Telephone 832-624-7531
Prepared Date 2019-05-31 00:00:00
Authorizer Name C******* B* H********
Authorizer Telephone 832-624-7920
Authorizer Title Exxonmobil Pipeline Company Sshe Manager
Authorizer Email C*******************@e*********.com
Narrative Exxonmobil pipeline company (empco) was notified at 5:46pm of a potential leak at the highway 225 surveillance site by a third party. Empco field operations arrived at 5:59pm and confirmed discovery of a valve packing release of chemical grade propylene. The pipeline segment was already isolated and shutdown due to planned recommissioning work from other pipeline maintenance. Field personnel addressed the issue by repacking the valve and stopping the leak at approximately 7:10pm. At the time of discovery, the initial release volume estimate was not determined to meet reportable thresholds. At approximately 8:39pm, engineering calculations produced an estimated total of 1,010 lbs for the chemical grade propylene release, which contained a combination of 939 lbs (5.12 bbls) of propylene and 71 lbs (.38 bbls) of propane. The release was reported to texas spill reporting hotline, reaching texas railroad commission and texas commission of environmental quality, at 8:44 p.M. And then the national response center at 8:53 p.M.

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