HL incident on 2019-05-01 — TX

Operator
Harvest Midstream Company
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$800
Incident datetime
2019-05-01 06:20
Report number
Location
TX
Narrative
A harvest operator arrived at the three rivers station and found a needle valve associated with the chemical injection quill assembly leaking. The operator immediately notified the control center and the pumps at the station were shut-in until the leak could be stopped. All other appropriate notifications were made. The chemical injector assembly was removed and the valve was closed and plugged. The operator notified the control room and the line was put back into service. Type of event: equipment failure valve failed due to internal corrosion. Direct cause: defective equipment valve material of construction not suitable for intended service. The failed valve was constructed of carbon steel and the recommended material for the injection valve is stainless steel. Root cause: inadequate monitoring of installation visually the valves appears similar to a stainless steel with an identifier stenciled into the body of the valve indicating carbon steel. Corrective actions it was verifired that all other chemical injections valves on the pearsall pipeline system were constructed of the proper material.
Detailed record list
Report Received Date
2019-05-31 00:00:00
Iyear
2019
Report Number
20190173
Supplemental Number
32583
Report Type
Supplemental Final
Operator Id
Name
Harvest Midstream Company
Operator Street Address
1111 Travis
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-05-01 06:20:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-05-01 06:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-05-01 06:25:00
Restart Datetime
2019-05-01 07:07:00
On Site Datetime
2019-05-01 06:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pearsall Oil System
Segment Name
Three Rivers Station
Onshore State Abbreviation
Tx
Onshore Postal Code
78071
Onshore City Name
Three Rivers
Onshore County Name
Live Oak
Designated Location
Milepost/valve Station
Designated Name
Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Needle Valve Chemical Injection Assembly
Installation Year
2018
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Corrosion
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
120
Est Cost Prop Damage
800
Est Cost Emergency
0
Est Cost Environmental
4000
Est Cost Other
0
Prpty
4920
Accident Psig
1000
Mop Psig
1100
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Equipment failure (corrosion) -needle valve that was part of the chemical injection quill assembly
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Wrong Equipment Specified Or Installed
Operation Type
Wrong Equipment Specified Or Installed
Related Inadequate Proc Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
T*** S* B****
Preparer Title
Sr. Regulatory Compliance Specialist
Preparer Email
T******@h***************.com
Preparer Telephone
713.289.2688
Prepared Date
2019-08-20 00:00:00
Authorizer Name
T*** S* B****
Authorizer Telephone
713.289.2688
Authorizer Title
Sr. Regulatory Compliance Specialist
Authorizer Email
T******@h***************.com
Narrative
A harvest operator arrived at the three rivers station and found a needle valve associated with the chemical injection quill assembly leaking. The operator immediately notified the control center and the pumps at the station were shut-in until the leak could be stopped. All other appropriate notifications were made. The chemical injector assembly was removed and the valve was closed and plugged. The operator notified the control room and the line was put back into service. Type of event: equipment failure valve failed due to internal corrosion. Direct cause: defective equipment valve material of construction not suitable for intended service. The failed valve was constructed of carbon steel and the recommended material for the injection valve is stainless steel. Root cause: inadequate monitoring of installation visually the valves appears similar to a stainless steel with an identifier stenciled into the body of the valve indicating carbon steel. Corrective actions it was verifired that all other chemical injections valves on the pearsall pipeline system were constructed of the proper material.
Report Received Date 2019-05-31 00:00:00
Iyear 2019
Report Number 20190173
Supplemental Number 32583
Report Type Supplemental Final
Operator Id 30782 PHMSA Enforcement
Name Harvest Midstream Company
Operator Street Address 1111 Travis
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-05-01 06:20:00
Location Latitude 28.40872 Google Maps OpenStreetMap
Location Longitude -98.21365 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-05-01 06:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-05-01 06:25:00
Restart Datetime 2019-05-01 07:07:00
On Site Datetime 2019-05-01 06:20:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Pearsall Oil System
Segment Name Three Rivers Station
Onshore State Abbreviation Tx
Onshore Postal Code 78071
Onshore City Name Three Rivers
Onshore County Name Live Oak
Designated Location Milepost/valve Station
Designated Name Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Needle Valve Chemical Injection Assembly
Installation Year 2018
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Corrosion
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 120
Est Cost Prop Damage 800
Est Cost Emergency 0
Est Cost Environmental 4000
Est Cost Other 0
Prpty 4920
Accident Psig 1000
Mop Psig 1100
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Equipment failure (corrosion) -needle valve that was part of the chemical injection quill assembly
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Wrong Equipment Specified Or Installed
Operation Type Wrong Equipment Specified Or Installed
Related Inadequate Proc Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name T*** S* B****
Preparer Title Sr. Regulatory Compliance Specialist
Preparer Email T******@h***************.com
Preparer Telephone 713.289.2688
Prepared Date 2019-08-20 00:00:00
Authorizer Name T*** S* B****
Authorizer Telephone 713.289.2688
Authorizer Title Sr. Regulatory Compliance Specialist
Authorizer Email T******@h***************.com
Narrative A harvest operator arrived at the three rivers station and found a needle valve associated with the chemical injection quill assembly leaking. The operator immediately notified the control center and the pumps at the station were shut-in until the leak could be stopped. All other appropriate notifications were made. The chemical injector assembly was removed and the valve was closed and plugged. The operator notified the control room and the line was put back into service. Type of event: equipment failure valve failed due to internal corrosion. Direct cause: defective equipment valve material of construction not suitable for intended service. The failed valve was constructed of carbon steel and the recommended material for the injection valve is stainless steel. Root cause: inadequate monitoring of installation visually the valves appears similar to a stainless steel with an identifier stenciled into the body of the valve indicating carbon steel. Corrective actions it was verifired that all other chemical injections valves on the pearsall pipeline system were constructed of the proper material.

All rights reserved. Copyright © by ClearPHMSA