HL incident on 2019-05-04 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$350
Incident datetime
2019-05-04 12:15
Report number
Location
TX
Narrative
At approximately 2300 hrs. On may 3rd, 2019. Energy transfer liquids control received indications of a leak at pump station # 3 on the s505 west texas gateway 16" ngl pipeline. Energy transfer liquids control contacted etc operations field personnel to investigate. Operations technicians arrived on location at 12:15 hrs. On 5/4 and found a leak on some tubing in the station. At 01:25 hrs. The technicians were able to isolate the leak location by closing valves 7 & 8 on pump # 3 to allow the isolated leak section to blow down. An investigation found the 1/2" tubing from a thermal relief on the discharge valve on pump # 3 to be loose at the fitting. All tubing and fittings on the discharge valve were removed and replaced. The isolation valves (7 & 8) were opened at 03:41 hrs. And the station was available for normal service at 04:00 hrs. The initial report was made to the nrc at 01:59 hrs. On may 4, 2019, report # 1244598 and the nrc 48 hr. Update was made at 20:00 hrs. On may 5, 2019, report # 1244739 etc's plan to prevent reoccurrences of this issue were to replace all tubing and fittings on the discharge valve and check the tubing and fittings throughout the entire station.
Detailed record list
Report Received Date
2019-05-30 00:00:00
Iyear
2019
Report Number
20190172
Supplemental Number
32218
Report Type
Original Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-05-03 23:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
243
Intentional Release Bbls
49.7
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2019-05-04 12:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-05-03 23:00:00
Restart Datetime
2019-05-04 04:00:00
On Site Datetime
2019-05-04 12:15:00
Nrc Rpt Datetime
2019-05-04 01:59:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
S505 West Tx Gateway 16"
Segment Name
Pump Station # 3
Onshore State Abbreviation
Tx
Onshore Postal Code
76943
Onshore City Name
Rural Location, Ozona Is Nearest City
Onshore County Name
Crockett
Designated Location
Milepost/valve Station
Designated Name
92.2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2012
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
6105
Est Cost Prop Damage
350
Est Cost Emergency
1300
Est Cost Environmental
0
Est Cost Other
500
Est Cost Other Details
Donation To Local Volunteer Fire Department For Support
Prpty
8255
Accident Psig
1267
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controllers actions were in accordance with our standard operating procedures and were appropriate for this event
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
Tubing Came Loose During Normal Operation
Preparer Name
C**** K*****
Preparer Title
Manager - Regulatory Compliance
Preparer Email
C***********@e*************.com
Preparer Telephone
979-531-9036
Prepared Date
2019-05-29 00:00:00
Authorizer Name
C**** K*****
Authorizer Telephone
979-531-9036
Authorizer Title
Manager - Regulatory Compliance
Authorizer Email
C***********@e*************.com
Narrative
At approximately 2300 hrs. On may 3rd, 2019. Energy transfer liquids control received indications of a leak at pump station # 3 on the s505 west texas gateway 16" ngl pipeline. Energy transfer liquids control contacted etc operations field personnel to investigate. Operations technicians arrived on location at 12:15 hrs. On 5/4 and found a leak on some tubing in the station. At 01:25 hrs. The technicians were able to isolate the leak location by closing valves 7 & 8 on pump # 3 to allow the isolated leak section to blow down. An investigation found the 1/2" tubing from a thermal relief on the discharge valve on pump # 3 to be loose at the fitting. All tubing and fittings on the discharge valve were removed and replaced. The isolation valves (7 & 8) were opened at 03:41 hrs. And the station was available for normal service at 04:00 hrs. The initial report was made to the nrc at 01:59 hrs. On may 4, 2019, report # 1244598 and the nrc 48 hr. Update was made at 20:00 hrs. On may 5, 2019, report # 1244739 etc's plan to prevent reoccurrences of this issue were to replace all tubing and fittings on the discharge valve and check the tubing and fittings throughout the entire station.
Report Received Date 2019-05-30 00:00:00
Iyear 2019
Report Number 20190172
Supplemental Number 32218
Report Type Original Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-05-03 23:00:00
Location Latitude 30.68425 Google Maps OpenStreetMap
Location Longitude -101.27124 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 243
Intentional Release Bbls 49.7
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2019-05-04 12:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-05-03 23:00:00
Restart Datetime 2019-05-04 04:00:00
On Site Datetime 2019-05-04 12:15:00
Nrc Rpt Datetime 2019-05-04 01:59:00
Nrc Rpt Num 1244598 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name S505 West Tx Gateway 16"
Segment Name Pump Station # 3
Onshore State Abbreviation Tx
Onshore Postal Code 76943
Onshore City Name Rural Location, Ozona Is Nearest City
Onshore County Name Crockett
Designated Location Milepost/valve Station
Designated Name 92.2
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2012
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 6105
Est Cost Prop Damage 350
Est Cost Emergency 1300
Est Cost Environmental 0
Est Cost Other 500
Est Cost Other Details Donation To Local Volunteer Fire Department For Support
Prpty 8255
Accident Psig 1267
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controllers actions were in accordance with our standard operating procedures and were appropriate for this event
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details Tubing Came Loose During Normal Operation
Preparer Name C**** K*****
Preparer Title Manager - Regulatory Compliance
Preparer Email C***********@e*************.com
Preparer Telephone 979-531-9036
Prepared Date 2019-05-29 00:00:00
Authorizer Name C**** K*****
Authorizer Telephone 979-531-9036
Authorizer Title Manager - Regulatory Compliance
Authorizer Email C***********@e*************.com
Narrative At approximately 2300 hrs. On may 3rd, 2019. Energy transfer liquids control received indications of a leak at pump station # 3 on the s505 west texas gateway 16" ngl pipeline. Energy transfer liquids control contacted etc operations field personnel to investigate. Operations technicians arrived on location at 12:15 hrs. On 5/4 and found a leak on some tubing in the station. At 01:25 hrs. The technicians were able to isolate the leak location by closing valves 7 & 8 on pump # 3 to allow the isolated leak section to blow down. An investigation found the 1/2" tubing from a thermal relief on the discharge valve on pump # 3 to be loose at the fitting. All tubing and fittings on the discharge valve were removed and replaced. The isolation valves (7 & 8) were opened at 03:41 hrs. And the station was available for normal service at 04:00 hrs. The initial report was made to the nrc at 01:59 hrs. On may 4, 2019, report # 1244598 and the nrc 48 hr. Update was made at 20:00 hrs. On may 5, 2019, report # 1244739 etc's plan to prevent reoccurrences of this issue were to replace all tubing and fittings on the discharge valve and check the tubing and fittings throughout the entire station.

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