HL incident on 2019-04-25 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2019-04-25 13:30
Report number
Location
TX
Narrative
On 4/25/2019 at approximately 13:00, aerial patrol was flying the 20" wortham to longview segment and noted crude oil on the ground at leagueville station. The pilot notified field personnel. Upon arrival on site field personnel noted approximately 2 bbls of crude oil out at the pump location and notified control center immediately. The pipeline was shutdown at 13:30. Upon investigation, the inboard seal on the mainline pump had failed due to an unknown cause. Additionally, a faulty connection was discovered on the seal pot alarm. Under normal circumstances the seal pot would alarm and pump would shut down automatically. The faulty connection to the seal pot alarm allowed the pump to continue running and excess crude oil to be released from the pump seal area. The seal pot alarm was repaired and the pump seal was replaced. All free product was recovered and contaminated soil is being remediated onsite. Other mainline pump unit at leagueville was inspected for pump seal and seal pot alarm issues and none were found. Upon replacement of the seal and repair of the seal pot alarm, control center was notified at 15:30 to restart the line. Area was visually monitored to assure normal startup and no to verify no additional issues existed.
Detailed record list
Report Received Date
2019-05-22 00:00:00
Iyear
2019
Report Number
20190165
Supplemental Number
32180
Report Type
Original Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-04-25 13:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2019-04-25 13:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-04-25 13:30:00
Restart Datetime
2019-04-25 15:30:00
On Site Datetime
2019-04-25 13:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
20" Wortham To Longview
Segment Name
22001
Onshore State Abbreviation
Tx
Onshore Postal Code
75778
Onshore City Name
Leagueville
Onshore County Name
Henderson
Designated Location
Survey Station No.
Designated Name
282875.7
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2016
Material Involved
Material Other Than Carbon Steel
Material Details
Viton
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
130
Est Cost Prop Damage
1500
Est Cost Emergency
1000
Est Cost Environmental
4370
Est Cost Other
0
Prpty
7000
Accident Psig
246
Mop Psig
815
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Unknown
Preparer Name
T*** N*******
Preparer Title
Sr. Manager - Dot Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Preparer Fax
877-917-0448
Prepared Date
2019-05-22 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Sr. Manager - Dot Compliance
Authorizer Email
T************@e*************.com
Narrative
On 4/25/2019 at approximately 13:00, aerial patrol was flying the 20" wortham to longview segment and noted crude oil on the ground at leagueville station. The pilot notified field personnel. Upon arrival on site field personnel noted approximately 2 bbls of crude oil out at the pump location and notified control center immediately. The pipeline was shutdown at 13:30. Upon investigation, the inboard seal on the mainline pump had failed due to an unknown cause. Additionally, a faulty connection was discovered on the seal pot alarm. Under normal circumstances the seal pot would alarm and pump would shut down automatically. The faulty connection to the seal pot alarm allowed the pump to continue running and excess crude oil to be released from the pump seal area. The seal pot alarm was repaired and the pump seal was replaced. All free product was recovered and contaminated soil is being remediated onsite. Other mainline pump unit at leagueville was inspected for pump seal and seal pot alarm issues and none were found. Upon replacement of the seal and repair of the seal pot alarm, control center was notified at 15:30 to restart the line. Area was visually monitored to assure normal startup and no to verify no additional issues existed.
Report Received Date 2019-05-22 00:00:00
Iyear 2019
Report Number 20190165
Supplemental Number 32180
Report Type Original Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-04-25 13:00:00
Location Latitude 32.23139 Google Maps OpenStreetMap
Location Longitude -95.66336 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2019-04-25 13:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-04-25 13:30:00
Restart Datetime 2019-04-25 15:30:00
On Site Datetime 2019-04-25 13:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name 20" Wortham To Longview
Segment Name 22001
Onshore State Abbreviation Tx
Onshore Postal Code 75778
Onshore City Name Leagueville
Onshore County Name Henderson
Designated Location Survey Station No.
Designated Name 282875.7
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2016
Material Involved Material Other Than Carbon Steel
Material Details Viton
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 130
Est Cost Prop Damage 1500
Est Cost Emergency 1000
Est Cost Environmental 4370
Est Cost Other 0
Prpty 7000
Accident Psig 246
Mop Psig 815
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Unknown
Preparer Name T*** N*******
Preparer Title Sr. Manager - Dot Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Preparer Fax 877-917-0448
Prepared Date 2019-05-22 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Sr. Manager - Dot Compliance
Authorizer Email T************@e*************.com
Narrative On 4/25/2019 at approximately 13:00, aerial patrol was flying the 20" wortham to longview segment and noted crude oil on the ground at leagueville station. The pilot notified field personnel. Upon arrival on site field personnel noted approximately 2 bbls of crude oil out at the pump location and notified control center immediately. The pipeline was shutdown at 13:30. Upon investigation, the inboard seal on the mainline pump had failed due to an unknown cause. Additionally, a faulty connection was discovered on the seal pot alarm. Under normal circumstances the seal pot would alarm and pump would shut down automatically. The faulty connection to the seal pot alarm allowed the pump to continue running and excess crude oil to be released from the pump seal area. The seal pot alarm was repaired and the pump seal was replaced. All free product was recovered and contaminated soil is being remediated onsite. Other mainline pump unit at leagueville was inspected for pump seal and seal pot alarm issues and none were found. Upon replacement of the seal and repair of the seal pot alarm, control center was notified at 15:30 to restart the line. Area was visually monitored to assure normal startup and no to verify no additional issues existed.

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