HL incident on 2019-04-21 — KS

Operator
Flint Hills Resources, Lc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2019-04-21 07:43
Report number
Location
KS
Narrative
Updated section g, questions 7 & 8 of the internal corrosion section and also included a summary of the laboratory results below. On 04/21/2019 at approximately 7:43 am, fhr operations personnel discovered a crude oil release at helena terminal. At approximately 7:45 am, the source of the leak was verified and the pipeline control center was contacted to shut down the outbound helena to pettus 16", index #60501020. The pcc blocked in the station tank valve and the incoming trap valve at pettus station at 7:51 am. Fhr personnel initiated air monitoring, no lel or h2s levels were found. The pcc opened the line into pettus tank to allow the line to de-pressurize. At approximately 8:16 am, fhr personnel deployed boom in the area to keep product onsite. At approximately 8:44 am, the nrc (#1243321) and texas railroad commission office of pipeline safety were notified. The impacted pipe section was cut out and replaced the morning of 04/22/2019 and pipe was sent to dnv lab for analysis. The dnv immediate cause analysis report indicates that the leak occurred due to internal corrosion that propagated through-wall at the 6:00 orientation. The leak was associated with a discrete pit and was located within an area of accumulated solids. The system was started back up at 6:45 pm on 04/22/2019. Clean up was completed at helena station on 04/25/2019.
Detailed record list
Report Received Date
2019-05-20 00:00:00
Iyear
2019
Report Number
20190162
Supplemental Number
33197
Report Type
Supplemental Final
Operator Id
Name
Flint Hills Resources, Lc
Operator Street Address
4111 East 37th Street North
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67220
Local Datetime
2019-04-20 12:32:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
56
Recovered Bbls
52
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-04-21 07:43:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-04-21 07:47:00
Restart Datetime
2019-04-22 18:45:00
On Site Datetime
2019-04-21 07:43:00
Nrc Rpt Datetime
2019-04-21 08:44:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Helena Receipt Terminal/station
Segment Name
Segment Id # 60501020 Helena To Pettus/tomlinson
Onshore State Abbreviation
Tx
Onshore Postal Code
78118
Onshore City Name
Karnes City
Onshore County Name
Karnes
Designated Location
Milepost/valve Station
Designated Name
0+0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.322
Pipe Smys
52000
Pipe Specification
Api 5l X52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Tenaris
Pipe Coating Type
Paint
Installation Year
2011
Manufactured Year
2011
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
276
Est Cost Prop Damage
5000
Est Cost Emergency
178570
Est Cost Environmental
10000
Est Cost Other
0
Prpty
193846
Accident Psig
675
Mop Psig
1462
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
It was determined that neither controller actions nor control room issues contributed to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
General Corrosion
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Low Or Intermittent Flow Segment
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
M**** T*****
Preparer Title
Senior Compliance Specialist
Preparer Email
M***********@f**.com
Preparer Telephone
409-273-9482
Preparer Fax
409-989-6450
Prepared Date
2020-01-16 00:00:00
Authorizer Name
M**** T*****
Authorizer Telephone
409-273-9482
Authorizer Title
Senior Compliance Specialist
Authorizer Email
M***********@f**.com
Narrative
Updated section g, questions 7 & 8 of the internal corrosion section and also included a summary of the laboratory results below. On 04/21/2019 at approximately 7:43 am, fhr operations personnel discovered a crude oil release at helena terminal. At approximately 7:45 am, the source of the leak was verified and the pipeline control center was contacted to shut down the outbound helena to pettus 16", index #60501020. The pcc blocked in the station tank valve and the incoming trap valve at pettus station at 7:51 am. Fhr personnel initiated air monitoring, no lel or h2s levels were found. The pcc opened the line into pettus tank to allow the line to de-pressurize. At approximately 8:16 am, fhr personnel deployed boom in the area to keep product onsite. At approximately 8:44 am, the nrc (#1243321) and texas railroad commission office of pipeline safety were notified. The impacted pipe section was cut out and replaced the morning of 04/22/2019 and pipe was sent to dnv lab for analysis. The dnv immediate cause analysis report indicates that the leak occurred due to internal corrosion that propagated through-wall at the 6:00 orientation. The leak was associated with a discrete pit and was located within an area of accumulated solids. The system was started back up at 6:45 pm on 04/22/2019. Clean up was completed at helena station on 04/25/2019.
Report Received Date 2019-05-20 00:00:00
Iyear 2019
Report Number 20190162
Supplemental Number 33197
Report Type Supplemental Final
Operator Id 22855 PHMSA Enforcement
Name Flint Hills Resources, Lc
Operator Street Address 4111 East 37th Street North
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67220
Local Datetime 2019-04-20 12:32:00
Location Latitude 28.937256 Google Maps OpenStreetMap
Location Longitude -97.798827 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 56
Recovered Bbls 52
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-04-21 07:43:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-04-21 07:47:00
Restart Datetime 2019-04-22 18:45:00
On Site Datetime 2019-04-21 07:43:00
Nrc Rpt Datetime 2019-04-21 08:44:00
Nrc Rpt Num 1243321 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Helena Receipt Terminal/station
Segment Name Segment Id # 60501020 Helena To Pettus/tomlinson
Onshore State Abbreviation Tx
Onshore Postal Code 78118
Onshore City Name Karnes City
Onshore County Name Karnes
Designated Location Milepost/valve Station
Designated Name 0+0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.322
Pipe Smys 52000
Pipe Specification Api 5l X52
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Tenaris
Pipe Coating Type Paint
Installation Year 2011
Manufactured Year 2011
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 276
Est Cost Prop Damage 5000
Est Cost Emergency 178570
Est Cost Environmental 10000
Est Cost Other 0
Prpty 193846
Accident Psig 675
Mop Psig 1462
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details It was determined that neither controller actions nor control room issues contributed to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results General Corrosion
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Low Or Intermittent Flow Segment
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name M**** T*****
Preparer Title Senior Compliance Specialist
Preparer Email M***********@f**.com
Preparer Telephone 409-273-9482
Preparer Fax 409-989-6450
Prepared Date 2020-01-16 00:00:00
Authorizer Name M**** T*****
Authorizer Telephone 409-273-9482
Authorizer Title Senior Compliance Specialist
Authorizer Email M***********@f**.com
Narrative Updated section g, questions 7 & 8 of the internal corrosion section and also included a summary of the laboratory results below. On 04/21/2019 at approximately 7:43 am, fhr operations personnel discovered a crude oil release at helena terminal. At approximately 7:45 am, the source of the leak was verified and the pipeline control center was contacted to shut down the outbound helena to pettus 16", index #60501020. The pcc blocked in the station tank valve and the incoming trap valve at pettus station at 7:51 am. Fhr personnel initiated air monitoring, no lel or h2s levels were found. The pcc opened the line into pettus tank to allow the line to de-pressurize. At approximately 8:16 am, fhr personnel deployed boom in the area to keep product onsite. At approximately 8:44 am, the nrc (#1243321) and texas railroad commission office of pipeline safety were notified. The impacted pipe section was cut out and replaced the morning of 04/22/2019 and pipe was sent to dnv lab for analysis. The dnv immediate cause analysis report indicates that the leak occurred due to internal corrosion that propagated through-wall at the 6:00 orientation. The leak was associated with a discrete pit and was located within an area of accumulated solids. The system was started back up at 6:45 pm on 04/22/2019. Clean up was completed at helena station on 04/25/2019.

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