HL incident on 2019-04-18 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2019-04-18 08:40
Report number
Location
TX
Narrative
On 4/18/2018 at 08:40 hrs, control center started up line after meter strainer was cleaned the previous day. At 0845 hrs, control center received a containment high level alarm and called a station technician to confirm. Technician responded to location and identified that a body bleed valve was incorrectly opened from previous day's maintenance activities. To prevent recurrence, the incorrectly followed maintenance procedure was reviewed with area personnel in an area safety meeting on 8/20/2019. Texas rrc incident #1973.
Detailed record list
Report Received Date
2019-05-16 00:00:00
Iyear
2019
Report Number
20190159
Supplemental Number
32667
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-04-18 08:40:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Condensate
Unintentional Release Bbls
0.36
Recovered Bbls
0.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2019-04-18 08:40:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-04-18 09:04:00
Restart Datetime
2019-04-18 15:24:00
On Site Datetime
2019-04-18 09:02:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cgp71b To Milton
Segment Name
C93d
Onshore State Abbreviation
Tx
Onshore Postal Code
78116
Onshore City Name
Gillett
Onshore County Name
Karnes County
Designated Location
Milepost/valve Station
Designated Name
Meter 2500
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Meter/prover
Installation Year
2017
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Other
Release Type Details
Incorrect Valve Setting Upon Restart Of Pipeline.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
0
Est Cost Emergency
100
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Operator Cleaned Up Material With Pads.
Prpty
150
Accident Psig
56
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No indication of control room causing incident.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
R*** T********
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2019-09-05 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-5585
Authorizer Title
Compliance Manager
Authorizer Email
S******@e****.com
Narrative
On 4/18/2018 at 08:40 hrs, control center started up line after meter strainer was cleaned the previous day. At 0845 hrs, control center received a containment high level alarm and called a station technician to confirm. Technician responded to location and identified that a body bleed valve was incorrectly opened from previous day's maintenance activities. To prevent recurrence, the incorrectly followed maintenance procedure was reviewed with area personnel in an area safety meeting on 8/20/2019. Texas rrc incident #1973.
Report Received Date 2019-05-16 00:00:00
Iyear 2019
Report Number 20190159
Supplemental Number 32667
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-04-18 08:40:00
Location Latitude 29.05436 Google Maps OpenStreetMap
Location Longitude -97.79099 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Condensate
Unintentional Release Bbls 0.36
Recovered Bbls 0.36
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2019-04-18 08:40:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-04-18 09:04:00
Restart Datetime 2019-04-18 15:24:00
On Site Datetime 2019-04-18 09:02:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cgp71b To Milton
Segment Name C93d
Onshore State Abbreviation Tx
Onshore Postal Code 78116
Onshore City Name Gillett
Onshore County Name Karnes County
Designated Location Milepost/valve Station
Designated Name Meter 2500
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Meter/prover
Installation Year 2017
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Other
Release Type Details Incorrect Valve Setting Upon Restart Of Pipeline.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 0
Est Cost Emergency 100
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Operator Cleaned Up Material With Pads.
Prpty 150
Accident Psig 56
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No indication of control room causing incident.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name R*** T********
Preparer Title Pipeline Compliance Engineer
Preparer Email R*********@e****.com
Preparer Telephone 713-381-4659
Prepared Date 2019-09-05 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713-381-5585
Authorizer Title Compliance Manager
Authorizer Email S******@e****.com
Narrative On 4/18/2018 at 08:40 hrs, control center started up line after meter strainer was cleaned the previous day. At 0845 hrs, control center received a containment high level alarm and called a station technician to confirm. Technician responded to location and identified that a body bleed valve was incorrectly opened from previous day's maintenance activities. To prevent recurrence, the incorrectly followed maintenance procedure was reviewed with area personnel in an area safety meeting on 8/20/2019. Texas rrc incident #1973.

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