HL incident on 2019-04-21 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5
Incident datetime
2019-04-21 17:30
Report number
Location
TX
Narrative
On 04/21/2019 at approximately 17:30, contractor discovered a 2" recirculation nozzle flanged connection on tank 390-105 leaked approximately 4 bbls of crude oil onto the ground. Contractor notified enterprise employee who tightened bolts on the flange and stopped the leak. Remediation was completed on 04/23/2019. Investigation determined the gasket was ansi 300 installed on an ansi 150 flange. Mismatched bolt holes were forced to fit and tightened to seal. Over time this cracked the gasket causing the leak. All gaskets on the 2" recirculation nozzle flanges on this tank were replaced and gaskets on flanged connections on other tanks were inspected.
Detailed record list
Report Received Date
2019-05-16 00:00:00
Iyear
2019
Report Number
20190158
Supplemental Number
32240
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2019-04-21 17:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2019-04-21 17:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Operator Employee Tightened Connection To Stop Leak
On Site Datetime
2019-04-21 17:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Appelt Tank Farm
Segment Name
Tank 390-105
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Tank Farm
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Compressed Fiber
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
240
Est Cost Prop Damage
5
Est Cost Emergency
0
Est Cost Environmental
44535
Est Cost Other
0
Prpty
44780
Accident Psig
20
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room personnel and procedures did not contribute to accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Preparer Name
D**** B*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
D*******@e****.com
Preparer Telephone
713-381-5647
Prepared Date
2019-06-05 00:00:00
Authorizer Name
D**** B*****
Authorizer Telephone
713-381-5647
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
D*******@e****.com
Narrative
On 04/21/2019 at approximately 17:30, contractor discovered a 2" recirculation nozzle flanged connection on tank 390-105 leaked approximately 4 bbls of crude oil onto the ground. Contractor notified enterprise employee who tightened bolts on the flange and stopped the leak. Remediation was completed on 04/23/2019. Investigation determined the gasket was ansi 300 installed on an ansi 150 flange. Mismatched bolt holes were forced to fit and tightened to seal. Over time this cracked the gasket causing the leak. All gaskets on the 2" recirculation nozzle flanges on this tank were replaced and gaskets on flanged connections on other tanks were inspected.
Report Received Date 2019-05-16 00:00:00
Iyear 2019
Report Number 20190158
Supplemental Number 32240
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2019-04-21 17:30:00
Location Latitude 29.7602 Google Maps OpenStreetMap
Location Longitude -95.1429 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2019-04-21 17:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Operator Employee Tightened Connection To Stop Leak
On Site Datetime 2019-04-21 17:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Appelt Tank Farm
Segment Name Tank 390-105
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Tank Farm
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Compressed Fiber
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 240
Est Cost Prop Damage 5
Est Cost Emergency 0
Est Cost Environmental 44535
Est Cost Other 0
Prpty 44780
Accident Psig 20
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room personnel and procedures did not contribute to accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Installation Ind Yes
Preparer Name D**** B*****
Preparer Title Pipeline Compliance Engineer
Preparer Email D*******@e****.com
Preparer Telephone 713-381-5647
Prepared Date 2019-06-05 00:00:00
Authorizer Name D**** B*****
Authorizer Telephone 713-381-5647
Authorizer Title Pipeline Compliance Engineer
Authorizer Email D*******@e****.com
Narrative On 04/21/2019 at approximately 17:30, contractor discovered a 2" recirculation nozzle flanged connection on tank 390-105 leaked approximately 4 bbls of crude oil onto the ground. Contractor notified enterprise employee who tightened bolts on the flange and stopped the leak. Remediation was completed on 04/23/2019. Investigation determined the gasket was ansi 300 installed on an ansi 150 flange. Mismatched bolt holes were forced to fit and tightened to seal. Over time this cracked the gasket causing the leak. All gaskets on the 2" recirculation nozzle flanges on this tank were replaced and gaskets on flanged connections on other tanks were inspected.

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