Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2019-04-17 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$10,000
Incident datetime
2019-04-17 10:00
Report number
Location
OK
Narrative
A third party pipeline operator inspecting their right-of-way within the shared pipeline corridor observed potential product on the ground. Local magellan personnel were contacted and operations control was notified. Investigative events procedures were implemented and resources responded to the site. Operations control initiated shutdown procedures on all magellan pipelines in the corridor and isolation valves were closed. While excavating impacted soil was found, collected, and containerized for proper disposal. The release originated from a pinhole in the longitudinal seam. The release was repaired with a type b sleeve. An additional sleeve was installed to repair other potential lack of fusion features within the joint. The inline inspection vendor for the 2014 multi-dataset ili run reviewed data signals in the vicinity of the release. No similar features were identified through the signal review process. Supplemental/final (05/21/2019): part a 5 latitude/longitude supplemental/final (01/21/2020): part e 2 maximum operating pressure (mop) correction
Detailed record list
Report Received Date
2019-05-15 00:00:00
Iyear
2019
Report Number
20190155
Supplemental Number
33213
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2019-04-17 10:00:00
Location Latitude
38.847215
Location Longitude
-94.744678
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.7
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Notification From Third Party
Incident Identified Datetime
2019-04-17 10:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-04-17 10:15:00
Restart Datetime
2019-04-19 02:22:00
On Site Datetime
2019-04-17 10:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Barnsdall-Kansas City No. 4-12" Line
Segment Name
Line Id 6025
Onshore State Abbreviation
Ks
Onshore Postal Code
66062
Onshore City Name
Olathe
Onshore County Name
Joohnson
Designated Location
Milepost/valve Station
Designated Name
176.61
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
32
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
12
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api5lx-42
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Coal Tar
Installation Year
1950
Manufactured Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
2500
Est Cost Gas Released
61
Est Cost Prop Damage
10000
Est Cost Emergency
20000
Est Cost Environmental
0
Est Cost Other
0
Prpty
32561
Accident Psig
151
Mop Psig
1186
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
146256
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Operations control personnel did not cause or contribute to this release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Lack Of Fusion
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Other Tool Tech Ind
Yes
Circ Wave Recent Year
2014
Other Tool
Multi-Data Set
Other Recent Year
2014
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1989
Hydrtst Most Rcnt Pressure
1858
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-01-21 00:00:00
Authorizer Name
S**** H******
Authorizer Telephone
918-574-7173
Authorizer Title
Supervisor Integrity Management
Authorizer Email
S************@m*********.com
Narrative
A third party pipeline operator inspecting their right-of-way within the shared pipeline corridor observed potential product on the ground. Local magellan personnel were contacted and operations control was notified. Investigative events procedures were implemented and resources responded to the site. Operations control initiated shutdown procedures on all magellan pipelines in the corridor and isolation valves were closed. While excavating impacted soil was found, collected, and containerized for proper disposal. The release originated from a pinhole in the longitudinal seam. The release was repaired with a type b sleeve. An additional sleeve was installed to repair other potential lack of fusion features within the joint. The inline inspection vendor for the 2014 multi-dataset ili run reviewed data signals in the vicinity of the release. No similar features were identified through the signal review process. Supplemental/final (05/21/2019): part a 5 latitude/longitude supplemental/final (01/21/2020): part e 2 maximum operating pressure (mop) correction
| Report Received Date | 2019-05-15 00:00:00 |
|---|---|
| Iyear | 2019 |
| Report Number | 20190155 |
| Supplemental Number | 33213 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2019-04-17 10:00:00 |
| Location Latitude | 38.847215 Google Maps OpenStreetMap |
| Location Longitude | -94.744678 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Mixture Of Refined Products (Transmix Or Other Mixture) |
| Unintentional Release Bbls | 0.7 |
| Recovered Bbls | 0.7 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Other |
| Accident Details | Notification From Third Party |
| Incident Identified Datetime | 2019-04-17 10:00:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2019-04-17 10:15:00 |
| Restart Datetime | 2019-04-19 02:22:00 |
| On Site Datetime | 2019-04-17 10:30:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Upstream Valve Type Ind | Remotely Controlled |
| Downstream Valve Type Ind | Remotely Controlled |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Barnsdall-Kansas City No. 4-12" Line |
| Segment Name | Line Id 6025 |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 66062 |
| Onshore City Name | Olathe |
| Onshore County Name | Joohnson |
| Designated Location | Milepost/valve Station |
| Designated Name | 176.61 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 32 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Pipe |
| Pipe Type | Pipe Seam |
| Pipe Diameter | 12 |
| Pipe Wall Thickness | 0.25 |
| Pipe Smys | 42000 |
| Pipe Specification | Api5lx-42 |
| Pipe Seam Type | Erw - Low Frequency |
| Pipe Manufacturer | Republic Steel |
| Pipe Coating Type | Coal Tar |
| Installation Year | 1950 |
| Manufactured Year | 1950 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 2500 |
| Est Cost Gas Released | 61 |
| Est Cost Prop Damage | 10000 |
| Est Cost Emergency | 20000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 32561 |
| Accident Psig | 151 |
| Mop Psig | 1186 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Length Segment Isolated | 146256 |
| Internal Inspection Ind | Yes |
| Operation Complications Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Operations control personnel did not cause or contribute to this release |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Material Failure Of Pipe Or Weld |
| Cause Details | Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field) |
| Field Exam Ind | Yes |
| Failure Type | Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field) |
| Other Factor | Yes |
| Other Factor Details | Lack Of Fusion |
| Additional Lack Fusion Ind | Yes |
| Collected Data Ind | Yes |
| Cir Trn Wave Mgn Flx Lkg Ind | Yes |
| Other Tool Tech Ind | Yes |
| Circ Wave Recent Year | 2014 |
| Other Tool | Multi-Data Set |
| Other Recent Year | 2014 |
| Has Hydrtst Conduc Before Ind | Yes |
| Hydrtst Most Rcnt Year | 1989 |
| Hydrtst Most Rcnt Pressure | 1858 |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | S****** L****** |
| Preparer Title | Ai Analyst |
| Preparer Email | S**************@m*********.com |
| Preparer Telephone | 918-574-7327 |
| Preparer Fax | 918-574-7376 |
| Prepared Date | 2020-01-21 00:00:00 |
| Authorizer Name | S**** H****** |
| Authorizer Telephone | 918-574-7173 |
| Authorizer Title | Supervisor Integrity Management |
| Authorizer Email | S************@m*********.com |
| Narrative | A third party pipeline operator inspecting their right-of-way within the shared pipeline corridor observed potential product on the ground. Local magellan personnel were contacted and operations control was notified. Investigative events procedures were implemented and resources responded to the site. Operations control initiated shutdown procedures on all magellan pipelines in the corridor and isolation valves were closed. While excavating impacted soil was found, collected, and containerized for proper disposal. The release originated from a pinhole in the longitudinal seam. The release was repaired with a type b sleeve. An additional sleeve was installed to repair other potential lack of fusion features within the joint. The inline inspection vendor for the 2014 multi-dataset ili run reviewed data signals in the vicinity of the release. No similar features were identified through the signal review process. Supplemental/final (05/21/2019): part a 5 latitude/longitude supplemental/final (01/21/2020): part e 2 maximum operating pressure (mop) correction |
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