HL incident on 2019-04-17 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2019-04-17 10:00
Report number
Location
OK
Narrative
A third party pipeline operator inspecting their right-of-way within the shared pipeline corridor observed potential product on the ground. Local magellan personnel were contacted and operations control was notified. Investigative events procedures were implemented and resources responded to the site. Operations control initiated shutdown procedures on all magellan pipelines in the corridor and isolation valves were closed. While excavating impacted soil was found, collected, and containerized for proper disposal. The release originated from a pinhole in the longitudinal seam. The release was repaired with a type b sleeve. An additional sleeve was installed to repair other potential lack of fusion features within the joint. The inline inspection vendor for the 2014 multi-dataset ili run reviewed data signals in the vicinity of the release. No similar features were identified through the signal review process. Supplemental/final (05/21/2019): part a 5 latitude/longitude supplemental/final (01/21/2020): part e 2 maximum operating pressure (mop) correction
Detailed record list
Report Received Date
2019-05-15 00:00:00
Iyear
2019
Report Number
20190155
Supplemental Number
33213
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2019-04-17 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.7
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Notification From Third Party
Incident Identified Datetime
2019-04-17 10:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-04-17 10:15:00
Restart Datetime
2019-04-19 02:22:00
On Site Datetime
2019-04-17 10:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Barnsdall-Kansas City No. 4-12" Line
Segment Name
Line Id 6025
Onshore State Abbreviation
Ks
Onshore Postal Code
66062
Onshore City Name
Olathe
Onshore County Name
Joohnson
Designated Location
Milepost/valve Station
Designated Name
176.61
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
32
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
12
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api5lx-42
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Coal Tar
Installation Year
1950
Manufactured Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
2500
Est Cost Gas Released
61
Est Cost Prop Damage
10000
Est Cost Emergency
20000
Est Cost Environmental
0
Est Cost Other
0
Prpty
32561
Accident Psig
151
Mop Psig
1186
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
146256
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Operations control personnel did not cause or contribute to this release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Lack Of Fusion
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Other Tool Tech Ind
Yes
Circ Wave Recent Year
2014
Other Tool
Multi-Data Set
Other Recent Year
2014
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1989
Hydrtst Most Rcnt Pressure
1858
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2020-01-21 00:00:00
Authorizer Name
S**** H******
Authorizer Telephone
918-574-7173
Authorizer Title
Supervisor Integrity Management
Authorizer Email
S************@m*********.com
Narrative
A third party pipeline operator inspecting their right-of-way within the shared pipeline corridor observed potential product on the ground. Local magellan personnel were contacted and operations control was notified. Investigative events procedures were implemented and resources responded to the site. Operations control initiated shutdown procedures on all magellan pipelines in the corridor and isolation valves were closed. While excavating impacted soil was found, collected, and containerized for proper disposal. The release originated from a pinhole in the longitudinal seam. The release was repaired with a type b sleeve. An additional sleeve was installed to repair other potential lack of fusion features within the joint. The inline inspection vendor for the 2014 multi-dataset ili run reviewed data signals in the vicinity of the release. No similar features were identified through the signal review process. Supplemental/final (05/21/2019): part a 5 latitude/longitude supplemental/final (01/21/2020): part e 2 maximum operating pressure (mop) correction
Report Received Date 2019-05-15 00:00:00
Iyear 2019
Report Number 20190155
Supplemental Number 33213
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2019-04-17 10:00:00
Location Latitude 38.847215 Google Maps OpenStreetMap
Location Longitude -94.744678 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 0.7
Recovered Bbls 0.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Notification From Third Party
Incident Identified Datetime 2019-04-17 10:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-04-17 10:15:00
Restart Datetime 2019-04-19 02:22:00
On Site Datetime 2019-04-17 10:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Barnsdall-Kansas City No. 4-12" Line
Segment Name Line Id 6025
Onshore State Abbreviation Ks
Onshore Postal Code 66062
Onshore City Name Olathe
Onshore County Name Joohnson
Designated Location Milepost/valve Station
Designated Name 176.61
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 32
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 12
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api5lx-42
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Republic Steel
Pipe Coating Type Coal Tar
Installation Year 1950
Manufactured Year 1950
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 2500
Est Cost Gas Released 61
Est Cost Prop Damage 10000
Est Cost Emergency 20000
Est Cost Environmental 0
Est Cost Other 0
Prpty 32561
Accident Psig 151
Mop Psig 1186
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 146256
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Operations control personnel did not cause or contribute to this release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Lack Of Fusion
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Other Tool Tech Ind Yes
Circ Wave Recent Year 2014
Other Tool Multi-Data Set
Other Recent Year 2014
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1989
Hydrtst Most Rcnt Pressure 1858
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2020-01-21 00:00:00
Authorizer Name S**** H******
Authorizer Telephone 918-574-7173
Authorizer Title Supervisor Integrity Management
Authorizer Email S************@m*********.com
Narrative A third party pipeline operator inspecting their right-of-way within the shared pipeline corridor observed potential product on the ground. Local magellan personnel were contacted and operations control was notified. Investigative events procedures were implemented and resources responded to the site. Operations control initiated shutdown procedures on all magellan pipelines in the corridor and isolation valves were closed. While excavating impacted soil was found, collected, and containerized for proper disposal. The release originated from a pinhole in the longitudinal seam. The release was repaired with a type b sleeve. An additional sleeve was installed to repair other potential lack of fusion features within the joint. The inline inspection vendor for the 2014 multi-dataset ili run reviewed data signals in the vicinity of the release. No similar features were identified through the signal review process. Supplemental/final (05/21/2019): part a 5 latitude/longitude supplemental/final (01/21/2020): part e 2 maximum operating pressure (mop) correction

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