HL incident on 2019-04-13 — NJ

Operator
Torrance Valley Pipeline Company Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$250
Incident datetime
2019-04-13 18:42
Report number
Location
NJ
Narrative
On april 13, 2019, at approximately 06:42 p.M. Pst, upon arrival at emidio station, station operator discovered injection pump #3 leaking, releasing approximately 27.75 barrels of crude oil; 26.75 barrels onto the bermed pump pad and 1 barrel onto soil. The operator responded by contacting the pipeline control center to shut down the pump. As an additional precaution, the operator closed the manual valve from tank 3000x08 further isolating the pump. Due to exceeding the reportable quantity of 5 barrels, at approximately 07:33 p.M. Pst, notification was made to cal oes, report number 19-2438. In addition, local cupa was notified. Released product was quickly recovered and cleaned up; contaminated soil was recovered and properly disposed. The failed pump was repaired and resumed operation the following morning on april 14, 2019. An investigation is underway for the cause of the pump failure and the results will be reported in a supplement report to this original 7000.1 report. __________________________________________________________________________________________________________________________ correction to original report narrative: the failed pd pump cover was replaced and the pump resumed operation the following morning on april 14, 2019. An investigation is underway for the cause of the pump cover failure... Supplemental/final report updates: part e - additional operating information, question 7, 7a, 7b - changed from yes to no part g6 - equipment failure, question 6 - equipment failure sub-cause: selected excessive vibration; deselected other and removed under investigation for description part h narrative description of the accident- the cause of failure was due to excessive vibration causing internal component (jam nut) to loosen and damage the liner cover. After the failure of this equipment, mitigative action taken was to inspect all pd pump jam nuts at all facilities to ensure tightness. Additionally, the inspection of the jam nuts has been added to a preventative maintenance schedule to be inspected annually. This concludes the investigation and actions taken for this incident.
Detailed record list
Report Received Date
2019-05-13 00:00:00
Iyear
2019
Report Number
20190152
Supplemental Number
32670
Report Type
Supplemental Final
Operator Id
Name
Torrance Valley Pipeline Company Llc
Operator Street Address
1 Sylvan Way 2nd Floor
Operator City Name
Parsippany
Operator State Abbreviation
NJ
Operator Postal Code
07054
Local Datetime
2019-04-13 18:42:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
27.75
Recovered Bbls
27.75
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-04-13 18:42:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Shutdown Injection Pumps Only
On Site Datetime
2019-04-13 18:42:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Emidio Station
Segment Name
M1 Pentland-Emidio
Onshore State Abbreviation
Ca
Onshore Postal Code
93301
Onshore City Name
Bakersfield
Onshore County Name
Kern
Designated Location
Milepost/valve Station
Designated Name
Emidio Sta
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Pump
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Cast Metal
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
250
Est Cost Emergency
10548
Est Cost Environmental
0
Est Cost Other
0
Prpty
10798
Accident Psig
226
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pumps were is steady state of operation. The operator did not make any changes that could have caused the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Crack In Body
Additional Vibration Ind
Yes
Preparer Name
A****** G*****
Preparer Title
Regulatory Advisor
Preparer Email
A*************@p********.com
Preparer Telephone
3102121764
Prepared Date
2019-09-06 00:00:00
Authorizer Name
T***** M*****
Authorizer Telephone
2816024224
Authorizer Title
Director Regulatory Compliance
Authorizer Email
T************@p********.com
Narrative
On april 13, 2019, at approximately 06:42 p.M. Pst, upon arrival at emidio station, station operator discovered injection pump #3 leaking, releasing approximately 27.75 barrels of crude oil; 26.75 barrels onto the bermed pump pad and 1 barrel onto soil. The operator responded by contacting the pipeline control center to shut down the pump. As an additional precaution, the operator closed the manual valve from tank 3000x08 further isolating the pump. Due to exceeding the reportable quantity of 5 barrels, at approximately 07:33 p.M. Pst, notification was made to cal oes, report number 19-2438. In addition, local cupa was notified. Released product was quickly recovered and cleaned up; contaminated soil was recovered and properly disposed. The failed pump was repaired and resumed operation the following morning on april 14, 2019. An investigation is underway for the cause of the pump failure and the results will be reported in a supplement report to this original 7000.1 report. __________________________________________________________________________________________________________________________ correction to original report narrative: the failed pd pump cover was replaced and the pump resumed operation the following morning on april 14, 2019. An investigation is underway for the cause of the pump cover failure... Supplemental/final report updates: part e - additional operating information, question 7, 7a, 7b - changed from yes to no part g6 - equipment failure, question 6 - equipment failure sub-cause: selected excessive vibration; deselected other and removed under investigation for description part h narrative description of the accident- the cause of failure was due to excessive vibration causing internal component (jam nut) to loosen and damage the liner cover. After the failure of this equipment, mitigative action taken was to inspect all pd pump jam nuts at all facilities to ensure tightness. Additionally, the inspection of the jam nuts has been added to a preventative maintenance schedule to be inspected annually. This concludes the investigation and actions taken for this incident.
Report Received Date 2019-05-13 00:00:00
Iyear 2019
Report Number 20190152
Supplemental Number 32670
Report Type Supplemental Final
Operator Id 39534 PHMSA Enforcement
Name Torrance Valley Pipeline Company Llc
Operator Street Address 1 Sylvan Way 2nd Floor
Operator City Name Parsippany
Operator State Abbreviation NJ
Operator Postal Code 07054
Local Datetime 2019-04-13 18:42:00
Location Latitude 35.063187 Google Maps OpenStreetMap
Location Longitude -119.065405 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 27.75
Recovered Bbls 27.75
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-04-13 18:42:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Shutdown Injection Pumps Only
On Site Datetime 2019-04-13 18:42:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Emidio Station
Segment Name M1 Pentland-Emidio
Onshore State Abbreviation Ca
Onshore Postal Code 93301
Onshore City Name Bakersfield
Onshore County Name Kern
Designated Location Milepost/valve Station
Designated Name Emidio Sta
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Pump
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Cast Metal
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 250
Est Cost Emergency 10548
Est Cost Environmental 0
Est Cost Other 0
Prpty 10798
Accident Psig 226
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pumps were is steady state of operation. The operator did not make any changes that could have caused the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Crack In Body
Additional Vibration Ind Yes
Preparer Name A****** G*****
Preparer Title Regulatory Advisor
Preparer Email A*************@p********.com
Preparer Telephone 3102121764
Prepared Date 2019-09-06 00:00:00
Authorizer Name T***** M*****
Authorizer Telephone 2816024224
Authorizer Title Director Regulatory Compliance
Authorizer Email T************@p********.com
Narrative On april 13, 2019, at approximately 06:42 p.M. Pst, upon arrival at emidio station, station operator discovered injection pump #3 leaking, releasing approximately 27.75 barrels of crude oil; 26.75 barrels onto the bermed pump pad and 1 barrel onto soil. The operator responded by contacting the pipeline control center to shut down the pump. As an additional precaution, the operator closed the manual valve from tank 3000x08 further isolating the pump. Due to exceeding the reportable quantity of 5 barrels, at approximately 07:33 p.M. Pst, notification was made to cal oes, report number 19-2438. In addition, local cupa was notified. Released product was quickly recovered and cleaned up; contaminated soil was recovered and properly disposed. The failed pump was repaired and resumed operation the following morning on april 14, 2019. An investigation is underway for the cause of the pump failure and the results will be reported in a supplement report to this original 7000.1 report. __________________________________________________________________________________________________________________________ correction to original report narrative: the failed pd pump cover was replaced and the pump resumed operation the following morning on april 14, 2019. An investigation is underway for the cause of the pump cover failure... Supplemental/final report updates: part e - additional operating information, question 7, 7a, 7b - changed from yes to no part g6 - equipment failure, question 6 - equipment failure sub-cause: selected excessive vibration; deselected other and removed under investigation for description part h narrative description of the accident- the cause of failure was due to excessive vibration causing internal component (jam nut) to loosen and damage the liner cover. After the failure of this equipment, mitigative action taken was to inspect all pd pump jam nuts at all facilities to ensure tightness. Additionally, the inspection of the jam nuts has been added to a preventative maintenance schedule to be inspected annually. This concludes the investigation and actions taken for this incident.

All rights reserved. Copyright © by ClearPHMSA