GD incident on 2019-09-04 — MI

Operator
Dte Gas Company
Cause
Equipment Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$150,000
Incident datetime
2019-09-04 11:00
Report number
Location
MI, WAYNE
Narrative
Dte gas employees identified a leak on the 36-inch van born pipeline during routine maintenance work on 9/4/2019. The pressure was initial lowered to 215 psig and monitored continuously until a blow down procedure was executed. It was determined after excavating that leak was on plug in flange on stopple. It appeared that the completion plug inside is leaking and possibly unseated. The repair was made and the pipe was return to service on 9/16/19.
Detailed record list
Occurred At
2019-09-04 11:00:00
Year
2019
Report Received Date
2019-12-20 00:00:00
Iyear
2019.0
Report Number
20190150.0
Supplemental Number
33823.0
Report Type
Supplemental Final
Operator Id
Name
Dte Gas Company
Operator Street Address
1 Energy Plaza
Operator City Name
Detroit
Operator State Abbreviation
MI
Operator Postal Code
48226
Local Datetime
2019-09-04 18:32:00
Location Street Address
45581 Ecorse Road
Location City Name
Van Buren Township
Location County Name
Wayne
Location State Abbreviation
MI
Location Postal Code
48111
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-09-07 14:09:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
4810.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-09-04 11:00:00
On Site Datetime
2019-09-04 11:00:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Other
System Part Details
Found A Leaking Plug In Flange On Stopple
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Leak
Leak Type
Seal Or Packing
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
150000.0
Est Cost Emergency
75000.0
Est Cost Other
0.0
Est Cost Unintentional Release
13468.0
Prpty
238468.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
289.0
Normal Psig
289.0
Mop Psig
300.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Stopple Control Fitting Ind
Yes
Preparer Name
F***** S****
Preparer Title
Manager Codes And Standards
Preparer Email
F***********@d********.com
Preparer Telephone
313-389-7762
Authorizer Name
F***** S****
Authorizer Title
Manager Codes And Standards
Authorizer Telephone
313-389-7762
Authorizer Email
F***********@d********.com
Narrative
Dte gas employees identified a leak on the 36-inch van born pipeline during routine maintenance work on 9/4/2019. The pressure was initial lowered to 215 psig and monitored continuously until a blow down procedure was executed. It was determined after excavating that leak was on plug in flange on stopple. It appeared that the completion plug inside is leaking and possibly unseated. The repair was made and the pipe was return to service on 9/16/19.
Occurred At 2019-09-04 11:00:00
Year 2019
Report Received Date 2019-12-20 00:00:00
Iyear 2019.0
Report Number 20190150.0
Supplemental Number 33823.0
Report Type Supplemental Final
Operator Id 12408 PHMSA Enforcement
Name Dte Gas Company
Operator Street Address 1 Energy Plaza
Operator City Name Detroit
Operator State Abbreviation MI
Operator Postal Code 48226
Local Datetime 2019-09-04 18:32:00
Location Street Address 45581 Ecorse Road
Location City Name Van Buren Township
Location County Name Wayne
Location State Abbreviation MI
Location Postal Code 48111
Location Latitude 42.24795 Google Maps OpenStreetMap
Location Longitude -83.48686 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-09-07 14:09:00
Nrc Rpt Num 1257534 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 4810.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-09-04 11:00:00
On Site Datetime 2019-09-04 11:00:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Other
System Part Details Found A Leaking Plug In Flange On Stopple
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Leak
Leak Type Seal Or Packing
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 150000.0
Est Cost Emergency 75000.0
Est Cost Other 0.0
Est Cost Unintentional Release 13468.0
Prpty 238468.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 289.0
Normal Psig 289.0
Mop Psig 300.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Stopple Control Fitting Ind Yes
Preparer Name F***** S****
Preparer Title Manager Codes And Standards
Preparer Email F***********@d********.com
Preparer Telephone 313-389-7762
Authorizer Name F***** S****
Authorizer Title Manager Codes And Standards
Authorizer Telephone 313-389-7762
Authorizer Email F***********@d********.com
Narrative Dte gas employees identified a leak on the 36-inch van born pipeline during routine maintenance work on 9/4/2019. The pressure was initial lowered to 215 psig and monitored continuously until a blow down procedure was executed. It was determined after excavating that leak was on plug in flange on stopple. It appeared that the completion plug inside is leaking and possibly unseated. The repair was made and the pipe was return to service on 9/16/19.

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