GD incident on 2019-08-28 — TX

Operator
Texas Gas Service Company, A Division Of One Gas, Inc.
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$15,000
Incident datetime
2019-08-28 17:55
Report number
Location
TX, TRAVIS
Narrative
A commercial customer requested that tgs relocate a 125' section of a 12" coated steel pipeline to accommodate the customer's new building construction. The customer's new building plan required a footer in close proximity to the existing pipeline. On 8-28-19, after isolation was complete, work began. The entire 125' of 12" coated steel main was laid in a new ditch and getting prepared for two 12" steel tie-ins to complete the relocation. Later in the day, upon detecting natural gas bleeding through a 12" isolation valve into the isolated pipeline, the texas gas service inspector ordered work to stop until a thread-o-ring (tor) could be installed to pull gas from the isolated piping where hot work was going to be performed. While the tor fitting was being obtained, the contractor's foreman directed his welder to attempt to ignite the gas in the north trench to test for gas. The spark traveled down the pipe to the south trench and ignited the gas there causing an injury to the employee. The inspectors, foreman and welder were disqualified and required to retrain and be re-evaluated prior to any return to work. In addition to the retrain and re-evaluation of the affected employees, texas gas service will be performing a safety training covering the importance of following construction and safety protocols when performing any construction work for texas gas service. Texas gas service at 21:45 (8/28/19) was notified that the injury (burns) to the employee would cause inpatient hospitalization which was the confirmed discovery time this is a reportable incident. The employee was released from the hospital on 8/29/19. The 48 hrs. Phmsa notice requirement was called in on 8/30/19 @ 11:01 am (nrc#1256868). Note: relocation was for a new commercial customer (car dealership that did not have existing address). The lat / long coordinates used for the incident on part a (5f) is at the specific location of the incident site. (the actual address used in the report is the closest known active address which is 10000 research blvd). The actual incident location is across the street from the 10000 research blvd address on the report which the lat / long coordinates point to.
Detailed record list
Occurred At
2019-08-28 17:55:00
Year
2019
Report Received Date
2019-09-26 00:00:00
Iyear
2019.0
Report Number
20190110.0
Supplemental Number
32789.0
Report Type
Supplemental Final
Operator Id
Name
Texas Gas Service Company, A Division Of One Gas, Inc.
Operator Street Address
1301 Mopac Expressway Suite 400
Operator City Name
Austin
Operator State Abbreviation
TX
Operator Postal Code
78746
Local Datetime
2019-08-28 17:55:00
Location Street Address
10000 Research Blvd
Location City Name
Austin
Location County Name
Travis
Location State Abbreviation
TX
Location Postal Code
78759
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-08-28 22:13:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
1053.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
1
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-08-28 17:55:00
On Site Datetime
2019-08-28 17:55:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
2019.0
Pipe Diameter
12.0
Pipe Specification
Api 5l
Pipe Manufacturer
Tmk Ipsco (Ky)
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Erw
Wt Steel
0.375
Release Type
Other
Release Type Details
12" Valve Bleed By
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
15000.0
Est Cost Emergency
10000.0
Est Cost Other
0.0
Est Cost Unintentional Release
3731.0
Prpty
28731.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
243.0
Normal Psig
245.0
Mop Psig
265.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The gas amount was too small to detect via the scada system
Employee Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Contractor Drug Test Ind
Yes
Num Contractors Tested
9
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Welder Flashed Excavation Hole With Welding Torch.
Related Failure Follow Ind
Yes
Category Type
Construction
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D*** L*******
Preparer Title
Director Engineering Texas Gas Service
Preparer Email
D********@o*****.com
Preparer Telephone
512-370-8213
Authorizer Name
D*** L*******
Authorizer Title
Director Engineering Texas Gas Service
Authorizer Telephone
512-370-8213
Authorizer Email
D********@o*****.com
Narrative
A*********************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ 11:01 am (nrc#1256868). Note: relocation was for a new commercial customer (car dealership that did not have existing address). The lat / long coordinates used for the incident on part a (5f) is at the specific location of the incident site. (the actual address used in the report is the closest known active address which is 10000 research blvd). ***********************************************************************************************************************************************.
Occurred At 2019-08-28 17:55:00
Year 2019
Report Received Date 2019-09-26 00:00:00
Iyear 2019.0
Report Number 20190110.0
Supplemental Number 32789.0
Report Type Supplemental Final
Operator Id 18532 PHMSA Enforcement
Name Texas Gas Service Company, A Division Of One Gas, Inc.
Operator Street Address 1301 Mopac Expressway Suite 400
Operator City Name Austin
Operator State Abbreviation TX
Operator Postal Code 78746
Local Datetime 2019-08-28 17:55:00
Location Street Address 10000 Research Blvd
Location City Name Austin
Location County Name Travis
Location State Abbreviation TX
Location Postal Code 78759
Location Latitude 30.389624 Google Maps OpenStreetMap
Location Longitude -97.74646 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-08-28 22:13:00
Nrc Rpt Num 1256708 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 1053.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 1
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-08-28 17:55:00
On Site Datetime 2019-08-28 17:55:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 2019.0
Pipe Diameter 12.0
Pipe Specification Api 5l
Pipe Manufacturer Tmk Ipsco (Ky)
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Erw
Wt Steel 0.375
Release Type Other
Release Type Details 12" Valve Bleed By
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 15000.0
Est Cost Emergency 10000.0
Est Cost Other 0.0
Est Cost Unintentional Release 3731.0
Prpty 28731.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 243.0
Normal Psig 245.0
Mop Psig 265.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The gas amount was too small to detect via the scada system
Employee Drug Test Ind Yes
Num Employees Tested 1
Num Employees Failed 0
Contractor Drug Test Ind Yes
Num Contractors Tested 9
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Welder Flashed Excavation Hole With Welding Torch.
Related Failure Follow Ind Yes
Category Type Construction
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D*** L*******
Preparer Title Director Engineering Texas Gas Service
Preparer Email D********@o*****.com
Preparer Telephone 512-370-8213
Authorizer Name D*** L*******
Authorizer Title Director Engineering Texas Gas Service
Authorizer Telephone 512-370-8213
Authorizer Email D********@o*****.com
Narrative A*********************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ 11:01 am (nrc#1256868). Note: relocation was for a new commercial customer (car dealership that did not have existing address). The lat / long coordinates used for the incident on part a (5f) is at the specific location of the incident site. (the actual address used in the report is the closest known active address which is 10000 research blvd). ***********************************************************************************************************************************************.

All rights reserved. Copyright © by ClearPHMSA