GD incident on 2019-08-14 — MI

Operator
Consumers Energy Co
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$294,600
Incident datetime
2019-08-14 15:56
Report number
Location
MI, SAGINAW
Narrative
On august 14, 2019 at approximately 15:56 hours consumers energy (ce) was notified of damage to a 12" steel medium pressure natural gas pipeline. The pipeline was struck by a trenching machine being used to install drain tile in a farm field. The damage occurred near 4675 hackett road, saginaw (saginaw county) michigan. A gas service worker (gsw) and distribution crew arrived at approximately 16:35 and 16:41 hours respectively. The gsw monitored the site continuously until the damaged pipeline segment was isolated and the blowing gas contained. Police and fire personnel were onsite and portions of the road were closed as a safety precaution. There were no fatalities or injuries as a result of the damage. The pipeline was isolated at approximately 19:17 hours by squeezing an 8" plastic pipeline at the consumers energy's zilwaukee city gate (cut and cap north of the damage) and closing valve m1312 to the south of the damage location. Once the pipeline was isolated and blowing gas contained, a location upstream of valve m1312 was cut and capped. An incident investigation determined the root cause as a third party damage. Several factors that may have contributed to the damage were also identified as follows (1) facility not located or marked - the one call ticket positive response 001(no conflict) was provided by the staking contractor following a conversation with a representative of the company installing drain tiles. (2) unclear communication between the ce staking contractor and the contractor installing the drainage tile. The staking technician spoke with contractor and was advised (per documented notes) the entire square doesn't need to be marked he needs the field east of hackett that isn't planted marked. Approximately 40' of 12" steel medium pressure pipeline was replaced between the zilwaukee city gate (north isolation point) and the southerly isolation point near valve m1312. Following the pipeline installation, temporary odorization equipment was installed to ensure adequate odor intensity as a result of derating from transmission pipeline. On july 20th at approximately 15:00 hours, crews turned the odorization equipment on and opened valves to introduce gas flow on the pipeline, returning the pipeline to normal operations.
Detailed record list
Occurred At
2019-08-14 15:56:00
Year
2019
Report Received Date
2019-09-13 00:00:00
Iyear
2019.0
Report Number
20190101.0
Supplemental Number
34389.0
Report Type
Supplemental Final
Operator Id
Name
Consumers Energy Co
Operator Street Address
One Energy Plaza
Operator City Name
Jackson
Operator State Abbreviation
MI
Operator Postal Code
49201
Local Datetime
2019-08-14 15:56:00
Location Street Address
4675 Hackett Road
Location City Name
Saginaw
Location County Name
Saginaw
Location State Abbreviation
MI
Location Postal Code
48603
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-08-16 12:10:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
2511.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-08-14 15:56:00
On Site Datetime
2019-08-14 16:35:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
55.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1942.0
Pipe Diameter
12.0
Pipe Specification
Api 5l
Pipe Manufacturer
National Tube
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.203
Release Type
Mechanical Puncture
Puncture Axial
12.0
Puncture Circum
6.0
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
294600.0
Est Cost Emergency
167.0
Est Cost Other
0.0
Est Cost Unintentional Release
5750.0
Prpty
300517.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
55.0
Normal Psig
55.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Trencher
Work Performed
Drainage
One Call Notified Ind
Yes
One Call Ticket Num
91981987
Locator Type
Contract Locator
Visible Marks
No
Service Interruption
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Locator Error
Preparer Name
C******* K***
Preparer Title
Senior Engineering Technical Analyst Ii
Preparer Email
C************@c********.com
Preparer Telephone
989-280-2963
Authorizer Name
J**** P****
Authorizer Title
Gas Compliance Lead
Authorizer Telephone
989-791-5749
Authorizer Email
J**********@c********.com
Narrative
On august 14, 2019 at approximately 15:56 hours consumers energy (ce) was notified of damage to a 12" steel medium pressure natural gas pipeline. The pipeline was struck by a trenching machine being used to install drain tile in a farm field. The damage occurred near 4675 hackett road, saginaw (saginaw county) michigan. A gas service worker (gsw) and distribution crew arrived at approximately 16:35 and 16:41 hours respectively. The gsw monitored the site continuously until the damaged pipeline segment was isolated and the blowing gas contained. Police and fire personnel were onsite and portions of the road were closed as a safety precaution. There were no fatalities or injuries as a result of the damage. The pipeline was isolated at approximately 19:17 hours by squeezing an 8" plastic pipeline at the consumers energy's zilwaukee city gate (cut and cap north of the damage) and closing valve m1312 to the south of the damage location. Once the pipeline was isolated and blowing gas contained, a location upstream of valve m1312 was cut and capped. An incident investigation determined the root cause as a third party damage. Several factors that may have contributed to the damage were also identified as follows (1) facility not located or marked - the one call ticket positive response 001(no conflict) was provided by the staking contractor following a conversation with a representative of the company installing drain tiles. (2) unclear communication between the ce staking contractor and the contractor installing the drainage tile. The staking technician spoke with contractor and was advised (per documented notes) the entire square doesn't need to be marked he needs the field east of hackett that isn't planted marked. Approximately 40' of 12" steel medium pressure pipeline was replaced between the zilwaukee city gate (north isolation point) and the southerly isolation point near valve m1312. Following the pipeline installation, temporary odorization equipment was installed to ensure adequate odor intensity as a result of derating from transmission pipeline. On july 20th at approximately 15:00 hours, crews turned the odorization equipment on and opened valves to introduce gas flow on the pipeline, returning the pipeline to normal operations.
Occurred At 2019-08-14 15:56:00
Year 2019
Report Received Date 2019-09-13 00:00:00
Iyear 2019.0
Report Number 20190101.0
Supplemental Number 34389.0
Report Type Supplemental Final
Operator Id 2748 PHMSA Enforcement
Name Consumers Energy Co
Operator Street Address One Energy Plaza
Operator City Name Jackson
Operator State Abbreviation MI
Operator Postal Code 49201
Local Datetime 2019-08-14 15:56:00
Location Street Address 4675 Hackett Road
Location City Name Saginaw
Location County Name Saginaw
Location State Abbreviation MI
Location Postal Code 48603
Location Latitude 43.47672 Google Maps OpenStreetMap
Location Longitude -84.069948 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-08-16 12:10:00
Nrc Rpt Num 1255353 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 2511.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-08-14 15:56:00
On Site Datetime 2019-08-14 16:35:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 55.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1942.0
Pipe Diameter 12.0
Pipe Specification Api 5l
Pipe Manufacturer National Tube
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.203
Release Type Mechanical Puncture
Puncture Axial 12.0
Puncture Circum 6.0
Class Location Type Class 2 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 294600.0
Est Cost Emergency 167.0
Est Cost Other 0.0
Est Cost Unintentional Release 5750.0
Prpty 300517.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 55.0
Normal Psig 55.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Trencher
Work Performed Drainage
One Call Notified Ind Yes
One Call Ticket Num 91981987
Locator Type Contract Locator
Visible Marks No
Service Interruption No
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Locator Error
Preparer Name C******* K***
Preparer Title Senior Engineering Technical Analyst Ii
Preparer Email C************@c********.com
Preparer Telephone 989-280-2963
Authorizer Name J**** P****
Authorizer Title Gas Compliance Lead
Authorizer Telephone 989-791-5749
Authorizer Email J**********@c********.com
Narrative On august 14, 2019 at approximately 15:56 hours consumers energy (ce) was notified of damage to a 12" steel medium pressure natural gas pipeline. The pipeline was struck by a trenching machine being used to install drain tile in a farm field. The damage occurred near 4675 hackett road, saginaw (saginaw county) michigan. A gas service worker (gsw) and distribution crew arrived at approximately 16:35 and 16:41 hours respectively. The gsw monitored the site continuously until the damaged pipeline segment was isolated and the blowing gas contained. Police and fire personnel were onsite and portions of the road were closed as a safety precaution. There were no fatalities or injuries as a result of the damage. The pipeline was isolated at approximately 19:17 hours by squeezing an 8" plastic pipeline at the consumers energy's zilwaukee city gate (cut and cap north of the damage) and closing valve m1312 to the south of the damage location. Once the pipeline was isolated and blowing gas contained, a location upstream of valve m1312 was cut and capped. An incident investigation determined the root cause as a third party damage. Several factors that may have contributed to the damage were also identified as follows (1) facility not located or marked - the one call ticket positive response 001(no conflict) was provided by the staking contractor following a conversation with a representative of the company installing drain tiles. (2) unclear communication between the ce staking contractor and the contractor installing the drainage tile. The staking technician spoke with contractor and was advised (per documented notes) the entire square doesn't need to be marked he needs the field east of hackett that isn't planted marked. Approximately 40' of 12" steel medium pressure pipeline was replaced between the zilwaukee city gate (north isolation point) and the southerly isolation point near valve m1312. Following the pipeline installation, temporary odorization equipment was installed to ensure adequate odor intensity as a result of derating from transmission pipeline. On july 20th at approximately 15:00 hours, crews turned the odorization equipment on and opened valves to introduce gas flow on the pipeline, returning the pipeline to normal operations.

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