GTG incident on 2019-07-29 — TX

Operator
Texas Eastern Transmission, Lp (Spectra Energy Partners, Lp)
Cause
Material Failure Of Pipe Or Weld
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$454,762
Incident datetime
2019-07-29 21:59
Report number
Location
TX
Narrative
Original report: 48 hr nrc report # 1253798 at approximately 8:28 pm edt on july 29, 2019, enbridge's gas control received a notification of a natural gas release from the public on texas eastern transmission's (tetlp) line 10 pipeline system at mp 658.85 in lauderdale county, oh. Tetlp dispatched employees to the location and discovered a leak at approximately 9:59 pm edt. Tetlp made the nrc notification at 11:41 pm edt following confirmed discovery of the leak. The pipeline was subsequently isolated at 10:33 pm edt, stopping the release of gas. The affected pipe was replaced and returned to service at approximately 6:35 pm edt on august 19, 2019. The apparent cause is still under investigation. Supplemental report: 01/02/2020 the apparent cause is a crack associated with pipe laid on sharp rock during original construction.
Detailed record list
Report Received Date
2019-08-26 00:00:00
Iyear
2019
Report Number
20190100
Supplemental Number
33138
Report Type
Supplemental Final
Operator Id
Name
Texas Eastern Transmission, Lp (Spectra Energy Partners, Lp)
Operator Street Address
915 North Eldridge Parkway
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2019-07-29 20:28:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2019-07-29 23:41:00
Commodity Released Type
Natural Gas
Unintentional Release
45
Intentional Release
26520.63
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2019-07-29 22:33:00
Restart Datetime
2019-08-19 18:35:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2019-07-29 21:59:00
On Site Datetime
2019-07-30 21:59:00
On Off Shore
Onshore
Onshore State Abbreviation
Oh
Onshore Postal Code
45715
Onshore City Name
Beverely
Onshore County Name
Morgan
Designated Location
Milepost
Designated Name
658.85
Pipe Fac Name
Line 10
Segment Name
Athe-Bern
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
30
Pipe Wall Thickness
0.375
Pipe Smys
52000
Pipe Specification
Api-5l X-52
Pipe Seam Type
Dsaw
Pipe Manufacturer
National Tube
Pipe Coating Type
Coal Tar
Installation Year
1952
Manufactured Year
1952
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
633
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
59406
Est Cost Intentional Release
0
Est Cost Prop Damage
454762
Est Cost Emergency
0
Est Cost Other
0
Prpty
514168
Accident Psig
806
Mop Psig
936
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
79728
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
It was determined the controller's actions did not contribute to the incident. The volume of the leak was too small to be detected by the controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Pwjf Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Metallurgical Ind
Yes
Other Factor
Yes
Other Factor Details
Pipe During Original Construction Installed On Sharp Rock
Additional Dent Ind
Yes
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2019
Geometry Recent Year
2019
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
M**** S******
Preparer Title
Senior Engineer
Preparer Email
M************@e*******.com
Preparer Telephone
713-627-4726
Authorizer Name
N***** A****
Authorizer Title
Manager Operational Compliance
Authorizer Telephone
713-627-5008
Authorizer Email
N***********@e*******.com
Narrative
Original report: 48 hr nrc report # 1253798 at approximately 8:28 pm edt on july 29, 2019, enbridge's gas control received a notification of a natural gas release from the public on texas eastern transmission's (tetlp) line 10 pipeline system at mp 658.85 in lauderdale county, oh. Tetlp dispatched employees to the location and discovered a leak at approximately 9:59 pm edt. Tetlp made the nrc notification at 11:41 pm edt following confirmed discovery of the leak. The pipeline was subsequently isolated at 10:33 pm edt, stopping the release of gas. The affected pipe was replaced and returned to service at approximately 6:35 pm edt on august 19, 2019. The apparent cause is still under investigation. Supplemental report: 01/02/2020 the apparent cause is a crack associated with pipe laid on sharp rock during original construction.
Report Received Date 2019-08-26 00:00:00
Iyear 2019
Report Number 20190100
Supplemental Number 33138
Report Type Supplemental Final
Operator Id 19235 PHMSA Enforcement
Name Texas Eastern Transmission, Lp (Spectra Energy Partners, Lp)
Operator Street Address 915 North Eldridge Parkway
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2019-07-29 20:28:00
Location Latitude 39.61083403 Google Maps OpenStreetMap
Location Longitude -81.628925 Google Maps OpenStreetMap
Nrc Rpt Num 1253581 NRC Report How to search
Nrc Rpt Datetime 2019-07-29 23:41:00
Commodity Released Type Natural Gas
Unintentional Release 45
Intentional Release 26520.63
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2019-07-29 22:33:00
Restart Datetime 2019-08-19 18:35:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2019-07-29 21:59:00
On Site Datetime 2019-07-30 21:59:00
On Off Shore Onshore
Onshore State Abbreviation Oh
Onshore Postal Code 45715
Onshore City Name Beverely
Onshore County Name Morgan
Designated Location Milepost
Designated Name 658.85
Pipe Fac Name Line 10
Segment Name Athe-Bern
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 30
Pipe Wall Thickness 0.375
Pipe Smys 52000
Pipe Specification Api-5l X-52
Pipe Seam Type Dsaw
Pipe Manufacturer National Tube
Pipe Coating Type Coal Tar
Installation Year 1952
Manufactured Year 1952
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 633
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 59406
Est Cost Intentional Release 0
Est Cost Prop Damage 454762
Est Cost Emergency 0
Est Cost Other 0
Prpty 514168
Accident Psig 806
Mop Psig 936
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 79728
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details It was determined the controller's actions did not contribute to the incident. The volume of the leak was too small to be detected by the controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Pwjf Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Metallurgical Ind Yes
Other Factor Yes
Other Factor Details Pipe During Original Construction Installed On Sharp Rock
Additional Dent Ind Yes
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2019
Geometry Recent Year 2019
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name M**** S******
Preparer Title Senior Engineer
Preparer Email M************@e*******.com
Preparer Telephone 713-627-4726
Authorizer Name N***** A****
Authorizer Title Manager Operational Compliance
Authorizer Telephone 713-627-5008
Authorizer Email N***********@e*******.com
Narrative Original report: 48 hr nrc report # 1253798 at approximately 8:28 pm edt on july 29, 2019, enbridge's gas control received a notification of a natural gas release from the public on texas eastern transmission's (tetlp) line 10 pipeline system at mp 658.85 in lauderdale county, oh. Tetlp dispatched employees to the location and discovered a leak at approximately 9:59 pm edt. Tetlp made the nrc notification at 11:41 pm edt following confirmed discovery of the leak. The pipeline was subsequently isolated at 10:33 pm edt, stopping the release of gas. The affected pipe was replaced and returned to service at approximately 6:35 pm edt on august 19, 2019. The apparent cause is still under investigation. Supplemental report: 01/02/2020 the apparent cause is a crack associated with pipe laid on sharp rock during original construction.

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