GD incident on 2019-07-01 — GA

Operator
Atlanta Gas Light Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$114,380
Incident datetime
2019-07-01 14:30
Report number
Location
GA, FULTON
Narrative
A 4-inch plastic natural gas main was ruptured by a contract crew while installing electric cable by directional drilling. Once the incident was made safe it was identified that repairs to the affected pipeline would exceed the $50,000 threshold for reporting where the national response center (nrc) was contacted at that time. Notification to the one-call center was made where the main was correctly located, however, the excavator failed to pothole where the facility was damaged. Additional nrc report number 1251281 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Detailed record list
Occurred At
2019-07-01 14:30:00
Year
2019
Report Received Date
2019-07-29 00:00:00
Iyear
2019.0
Report Number
20190082.0
Supplemental Number
32479.0
Report Type
Original Final
Operator Id
Name
Atlanta Gas Light Co
Operator Street Address
10 Peachtree Place Ne
Operator City Name
Atlanta
Operator State Abbreviation
GA
Operator Postal Code
30309
Local Datetime
2019-07-01 14:27:00
Location Street Address
Tell Road Sw At Pinella Drive Sw
Location City Name
Atlanta
Location County Name
Fulton
Location State Abbreviation
GA
Location Postal Code
30331
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-07-02 14:48:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
7463.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-07-01 14:30:00
On Site Datetime
2019-07-01 14:47:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
96.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2004.0
Pipe Diameter
4.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Phillips-Drisco Pipe
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
4.0
Puncture Circum
4.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
114380.0
Est Cost Emergency
10000.0
Est Cost Other
0.0
Est Cost Unintentional Release
20222.0
Prpty
144602.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
84.0
Accident Psig
45.0
Normal Psig
45.0
Mop Psig
45.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Electric
One Call Notified Ind
Yes
One Call Ticket Num
4189400028
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
26.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
R**** M*******
Preparer Title
Lead Compliance Engineer
Preparer Email
R*******@s*********.com
Preparer Telephone
(404) 584-3733
Preparer Fax
(404) 584-4710
Authorizer Name
R*** S*****
Authorizer Title
Director Compliance And Qa
Authorizer Telephone
404-584-4910
Authorizer Email
R******@s*********.com
Narrative
A 4-inch plastic natural gas main was ruptured by a contract crew while installing electric cable by directional drilling. Once the incident was made safe it was identified that repairs to the affected pipeline would exceed the $50,000 threshold for reporting where the national response center (nrc) was contacted at that time. Notification to the one-call center was made where the main was correctly located, however, the excavator failed to pothole where the facility was damaged. Additional nrc report number 1251281 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.
Occurred At 2019-07-01 14:30:00
Year 2019
Report Received Date 2019-07-29 00:00:00
Iyear 2019.0
Report Number 20190082.0
Supplemental Number 32479.0
Report Type Original Final
Operator Id 792 PHMSA Enforcement
Name Atlanta Gas Light Co
Operator Street Address 10 Peachtree Place Ne
Operator City Name Atlanta
Operator State Abbreviation GA
Operator Postal Code 30309
Local Datetime 2019-07-01 14:27:00
Location Street Address Tell Road Sw At Pinella Drive Sw
Location City Name Atlanta
Location County Name Fulton
Location State Abbreviation GA
Location Postal Code 30331
Location Latitude 33.680462 Google Maps OpenStreetMap
Location Longitude -84.530696 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-07-02 14:48:00
Nrc Rpt Num 1250772 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 7463.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-07-01 14:30:00
On Site Datetime 2019-07-01 14:47:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 96.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2004.0
Pipe Diameter 4.0
Pipe Specification Astm D2513
Pipe Manufacturer Phillips-Drisco Pipe
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 4.0
Puncture Circum 4.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 114380.0
Est Cost Emergency 10000.0
Est Cost Other 0.0
Est Cost Unintentional Release 20222.0
Prpty 144602.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 84.0
Accident Psig 45.0
Normal Psig 45.0
Mop Psig 45.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Electric
One Call Notified Ind Yes
One Call Ticket Num 4189400028
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 26.0
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name R**** M*******
Preparer Title Lead Compliance Engineer
Preparer Email R*******@s*********.com
Preparer Telephone (404) 584-3733
Preparer Fax (404) 584-4710
Authorizer Name R*** S*****
Authorizer Title Director Compliance And Qa
Authorizer Telephone 404-584-4910
Authorizer Email R******@s*********.com
Narrative A 4-inch plastic natural gas main was ruptured by a contract crew while installing electric cable by directional drilling. Once the incident was made safe it was identified that repairs to the affected pipeline would exceed the $50,000 threshold for reporting where the national response center (nrc) was contacted at that time. Notification to the one-call center was made where the main was correctly located, however, the excavator failed to pothole where the facility was damaged. Additional nrc report number 1251281 was created for the same event after a supplemental call was placed with the nrc to update the initial telephonic notice.

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