Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2019-06-23 — MO
Operator
Spire Missouri Inc. West
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$140,077
Incident datetime
2019-06-23 23:15
Report number
Location
MO, MCDONALD COUNTY
Narrative
Flooding caused tree to overturn, trees root system then fractured 2 inch coated steel main near intersection of state highway ee and indian creek lanagan, missouri. Gas was made safe at approximately 02:07 june 24th. A temporary bypass was installed until a permanent repair was completed. A 48 hour update to the nrc was made on june 26, 2019 at 11:06am. Report number 1250151.
Detailed record list
Occurred At
2019-06-23 23:15:00
Year
2019
Report Received Date
2019-07-23 00:00:00
Iyear
2019.0
Report Number
20190080.0
Supplemental Number
32910.0
Report Type
Supplemental Final
Operator Id
30769
Name
Spire Missouri Inc. West
Operator Street Address
700 Market Street
Operator City Name
Saint Louis
Operator State Abbreviation
MO
Operator Postal Code
63101
Local Datetime
2019-06-23 23:08:00
Location Street Address
Indian Creek Drive At Route Ee
Location City Name
Lanagan
Location County Name
Mcdonald County
Location State Abbreviation
MO
Location Postal Code
64847-8888
Location Latitude
36.599561
Location Longitude
-94.449958
Nrc Rpt Datetime
2019-06-24 10:36:00
Nrc Rpt Num
1249893
Commodity Released Type
Natural Gas
Unintentional Release
74.49
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-06-23 23:15:00
On Site Datetime
2019-06-24 23:45:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1969.0
Pipe Diameter
2.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
6.5
Rupture Width
2.1
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
140077.0
Est Cost Emergency
500.0
Est Cost Other
0.0
Est Cost Unintentional Release
368.0
Prpty
140945.0
Commercial Affected
10.0
Industrial Affected
0.0
Residences Affected
75.0
Accident Psig
50.0
Normal Psig
50.0
Mop Psig
55.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The actions of the controller did not cause or contribute to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Other
Nf Other Details
Flooding Caused Tree To Overturn, The Tree's Root System Then Fractured 2 Inch Distribution Main.
Nf Extreme Weather Ind
No
Preparer Name
N***** C**********
Preparer Title
Manager Pipeline Safety
Preparer Email
N*****************@s**********.com
Preparer Telephone
314-349-2929
Authorizer Name
C**** H********
Authorizer Title
Vp Operations Services
Authorizer Telephone
314-349-2972
Authorizer Email
C**************@s**********.com
Narrative
Flooding caused tree to overturn, trees root system then fractured 2 inch coated steel main near intersection of state highway ee and indian creek lanagan, missouri. Gas was made safe at approximately 02:07 june 24th. A temporary bypass was installed until a permanent repair was completed. A 48 hour update to the nrc was made on june 26, 2019 at 11:06am. Report number 1250151.
| Occurred At | 2019-06-23 23:15:00 |
|---|---|
| Year | 2019 |
| Report Received Date | 2019-07-23 00:00:00 |
| Iyear | 2019.0 |
| Report Number | 20190080.0 |
| Supplemental Number | 32910.0 |
| Report Type | Supplemental Final |
| Operator Id | 30769 PHMSA Enforcement |
| Name | Spire Missouri Inc. West |
| Operator Street Address | 700 Market Street |
| Operator City Name | Saint Louis |
| Operator State Abbreviation | MO |
| Operator Postal Code | 63101 |
| Local Datetime | 2019-06-23 23:08:00 |
| Location Street Address | Indian Creek Drive At Route Ee |
| Location City Name | Lanagan |
| Location County Name | Mcdonald County |
| Location State Abbreviation | MO |
| Location Postal Code | 64847-8888 |
| Location Latitude | 36.599561 Google Maps OpenStreetMap |
| Location Longitude | -94.449958 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2019-06-24 10:36:00 |
| Nrc Rpt Num | 1249893 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 74.49 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0.0 |
| Incident Identified Datetime | 2019-06-23 23:15:00 |
| On Site Datetime | 2019-06-24 23:45:00 |
| Federal | No |
| Location Type | Utility Right-Of-Way / Easement |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 48.0 |
| Crossing | No |
| Pipe Facility Type | Investor Owned |
| System Part Involved | Main |
| Installation Year | 1969.0 |
| Pipe Diameter | 2.0 |
| Pipe Specification | Unknown |
| Pipe Manufacturer | Unknown |
| Material Involved | Steel |
| Steel Seam Type | Other |
| Steel Seam Type Details | Unknown |
| Release Type | Rupture |
| Rupture Orient | Circumferential |
| Rupture Length | 6.5 |
| Rupture Width | 2.1 |
| Class Location Type | Class 2 Location |
| Est Cost Oper Paid | 0.0 |
| Est Cost Prop Damage | 140077.0 |
| Est Cost Emergency | 500.0 |
| Est Cost Other | 0.0 |
| Est Cost Unintentional Release | 368.0 |
| Prpty | 140945.0 |
| Commercial Affected | 10.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 75.0 |
| Accident Psig | 50.0 |
| Normal Psig | 50.0 |
| Mop Psig | 55.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | No |
| Accident Identifier | Notification From Public |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The actions of the controller did not cause or contribute to the event. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Natural Force Damage |
| Cause Details | Heavy Rains/floods |
| Natural Force Type | Heavy Rains/floods |
| Heavy Rains Subtype | Other |
| Nf Other Details | Flooding Caused Tree To Overturn, The Tree's Root System Then Fractured 2 Inch Distribution Main. |
| Nf Extreme Weather Ind | No |
| Preparer Name | N***** C********** |
| Preparer Title | Manager Pipeline Safety |
| Preparer Email | N*****************@s**********.com |
| Preparer Telephone | 314-349-2929 |
| Authorizer Name | C**** H******** |
| Authorizer Title | Vp Operations Services |
| Authorizer Telephone | 314-349-2972 |
| Authorizer Email | C**************@s**********.com |
| Narrative | Flooding caused tree to overturn, trees root system then fractured 2 inch coated steel main near intersection of state highway ee and indian creek lanagan, missouri. Gas was made safe at approximately 02:07 june 24th. A temporary bypass was installed until a permanent repair was completed. A 48 hour update to the nrc was made on june 26, 2019 at 11:06am. Report number 1250151. |
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