GD incident on 2019-06-18 — FL

Operator
Peoples Gas System Inc
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$39,265
Incident datetime
2019-06-18 16:09
Report number
Location
FL, ORANGE
Narrative
Contractor, gamez professional drilling, inc., damaged peoples gas' (pgs') 4' plastic gas main during installation of a communications cable. The contractor requested and obtained a locate for the excavation, the gas pipeline was correctly marked, and the locate marks were visible in the area. The gas main was damaged during the 3rd party's directional drilling process. The resulting gas leak was made safe by squeezing the 4' plastic gas main and was repaired by installing a new 4' plastic pipe. The pipe had a leakage resurvey performed after the repair on 06/19/19.
Detailed record list
Occurred At
2019-06-18 16:09:00
Year
2019
Report Received Date
2019-07-18 00:00:00
Iyear
2019.0
Report Number
20190076.0
Supplemental Number
32736.0
Report Type
Supplemental Final
Operator Id
Name
Peoples Gas System Inc
Operator Street Address
Po Box 2562
Operator City Name
Tampa
Operator State Abbreviation
FL
Operator Postal Code
33601
Local Datetime
2019-06-18 16:00:00
Location Street Address
Seidel Rd
Location City Name
Winter Garden
Location County Name
Orange
Location State Abbreviation
FL
Location Postal Code
34787
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-06-19 14:40:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
112.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-06-18 16:09:00
On Site Datetime
2019-06-18 16:25:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
180.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2017.0
Pipe Diameter
4.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Drisco
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic Unknown Ind
Unknown
Material Pe Pipe Code
Unknown
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
2.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
39265.0
Est Cost Emergency
17643.0
Est Cost Other
0.0
Est Cost Unintentional Release
1114.0
Prpty
58022.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
194.0
Accident Psig
43.0
Normal Psig
40.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Event was caused by 3rd party excavator
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
County Road
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Cable Tv
One Call Notified Ind
Yes
One Call Ticket Num
160900759
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
20.0
Root Cause Category
Excavation Issue
Root Cause Type
Marks Faded Or Not Maintained
Preparer Name
A**** S****
Preparer Title
Coordinator Sms Documentation
Preparer Email
A******@t*********.com
Preparer Telephone
813-275-3723
Authorizer Name
R****** H*****
Authorizer Title
Manager Pipeline Safety Compliance
Authorizer Telephone
407-420-6667
Authorizer Email
R******@t*********.com
Narrative
Contractor, gamez professional drilling, inc., damaged peoples gas' (pgs') 4' plastic gas main during installation of a communications cable. The contractor requested and obtained a locate for the excavation, the gas pipeline was correctly marked, and the locate marks were visible in the area. The gas main was damaged during the 3rd party's directional drilling process. The resulting gas leak was made safe by squeezing the 4' plastic gas main and was repaired by installing a new 4' plastic pipe. The pipe had a leakage resurvey performed after the repair on 06/19/19.
Occurred At 2019-06-18 16:09:00
Year 2019
Report Received Date 2019-07-18 00:00:00
Iyear 2019.0
Report Number 20190076.0
Supplemental Number 32736.0
Report Type Supplemental Final
Operator Id 15348 PHMSA Enforcement
Name Peoples Gas System Inc
Operator Street Address Po Box 2562
Operator City Name Tampa
Operator State Abbreviation FL
Operator Postal Code 33601
Local Datetime 2019-06-18 16:00:00
Location Street Address Seidel Rd
Location City Name Winter Garden
Location County Name Orange
Location State Abbreviation FL
Location Postal Code 34787
Location Latitude 28.4249337 Google Maps OpenStreetMap
Location Longitude -81.6198238 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-06-19 14:40:00
Nrc Rpt Num 1249427 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 112.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-06-18 16:09:00
On Site Datetime 2019-06-18 16:25:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 180.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2017.0
Pipe Diameter 4.0
Pipe Specification Astm D2513
Pipe Manufacturer Drisco
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Wt Plastic Unknown Ind Unknown
Material Pe Pipe Code Unknown
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 2.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 39265.0
Est Cost Emergency 17643.0
Est Cost Other 0.0
Est Cost Unintentional Release 1114.0
Prpty 58022.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 194.0
Accident Psig 43.0
Normal Psig 40.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Event was caused by 3rd party excavator
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype County Road
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Cable Tv
One Call Notified Ind Yes
One Call Ticket Num 160900759
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 20.0
Root Cause Category Excavation Issue
Root Cause Type Marks Faded Or Not Maintained
Preparer Name A**** S****
Preparer Title Coordinator Sms Documentation
Preparer Email A******@t*********.com
Preparer Telephone 813-275-3723
Authorizer Name R****** H*****
Authorizer Title Manager Pipeline Safety Compliance
Authorizer Telephone 407-420-6667
Authorizer Email R******@t*********.com
Narrative Contractor, gamez professional drilling, inc., damaged peoples gas' (pgs') 4' plastic gas main during installation of a communications cable. The contractor requested and obtained a locate for the excavation, the gas pipeline was correctly marked, and the locate marks were visible in the area. The gas main was damaged during the 3rd party's directional drilling process. The resulting gas leak was made safe by squeezing the 4' plastic gas main and was repaired by installing a new 4' plastic pipe. The pipe had a leakage resurvey performed after the repair on 06/19/19.

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