GD incident on 2019-05-24 — CO

Operator
Black Hills Energy
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$33,718
Incident datetime
2019-05-24 14:50
Report number
Location
CO, WELD
Narrative
14:50 field resource center (frc) received call from damaging party. -14:53 frc dispatched operations tech #1 -15:09 operations tech #1 arrived on scene and communicated with fd/pd and assessed the situation. -15:14 operations tech #1 called in code 2, requesting bhe personnel to assist. -bhe operations techs #2&#3 arrive to assist. -operations used mapping and locating equipment to determine the 6' high pressure was the main damaged, not the 2' pe. -operations supervisor contacted contract welder to mobilize for shut down and repair. -operations supervisor/manager determined that the venting gas could safely continue to vent to atmosphere and did not present a hazard to the public or property. -approximately two miles of line pack began to be reduced down to 100 psi to safely perform stoppling procedure. -2:30 leak was stopped and repairs began. -5:30 pressure was restored. -commercial customer's service was restored on the morning of may 28, 2019.
Detailed record list
Occurred At
2019-05-24 14:50:00
Year
2019
Report Received Date
2019-06-24 00:00:00
Iyear
2019.0
Report Number
20190062.0
Supplemental Number
34752.0
Report Type
Supplemental Final
Operator Id
Name
Black Hills Energy
Operator Street Address
2287 College Road Po Box 2006
Operator City Name
Council Bluffs
Operator State Abbreviation
IA
Operator Postal Code
51502
Local Datetime
2019-05-24 14:50:00
Time Zone
Mountain
Daylight Savings Ind
No
Location Street Address
4306 County Road 22
Location City Name
Frederick
Location County Name
Weld
Location State Abbreviation
CO
Location Postal Code
80516
Location Latitude
Location Longitude
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Datetime
2019-06-04 14:55:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
9762.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-05-24 14:50:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2019-05-24 14:50:00
On Site Datetime
2019-05-24 15:09:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Other Underground Facilities
No
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Uncased
Pipe Facility Type
Investor Owned
System Part Involved
Main
Pipe Diameter
6.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Seamless
Wt Steel
0.188
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
2.0
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
33718.0
Est Cost Emergency
2000.0
Est Cost Other
0.0
Gas Cost In Mcf
4.5475
Est Cost Unintentional Release
44393.0
Est Cost Intentional Release
0.0
Prpty
80111.0
Commercial Affected
4.0
Industrial Affected
1.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
5.0
Accident Psig
250.0
Normal Psig
250.0
Mop Psig
250.0
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2019-05-24 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Odorized By Others
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The system is not monitored by scada.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
County Road
Excavator Type
Contractor
Excavator Equipment
Directional Drilling
Work Performed
Cable Tv
One Call Notified Ind
Yes
One Call Ticket Num
914101991
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
3.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name
S***** D*******
Preparer Title
Pipeline Safety And Compliance Coordinator
Preparer Email
S**************@b*************.com
Preparer Telephone
719 359-0586
Authorizer Name
S***** D*******
Authorizer Title
Pipeline Safety And Compliance Coordinator
Authorizer Telephone
719 359-0586
Authorizer Email
S**************@b*************.com
Narrative
14:50 field resource center (frc) received call from damaging party. -14:53 frc dispatched operations tech #1 -15:09 operations tech #1 arrived on scene and communicated with fd/pd and assessed the situation. -15:14 operations tech #1 called in code 2, requesting bhe personnel to assist. -bhe operations techs #2&#3 arrive to assist. -operations used mapping and locating equipment to determine the 6' high pressure was the main damaged, not the 2' pe. -operations supervisor contacted contract welder to mobilize for shut down and repair. -operations supervisor/manager determined that the venting gas could safely continue to vent to atmosphere and did not present a hazard to the public or property. -approximately two miles of line pack began to be reduced down to 100 psi to safely perform stoppling procedure. -2:30 leak was stopped and repairs began. -5:30 pressure was restored. -commercial customer's service was restored on the morning of may 28, 2019.
Occurred At 2019-05-24 14:50:00
Year 2019
Report Received Date 2019-06-24 00:00:00
Iyear 2019.0
Report Number 20190062.0
Supplemental Number 34752.0
Report Type Supplemental Final
Operator Id 15359 PHMSA Enforcement
Name Black Hills Energy
Operator Street Address 2287 College Road Po Box 2006
Operator City Name Council Bluffs
Operator State Abbreviation IA
Operator Postal Code 51502
Local Datetime 2019-05-24 14:50:00
Time Zone Mountain
Daylight Savings Ind No
Location Street Address 4306 County Road 22
Location City Name Frederick
Location County Name Weld
Location State Abbreviation CO
Location Postal Code 80516
Location Latitude 40.146025 Google Maps OpenStreetMap
Location Longitude -104.974903 Google Maps OpenStreetMap
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Datetime 2019-06-04 14:55:00
Nrc Rpt Num 1247821 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 9762.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-05-24 14:50:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2019-05-24 14:50:00
On Site Datetime 2019-05-24 15:09:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48.0
Other Underground Facilities No
Crossing Yes
Road Crossing Ind Yes
Road Type Uncased
Pipe Facility Type Investor Owned
System Part Involved Main
Pipe Diameter 6.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Seamless
Wt Steel 0.188
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 2.0
Class Location Type Class 2 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 33718.0
Est Cost Emergency 2000.0
Est Cost Other 0.0
Gas Cost In Mcf 4.5475
Est Cost Unintentional Release 44393.0
Est Cost Intentional Release 0.0
Prpty 80111.0
Commercial Affected 4.0
Industrial Affected 1.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 5.0
Accident Psig 250.0
Normal Psig 250.0
Mop Psig 250.0
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2019-05-24 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Odorized By Others
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The system is not monitored by scada.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype County Road
Excavator Type Contractor
Excavator Equipment Directional Drilling
Work Performed Cable Tv
One Call Notified Ind Yes
One Call Ticket Num 914101991
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 3.0
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name S***** D*******
Preparer Title Pipeline Safety And Compliance Coordinator
Preparer Email S**************@b*************.com
Preparer Telephone 719 359-0586
Authorizer Name S***** D*******
Authorizer Title Pipeline Safety And Compliance Coordinator
Authorizer Telephone 719 359-0586
Authorizer Email S**************@b*************.com
Narrative 14:50 field resource center (frc) received call from damaging party. -14:53 frc dispatched operations tech #1 -15:09 operations tech #1 arrived on scene and communicated with fd/pd and assessed the situation. -15:14 operations tech #1 called in code 2, requesting bhe personnel to assist. -bhe operations techs #2&#3 arrive to assist. -operations used mapping and locating equipment to determine the 6' high pressure was the main damaged, not the 2' pe. -operations supervisor contacted contract welder to mobilize for shut down and repair. -operations supervisor/manager determined that the venting gas could safely continue to vent to atmosphere and did not present a hazard to the public or property. -approximately two miles of line pack began to be reduced down to 100 psi to safely perform stoppling procedure. -2:30 leak was stopped and repairs began. -5:30 pressure was restored. -commercial customer's service was restored on the morning of may 28, 2019.

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