GD incident on 2019-05-13 — CA

Operator
Southern California Gas Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$95,090
Incident datetime
2019-05-13 22:32
Report number
Location
CA, SAN BERNARDINO
Narrative
On may 14, 2019, a third party contractor while auguring to install guard rail posts damaged an 8-inch steel main causing a gas leak. Socalgas company crew responded and controlled the gas. No injuries or further damage resulted from this incident. The 8-inch steel main was repaired by replacing a section of the pipe. Investigation of the incident showed that there was a valid USA ticket for the contractor and the 8-inch main was properly marked. The contractor failed to use hand tools where required. This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. 8/9/2019 update: updated part d (2b.) estimated cost of operator's property damage & repairs from $200,000 to $95,090. Submitted final report.
Detailed record list
Occurred At
2019-05-13 22:32:00
Year
2019
Report Received Date
2019-06-12 00:00:00
Iyear
2019.0
Report Number
20190058.0
Supplemental Number
32536.0
Report Type
Supplemental Final
Operator Id
Name
Southern California Gas Co
Operator Street Address
555 West Fifth Street
Operator City Name
Los Angeles
Operator State Abbreviation
CA
Operator Postal Code
90013
Local Datetime
2019-05-13 22:32:00
Location Street Address
15563 Feldspar Dr.
Location City Name
Chino Hills
Location County Name
San Bernardino
Location State Abbreviation
CA
Location Postal Code
91709-2125
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-05-14 05:55:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
2270.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-05-13 22:32:00
On Site Datetime
2019-05-13 23:00:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1978.0
Pipe Diameter
8.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.188
Release Type
Mechanical Puncture
Puncture Axial
1.5
Puncture Circum
1.3
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
95090.0
Est Cost Emergency
200.0
Est Cost Other
0.0
Est Cost Unintentional Release
13620.0
Prpty
108910.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
45.0
Normal Psig
45.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
State Highway
Excavator Type
Contractor
Excavator Equipment
Auger
Work Performed
Fencing
One Call Notified Ind
Yes
One Call Ticket Num
191190876
One Call Center Name
Usa North
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
A***** W*****
Preparer Title
Pipeline Safety Compliance Advisor
Preparer Email
A*******@s**************.com
Preparer Telephone
818-632-8407
Authorizer Name
A***** W*****
Authorizer Title
Pipeline Safety Compliance Advisor
Authorizer Telephone
818-632-8407
Authorizer Email
A*******@s**************.com
Narrative
On may 14, 2019, a third party contractor while auguring to install guard rail posts damaged an 8-inch steel main causing a gas leak. Socalgas company crew responded and controlled the gas. No injuries or further damage resulted from this incident. The 8-inch steel main was repaired by replacing a section of the pipe. Investigation of the incident showed that there was a valid USA ticket for the contractor and the 8-inch main was properly marked. The contractor failed to use hand tools where required. This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. 8/9/2019 update: updated part d (2b.) estimated cost of operator's property damage & repairs from $200,000 to $95,090. Submitted final report.
Occurred At 2019-05-13 22:32:00
Year 2019
Report Received Date 2019-06-12 00:00:00
Iyear 2019.0
Report Number 20190058.0
Supplemental Number 32536.0
Report Type Supplemental Final
Operator Id 18484 PHMSA Enforcement
Name Southern California Gas Co
Operator Street Address 555 West Fifth Street
Operator City Name Los Angeles
Operator State Abbreviation CA
Operator Postal Code 90013
Local Datetime 2019-05-13 22:32:00
Location Street Address 15563 Feldspar Dr.
Location City Name Chino Hills
Location County Name San Bernardino
Location State Abbreviation CA
Location Postal Code 91709-2125
Location Latitude 33.97081 Google Maps OpenStreetMap
Location Longitude -117.7502 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-05-14 05:55:00
Nrc Rpt Num 1245573 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 2270.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-05-13 22:32:00
On Site Datetime 2019-05-13 23:00:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1978.0
Pipe Diameter 8.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.188
Release Type Mechanical Puncture
Puncture Axial 1.5
Puncture Circum 1.3
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 95090.0
Est Cost Emergency 200.0
Est Cost Other 0.0
Est Cost Unintentional Release 13620.0
Prpty 108910.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 45.0
Normal Psig 45.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype State Highway
Excavator Type Contractor
Excavator Equipment Auger
Work Performed Fencing
One Call Notified Ind Yes
One Call Ticket Num 191190876
One Call Center Name Usa North
Locator Type Utility Owner
Visible Marks Yes
Service Interruption No
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name A***** W*****
Preparer Title Pipeline Safety Compliance Advisor
Preparer Email A*******@s**************.com
Preparer Telephone 818-632-8407
Authorizer Name A***** W*****
Authorizer Title Pipeline Safety Compliance Advisor
Authorizer Telephone 818-632-8407
Authorizer Email A*******@s**************.com
Narrative On may 14, 2019, a third party contractor while auguring to install guard rail posts damaged an 8-inch steel main causing a gas leak. Socalgas company crew responded and controlled the gas. No injuries or further damage resulted from this incident. The 8-inch steel main was repaired by replacing a section of the pipe. Investigation of the incident showed that there was a valid USA ticket for the contractor and the 8-inch main was properly marked. The contractor failed to use hand tools where required. This incident was reported to DOT and cpuc due to gas release and estimated property damage of $50,000 or more. 8/9/2019 update: updated part d (2b.) estimated cost of operator's property damage & repairs from $200,000 to $95,090. Submitted final report.

All rights reserved. Copyright © by ClearPHMSA