GD incident on 2019-04-30 — CO

Operator
Public Service Co Of Colorado
Cause
Notification Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,206
Incident datetime
2019-04-30 11:37
Report number
Location
CO, JEFFERSON
Narrative
The local fire department notified our dispatch of a gas leak. The company responder had just arrived when the explosion occurred. The fire department had already evacuated occupants and no injuries were suffered. The gas leak was caused by a third party excavator installing an electric ground rod. Please note response to a13b indicates that service to structure was initially squeezed off and then permanently cut-off. If and when service is resumed to this address, a new service will be installed. Please note original nrc report number is 1244219. Report was corrected to a pipeline incident and issued nrc number 1244222.
Detailed record list
Occurred At
2019-04-30 11:37:00
Year
2019
Report Received Date
2019-05-28 00:00:00
Iyear
2019.0
Report Number
20190053.0
Supplemental Number
32200.0
Report Type
Original Final
Operator Id
Name
Public Service Co Of Colorado
Operator Street Address
3500 Blake St
Operator City Name
Denver
Operator State Abbreviation
CO
Operator Postal Code
80205
Local Datetime
2019-04-30 12:25:00
Location Street Address
22555 Treetop Lane
Location City Name
Golden
Location County Name
Jefferson
Location State Abbreviation
CO
Location Postal Code
80401
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-04-30 13:56:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
47.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
6.0
Incident Identified Datetime
2019-04-30 11:37:00
On Site Datetime
2019-04-30 12:24:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
32.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service
Installation Year
1994.0
Pipe Diameter
0.75
Pipe Specification
Astm D2513
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
0.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
151010.0
Est Cost Prop Damage
6206.0
Est Cost Emergency
2944.0
Est Cost Other
0.0
Est Cost Unintentional Release
105.0
Prpty
160265.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
5.0
Accident Psig
56.0
Normal Psig
56.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident did not result in pressures out side normal ranges or any alarms.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Hand Tools
Work Performed
Electric
One Call Notified Ind
No
Service Interruption
Yes
Service Interruption Hours
4.0
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
K******** F***
Preparer Title
Gas Distribution Engineer
Preparer Email
K*************@x*********.com
Preparer Telephone
303-571-3365
Authorizer Name
M*** N****
Authorizer Title
Principal Engineer
Authorizer Telephone
303-571-3931
Authorizer Email
M*********@x*********.com
Narrative
The local fire department notified our dispatch of a gas leak. The company responder had just arrived when the explosion occurred. The fire department had already evacuated occupants and no injuries were suffered. The gas leak was caused by a third party excavator installing an electric ground rod. Please note response to a13b indicates that service to structure was initially squeezed off and then permanently cut-off. If and when service is resumed to this address, a new service will be installed. Please note original nrc report number is 1244219. Report was corrected to a pipeline incident and issued nrc number 1244222.
Occurred At 2019-04-30 11:37:00
Year 2019
Report Received Date 2019-05-28 00:00:00
Iyear 2019.0
Report Number 20190053.0
Supplemental Number 32200.0
Report Type Original Final
Operator Id 15931 PHMSA Enforcement
Name Public Service Co Of Colorado
Operator Street Address 3500 Blake St
Operator City Name Denver
Operator State Abbreviation CO
Operator Postal Code 80205
Local Datetime 2019-04-30 12:25:00
Location Street Address 22555 Treetop Lane
Location City Name Golden
Location County Name Jefferson
Location State Abbreviation CO
Location Postal Code 80401
Location Latitude 39.69741 Google Maps OpenStreetMap
Location Longitude -105.25469 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-04-30 13:56:00
Nrc Rpt Num 1244219 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 47.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 6.0
Incident Identified Datetime 2019-04-30 11:37:00
On Site Datetime 2019-04-30 12:24:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 32.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Service
Installation Year 1994.0
Pipe Diameter 0.75
Pipe Specification Astm D2513
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 0.5
Class Location Type Class 3 Location
Est Cost Oper Paid 151010.0
Est Cost Prop Damage 6206.0
Est Cost Emergency 2944.0
Est Cost Other 0.0
Est Cost Unintentional Release 105.0
Prpty 160265.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 5.0
Accident Psig 56.0
Normal Psig 56.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The incident did not result in pressures out side normal ranges or any alarms.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Hand Tools
Work Performed Electric
One Call Notified Ind No
Service Interruption Yes
Service Interruption Hours 4.0
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name K******** F***
Preparer Title Gas Distribution Engineer
Preparer Email K*************@x*********.com
Preparer Telephone 303-571-3365
Authorizer Name M*** N****
Authorizer Title Principal Engineer
Authorizer Telephone 303-571-3931
Authorizer Email M*********@x*********.com
Narrative The local fire department notified our dispatch of a gas leak. The company responder had just arrived when the explosion occurred. The fire department had already evacuated occupants and no injuries were suffered. The gas leak was caused by a third party excavator installing an electric ground rod. Please note response to a13b indicates that service to structure was initially squeezed off and then permanently cut-off. If and when service is resumed to this address, a new service will be installed. Please note original nrc report number is 1244219. Report was corrected to a pipeline incident and issued nrc number 1244222.

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