GTG incident on 2019-03-20 — NE

Operator
Northern Natural Gas Co
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100,000
Incident datetime
2019-03-20 12:00
Report number
Location
NE
Narrative
On march 20, 2019, the ogden (iowa) field operations team was notified by the county sheriff of gas blowing under the flood waters of the des moines river near the town of lehigh, iowa. The lehigh take-off valve setting is located in this area and was completely submerged by the flood waters of the des moines, river. The leak was small enough that no loss of service occurred. The field operations team inspected the site daily to monitor the leak and check on flood water levels. The site was still under water as of april 12, 2019 but the leak was visible from shore. The butt weld below the blow off valve between the weld neck flange and tee is cracked probably due to being struck by floating ice. The weld quality is not suspected so it won't be sent to a laboratory for any further analysis. The take-off setting was totally bypassed to eliminate the leak. The section of a-line was isolated, blown down and capped. The town of lehigh, ia is being fed from the b-line.
Detailed record list
Report Received Date
2019-04-12 00:00:00
Iyear
2019
Report Number
20190042
Supplemental Number
32017
Report Type
Supplemental Final
Operator Id
Name
Northern Natural Gas Co
Operator Street Address
1111 South 103rd Street
Operator City Name
Omaha
Operator State Abbreviation
NE
Operator Postal Code
68124
Local Datetime
2019-03-20 12:00:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2019-03-20 16:30:00
Commodity Released Type
Natural Gas
Unintentional Release
62000
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
Service To The Town Of Lehigh, Ia Could Be Maintained With The Leak.
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2019-03-20 12:00:00
On Site Datetime
2019-03-20 13:00:00
On Off Shore
Onshore
Onshore State Abbreviation
Ia
Onshore Postal Code
50557
Onshore City Name
Not Within A Municipality
Onshore County Name
Webster
Designated Location
Milepost
Designated Name
20.88
Pipe Fac Name
Ogden To Ventura
Segment Name
M520a
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Weld/fusion, Including Heat-Affected Zone
Weld Subtype
Other Butt Weld
Installation Year
1956
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
70
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
142600
Est Cost Intentional Release
0
Est Cost Prop Damage
100000
Est Cost Emergency
10000
Est Cost Other
0
Prpty
252600
Accident Psig
360
Mop Psig
380
Mop Cfr Section
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
10600
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
2-Inch Pipeline
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
2-Inch Pipeline
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak is so small that scada did not register a pressure drop and there was no loss of service.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Other
Nf Other Details
Floating Debris (Wood Or Ice) Struck Above Ground Appurtenance That Was Submerged In Flood Waters And Caused Leakage.
Nf Extreme Weather Ind
No
Preparer Name
J*** A G******
Preparer Title
Sr Corrosion Specialist - Pipeline Safety
Preparer Email
J***********@n****.com
Preparer Telephone
402-398-7494
Authorizer Name
T** C******
Authorizer Title
Vp Pipeline Safety And Risk
Authorizer Telephone
402-398-7715
Authorizer Email
T*************@n****.com
Narrative
On march 20, 2019, the ogden (iowa) field operations team was notified by the county sheriff of gas blowing under the flood waters of the des moines river near the town of lehigh, iowa. The lehigh take-off valve setting is located in this area and was completely submerged by the flood waters of the des moines, river. The leak was small enough that no loss of service occurred. The field operations team inspected the site daily to monitor the leak and check on flood water levels. The site was still under water as of april 12, 2019 but the leak was visible from shore. The butt weld below the blow off valve between the weld neck flange and tee is cracked probably due to being struck by floating ice. The weld quality is not suspected so it won't be sent to a laboratory for any further analysis. The take-off setting was totally bypassed to eliminate the leak. The section of a-line was isolated, blown down and capped. The town of lehigh, ia is being fed from the b-line.
Report Received Date 2019-04-12 00:00:00
Iyear 2019
Report Number 20190042
Supplemental Number 32017
Report Type Supplemental Final
Operator Id 13750 PHMSA Enforcement
Name Northern Natural Gas Co
Operator Street Address 1111 South 103rd Street
Operator City Name Omaha
Operator State Abbreviation NE
Operator Postal Code 68124
Local Datetime 2019-03-20 12:00:00
Location Latitude 42.348676 Google Maps OpenStreetMap
Location Longitude -94.040829 Google Maps OpenStreetMap
Nrc Rpt Num 1240413 NRC Report How to search
Nrc Rpt Datetime 2019-03-20 16:30:00
Commodity Released Type Natural Gas
Unintentional Release 62000
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain Service To The Town Of Lehigh, Ia Could Be Maintained With The Leak.
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2019-03-20 12:00:00
On Site Datetime 2019-03-20 13:00:00
On Off Shore Onshore
Onshore State Abbreviation Ia
Onshore Postal Code 50557
Onshore City Name Not Within A Municipality
Onshore County Name Webster
Designated Location Milepost
Designated Name 20.88
Pipe Fac Name Ogden To Ventura
Segment Name M520a
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Weld/fusion, Including Heat-Affected Zone
Weld Subtype Other Butt Weld
Installation Year 1956
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 70
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 142600
Est Cost Intentional Release 0
Est Cost Prop Damage 100000
Est Cost Emergency 10000
Est Cost Other 0
Prpty 252600
Accident Psig 360
Mop Psig 380
Mop Cfr Section 192.619(C) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 10600
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details 2-Inch Pipeline
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details 2-Inch Pipeline
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak is so small that scada did not register a pressure drop and there was no loss of service.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Heavy Rains/floods
Natural Force Type Heavy Rains/floods
Heavy Rains Subtype Other
Nf Other Details Floating Debris (Wood Or Ice) Struck Above Ground Appurtenance That Was Submerged In Flood Waters And Caused Leakage.
Nf Extreme Weather Ind No
Preparer Name J*** A G******
Preparer Title Sr Corrosion Specialist - Pipeline Safety
Preparer Email J***********@n****.com
Preparer Telephone 402-398-7494
Authorizer Name T** C******
Authorizer Title Vp Pipeline Safety And Risk
Authorizer Telephone 402-398-7715
Authorizer Email T*************@n****.com
Narrative On march 20, 2019, the ogden (iowa) field operations team was notified by the county sheriff of gas blowing under the flood waters of the des moines river near the town of lehigh, iowa. The lehigh take-off valve setting is located in this area and was completely submerged by the flood waters of the des moines, river. The leak was small enough that no loss of service occurred. The field operations team inspected the site daily to monitor the leak and check on flood water levels. The site was still under water as of april 12, 2019 but the leak was visible from shore. The butt weld below the blow off valve between the weld neck flange and tee is cracked probably due to being struck by floating ice. The weld quality is not suspected so it won't be sent to a laboratory for any further analysis. The take-off setting was totally bypassed to eliminate the leak. The section of a-line was isolated, blown down and capped. The town of lehigh, ia is being fed from the b-line.

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