GD incident on 2019-03-05 — NY

Operator
Keyspan Energy Delivery - Ny City
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$11,800
Incident datetime
2019-03-05 11:24
Report number
Location
NY, KINGS
Narrative
**supplement created 5/28/2019. Revised number of individuals injured to 0 based on information at site. We do not know the extent of the injuries, but 4 people were treated for minor injuries (minor burns, sprain). No further detail has been provided and no update has been provided to the company regarding more serious injury to any individual(s).** at 11:38, national grid dispatch and schedule was notified by the fdny of a fire in a trench at the intersection of kent ave and broadway. Customer meter services (cms) was dispatched to the location.And discovered 12 inch cast iron main leaking and ignited inside the trench. The root cause of the incident was third party damage as a result of city/state construction activity. The gas main was marked out but mark-out failed to mark the location of a tee connection and stub. There was a 1 foot gap between gas main and new water main. Additionally, it was found that the national grid inspector on-site failed to identify the tee that was on the print ids but not on the markout. The contractor hit the stub piece while excavating with the backhoe and the gas main ignited. Field operations located the damage and secured the main on either side of the fire on 3/5/2019 at 20:00. There were 4 injuries on the location (3 males were taken to cornell medical center for fire related injuries and 1 male was taken to wyckoff hospital for a non-fire related injury). Field operations secured the main on either side of the fire at (3/5/2019 at approx. 20:00) using stopper and creating a firewall, causing the temporary interruption of service to (1) customer. Field operations replaced a 7 foot section of the affected main to make the repair. As a result of this incident, an incident analysis was performed. As recommended by principles of pipeline safety management, all future city/state construction daily reports will now include documentation for the inspector to verify the gas markouts and perform the job walk-through.
Detailed record list
Occurred At
2019-03-05 11:24:00
Year
2019
Report Received Date
2019-04-01 00:00:00
Iyear
2019.0
Report Number
20190034.0
Supplemental Number
32205.0
Report Type
Supplemental Final
Operator Id
Name
Keyspan Energy Delivery - Ny City
Operator Street Address
2 Hanson Place
Operator City Name
Brooklyn
Operator State Abbreviation
NY
Operator Postal Code
11217
Local Datetime
2019-03-05 11:00:00
Location Street Address
Intersection Of Kent Avenue And Broadway
Location City Name
Brooklyn
Location County Name
Kings
Location State Abbreviation
NY
Location Postal Code
11249
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-03-05 14:42:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
1158.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2019-03-05 11:24:00
On Site Datetime
2019-03-05 11:45:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Pipe Diameter
12.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Cast/wrought Iron
Release Type
Mechanical Puncture
Puncture Axial
6.0
Puncture Circum
6.0
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
11800.0
Est Cost Emergency
36240.0
Est Cost Other
0.0
Est Cost Unintentional Release
5155.0
Prpty
53195.0
Commercial Affected
1.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
0.3
Normal Psig
0.33
Mop Psig
0.43
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The operator did not find that an investigation of the controller's actions or control room issues was necessary. This incident was due to a report of contractor damage.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date
2019-02-19 00:00:00
Ex Hydrotest Conducted Ind
No
Prior Notification Ind
Yes
One Call System Ind
Yes
Contractor Ind
Yes
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Water
One Call Notified Ind
Yes
One Call Ticket Num
190590316
One Call Center Name
New York 811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
7.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name
C****** B*****
Preparer Title
Principal Program Manager Gas Work Methods
Preparer Email
C*************@n***********.com
Preparer Telephone
6317703549
Authorizer Name
C****** B*****
Authorizer Title
Principal Program Manager Gas Work Methods
Authorizer Telephone
6317703549
Authorizer Email
C*************@n***********.com
Narrative
**supplement created 5/28/2019. Revised number of individuals injured to 0 based on information at site. We do not know the extent of the injuries, but 4 people were treated for minor injuries (minor burns, sprain). No further detail has been provided and no update has been provided to the company regarding more serious injury to any individual(s).** at 11:38, national grid dispatch and schedule was notified by the fdny of a fire in a trench at the intersection of kent ave and broadway. Customer meter services (cms) was dispatched to the location.And discovered 12 inch cast iron main leaking and ignited inside the trench. The root cause of the incident was third party damage as a result of city/state construction activity. The gas main was marked out but mark-out failed to mark the location of a tee connection and stub. There was a 1 foot gap between gas main and new water main. Additionally, it was found that the national grid inspector on-site failed to identify the tee that was on the print ids but not on the markout. The contractor hit the stub piece while excavating with the backhoe and the gas main ignited. Field operations located the damage and secured the main on either side of the fire on 3/5/2019 at 20:00. There were 4 injuries on the location (3 males were taken to cornell medical center for fire related injuries and 1 male was taken to wyckoff hospital for a non-fire related injury). Field operations secured the main on either side of the fire at (3/5/2019 at approx. 20:00) using stopper and creating a firewall, causing the temporary interruption of service to (1) customer. Field operations replaced a 7 foot section of the affected main to make the repair. As a result of this incident, an incident analysis was performed. As recommended by principles of pipeline safety management, all future city/state construction daily reports will now include documentation for the inspector to verify the gas markouts and perform the job walk-through.
Occurred At 2019-03-05 11:24:00
Year 2019
Report Received Date 2019-04-01 00:00:00
Iyear 2019.0
Report Number 20190034.0
Supplemental Number 32205.0
Report Type Supplemental Final
Operator Id 1800 PHMSA Enforcement
Name Keyspan Energy Delivery - Ny City
Operator Street Address 2 Hanson Place
Operator City Name Brooklyn
Operator State Abbreviation NY
Operator Postal Code 11217
Local Datetime 2019-03-05 11:00:00
Location Street Address Intersection Of Kent Avenue And Broadway
Location City Name Brooklyn
Location County Name Kings
Location State Abbreviation NY
Location Postal Code 11249
Location Latitude 40.712043 Google Maps OpenStreetMap
Location Longitude -73.968144 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-03-05 14:42:00
Nrc Rpt Num 1239301 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 1158.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2019-03-05 11:24:00
On Site Datetime 2019-03-05 11:45:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Pipe Diameter 12.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Cast/wrought Iron
Release Type Mechanical Puncture
Puncture Axial 6.0
Puncture Circum 6.0
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 11800.0
Est Cost Emergency 36240.0
Est Cost Other 0.0
Est Cost Unintentional Release 5155.0
Prpty 53195.0
Commercial Affected 1.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 0.3
Normal Psig 0.33
Mop Psig 0.43
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The operator did not find that an investigation of the controller's actions or control room issues was necessary. This incident was due to a report of contractor damage.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date 2019-02-19 00:00:00
Ex Hydrotest Conducted Ind No
Prior Notification Ind Yes
One Call System Ind Yes
Contractor Ind Yes
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Water
One Call Notified Ind Yes
One Call Ticket Num 190590316
One Call Center Name New York 811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 7.0
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Incomplete Marks At Damage Location
Preparer Name C****** B*****
Preparer Title Principal Program Manager Gas Work Methods
Preparer Email C*************@n***********.com
Preparer Telephone 6317703549
Authorizer Name C****** B*****
Authorizer Title Principal Program Manager Gas Work Methods
Authorizer Telephone 6317703549
Authorizer Email C*************@n***********.com
Narrative **supplement created 5/28/2019. Revised number of individuals injured to 0 based on information at site. We do not know the extent of the injuries, but 4 people were treated for minor injuries (minor burns, sprain). No further detail has been provided and no update has been provided to the company regarding more serious injury to any individual(s).** at 11:38, national grid dispatch and schedule was notified by the fdny of a fire in a trench at the intersection of kent ave and broadway. Customer meter services (cms) was dispatched to the location.And discovered 12 inch cast iron main leaking and ignited inside the trench. The root cause of the incident was third party damage as a result of city/state construction activity. The gas main was marked out but mark-out failed to mark the location of a tee connection and stub. There was a 1 foot gap between gas main and new water main. Additionally, it was found that the national grid inspector on-site failed to identify the tee that was on the print ids but not on the markout. The contractor hit the stub piece while excavating with the backhoe and the gas main ignited. Field operations located the damage and secured the main on either side of the fire on 3/5/2019 at 20:00. There were 4 injuries on the location (3 males were taken to cornell medical center for fire related injuries and 1 male was taken to wyckoff hospital for a non-fire related injury). Field operations secured the main on either side of the fire at (3/5/2019 at approx. 20:00) using stopper and creating a firewall, causing the temporary interruption of service to (1) customer. Field operations replaced a 7 foot section of the affected main to make the repair. As a result of this incident, an incident analysis was performed. As recommended by principles of pipeline safety management, all future city/state construction daily reports will now include documentation for the inspector to verify the gas markouts and perform the job walk-through.

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