GD incident on 2019-01-31 — OH

Operator
Columbia Gas Of Ohio Inc
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,200
Incident datetime
2019-01-31 03:42
Report number
Location
OH, ERIE
Narrative
At approximately 03:39 on 01-31-2019, a driver of a motor vehicle failed to control the vehicle and traveled approximately 100 feet off the roadway striking the meter setting at 15319 darrow rd., vermilion. The driver of the vehicle fled the scene. The damage to the meter setting resulted in a release of natural gas and a subsequent explosion and fire. The vermilion township fire department evacuated the occupants of the home and battled the fire until columbia gas of ohio representatives arrived at the scene and turned the service line valve off to stop the flow of gas. Once the fire was contained, a surface leak survey was completed with no leakage found. The riser was disassembled and the service line passed a pressure test. The service line was cut and plugged at the main and not placed back in service. The nrc number was corrected in part a. *******per phmsas direction I updated a-13b to reflect that the distribution service line was restarted despite being physically disconnected and plugged on 1-31-19 at 10:00am.*******
Detailed record list
Occurred At
2019-01-31 03:42:00
Year
2019
Report Received Date
2019-03-01 00:00:00
Iyear
2019.0
Report Number
20190019.0
Supplemental Number
32649.0
Report Type
Supplemental Final
Operator Id
Name
Columbia Gas Of Ohio Inc
Operator Street Address
290 W Nationwide Blvd
Operator City Name
Columbus
Operator State Abbreviation
OH
Operator Postal Code
43215
Local Datetime
2019-01-31 03:39:00
Location Street Address
15319 Darrow Rd.
Location City Name
Vermilion
Location County Name
Erie
Location State Abbreviation
OH
Location Postal Code
44089
Location Latitude
Location Longitude
Nrc Rpt Datetime
2019-01-31 04:50:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
21.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
2.0
Incident Identified Datetime
2019-01-31 03:42:00
On Site Datetime
2019-01-31 04:05:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Outside Meter/regulator Set
Installation Year
1972.0
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Leak
Leak Type
Other
Leak Type Other
Due To Vehicular Damage
Class Location Type
Class 3 Location
Est Cost Oper Paid
212700.0
Est Cost Prop Damage
1200.0
Est Cost Emergency
4327.0
Est Cost Other
0.0
Est Cost Unintentional Release
69.0
Prpty
218296.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Preparer Name
R** R* S****
Preparer Title
Manager Of Compliance
Preparer Email
R******@n*******.com
Preparer Telephone
614-818-2110
Preparer Fax
614-818-2151
Authorizer Name
R** R* S****
Authorizer Title
Manager Of Compliance
Authorizer Telephone
614-818-2110
Authorizer Email
R******@n*******.com
Narrative
At approximately 03:39 on 01-31-2019, a driver of a motor vehicle failed to control the vehicle and traveled approximately 100 feet off the roadway striking the meter setting at 15319 darrow rd., vermilion. The driver of the vehicle fled the scene. The damage to the meter setting resulted in a release of natural gas and a subsequent explosion and fire. The vermilion township fire department evacuated the occupants of the home and battled the fire until columbia gas of ohio representatives arrived at the scene and turned the service line valve off to stop the flow of gas. Once the fire was contained, a surface leak survey was completed with no leakage found. The riser was disassembled and the service line passed a pressure test. The service line was cut and plugged at the main and not placed back in service. The nrc number was corrected in part a. *******per phmsas direction I updated a-13b to reflect that the distribution service line was restarted despite being physically disconnected and plugged on 1-31-19 at 10:00am.*******
Occurred At 2019-01-31 03:42:00
Year 2019
Report Received Date 2019-03-01 00:00:00
Iyear 2019.0
Report Number 20190019.0
Supplemental Number 32649.0
Report Type Supplemental Final
Operator Id 2596 PHMSA Enforcement
Name Columbia Gas Of Ohio Inc
Operator Street Address 290 W Nationwide Blvd
Operator City Name Columbus
Operator State Abbreviation OH
Operator Postal Code 43215
Local Datetime 2019-01-31 03:39:00
Location Street Address 15319 Darrow Rd.
Location City Name Vermilion
Location County Name Erie
Location State Abbreviation OH
Location Postal Code 44089
Location Latitude 41.38932 Google Maps OpenStreetMap
Location Longitude -82.35938 Google Maps OpenStreetMap
Nrc Rpt Datetime 2019-01-31 04:50:00
Nrc Rpt Num 1236403 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 21.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 2.0
Incident Identified Datetime 2019-01-31 03:42:00
On Site Datetime 2019-01-31 04:05:00
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Outside Meter/regulator Set
Installation Year 1972.0
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Leak
Leak Type Other
Leak Type Other Due To Vehicular Damage
Class Location Type Class 3 Location
Est Cost Oper Paid 212700.0
Est Cost Prop Damage 1200.0
Est Cost Emergency 4327.0
Est Cost Other 0.0
Est Cost Unintentional Release 69.0
Prpty 218296.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 1.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Third Party
Preparer Name R** R* S****
Preparer Title Manager Of Compliance
Preparer Email R******@n*******.com
Preparer Telephone 614-818-2110
Preparer Fax 614-818-2151
Authorizer Name R** R* S****
Authorizer Title Manager Of Compliance
Authorizer Telephone 614-818-2110
Authorizer Email R******@n*******.com
Narrative At approximately 03:39 on 01-31-2019, a driver of a motor vehicle failed to control the vehicle and traveled approximately 100 feet off the roadway striking the meter setting at 15319 darrow rd., vermilion. The driver of the vehicle fled the scene. The damage to the meter setting resulted in a release of natural gas and a subsequent explosion and fire. The vermilion township fire department evacuated the occupants of the home and battled the fire until columbia gas of ohio representatives arrived at the scene and turned the service line valve off to stop the flow of gas. Once the fire was contained, a surface leak survey was completed with no leakage found. The riser was disassembled and the service line passed a pressure test. The service line was cut and plugged at the main and not placed back in service. The nrc number was corrected in part a. *******per phmsas direction I updated a-13b to reflect that the distribution service line was restarted despite being physically disconnected and plugged on 1-31-19 at 10:00am.*******

All rights reserved. Copyright © by ClearPHMSA