GD incident on 2018-12-13 — GA

Operator
Atlanta Gas Light Co
Cause
Notification Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,667,000
Incident datetime
2018-12-13 14:20
Report number
Location
GA, CHATHAM
Narrative
At approximately 13:57 on december 13, 2018 atlanta gas light company (aglc) received telephonic notice from the savannah fire department indicating that damage had occurred to aglc natural gas facilities in the area of 100 general mcintosh blvd in savannah, ga. Shortly after arrival to the site, aglc crews determined damage had occurred to a 125 psig 8-inch steel main that crosses the savannah river supplying customers to hutchison island. The damaged was found to occur on the west land side of the river. To stop the flow of gas at the damage, a nearby valve was turned off which caused a total of seventeen customers to lose natural gas service for approximately 9 hours. The excavator responsible for the damage was drilling for pilings as part of a site development project in the area. There was no valid locate request at the time of excavation. The most recent locate request for the area of the damage by the excavator was received by aglc on august 23, 2018. As a normal locate request in georgia is valid for thirty (30) days, this request was valid until september 22, 2018. As the pipeline is still shut down pending repair or replacement, customers who lost natural gas service due to the damage, are being provided service by a compressed natural gas tanker that has been placed on the island. Pipeline that was damaged was replaced with a new 8-inch steel pipeline. Natural gas was restored to customers on the island on may 15, 2019. During the pipeline shutdown, customers were provided service by compressed natural gas facilities that were placed on the island. Additional nrc report number 1232992 was created for the same event after a 48-hour supplemental call was placed with the nrc.
Detailed record list
Occurred At
2018-12-13 14:20:00
Year
2018
Report Received Date
2019-01-10 00:00:00
Iyear
2018.0
Report Number
20190005.0
Supplemental Number
32625.0
Report Type
Supplemental Final
Operator Id
Name
Atlanta Gas Light Co
Operator Street Address
10 Peachtree Place Ne
Operator City Name
Atlanta
Operator State Abbreviation
GA
Operator Postal Code
30309
Local Datetime
2018-12-13 13:57:00
Location Street Address
100 General Mcintosh Blvd.
Location City Name
Savannah
Location County Name
Chatham
Location State Abbreviation
GA
Location Postal Code
31401
Location Latitude
Location Longitude
Nrc Rpt Datetime
2018-12-13 15:15:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
175.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2018-12-13 14:20:00
On Site Datetime
2018-12-13 14:00:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
840.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2007.0
Pipe Diameter
8.0
Pipe Specification
Api 5l
Pipe Manufacturer
Maverick Steel
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.219
Release Type
Mechanical Puncture
Puncture Axial
0.1
Puncture Circum
2.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
1667000.0
Est Cost Emergency
5000.0
Est Cost Other
376500.0
Est Cost Other Details
Cng Costs Related To Keeping Customers In Service.
Est Cost Unintentional Release
724.0
Prpty
2049224.0
Commercial Affected
2.0
Industrial Affected
0.0
Residences Affected
15.0
Accident Psig
110.0
Normal Psig
125.0
Mop Psig
125.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Easement
Excavator Type
Contractor
Excavator Equipment
Drilling
Work Performed
Site Development
One Call Notified Ind
No
Locator Type
Contract Locator
Visible Marks
No
Service Interruption
Yes
Service Interruption Hours
9.0
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
R*** S*****
Preparer Title
Director Compliance And Quality Assurance
Preparer Email
R******@s*********.com
Preparer Telephone
404-584-4910
Authorizer Name
R*** S*****
Authorizer Title
Director Compliance And Quality Assurance
Authorizer Telephone
404-584-4910
Authorizer Email
R******@s*********.com
Narrative
At approximately 13:57 on december 13, 2018 atlanta gas light company (aglc) received telephonic notice from the savannah fire department indicating that damage had occurred to aglc natural gas facilities in the area of 100 general mcintosh blvd in savannah, ga. Shortly after arrival to the site, aglc crews determined damage had occurred to a 125 psig 8-inch steel main that crosses the savannah river supplying customers to hutchison island. The damaged was found to occur on the west land side of the river. To stop the flow of gas at the damage, a nearby valve was turned off which caused a total of seventeen customers to lose natural gas service for approximately 9 hours. The excavator responsible for the damage was drilling for pilings as part of a site development project in the area. There was no valid locate request at the time of excavation. The most recent locate request for the area of the damage by the excavator was received by aglc on august 23, 2018. As a normal locate request in georgia is valid for thirty (30) days, this request was valid until september 22, 2018. As the pipeline is still shut down pending repair or replacement, customers who lost natural gas service due to the damage, are being provided service by a compressed natural gas tanker that has been placed on the island. Pipeline that was damaged was replaced with a new 8-inch steel pipeline. Natural gas was restored to customers on the island on may 15, 2019. During the pipeline shutdown, customers were provided service by compressed natural gas facilities that were placed on the island. Additional nrc report number 1232992 was created for the same event after a 48-hour supplemental call was placed with the nrc.
Occurred At 2018-12-13 14:20:00
Year 2018
Report Received Date 2019-01-10 00:00:00
Iyear 2018.0
Report Number 20190005.0
Supplemental Number 32625.0
Report Type Supplemental Final
Operator Id 792 PHMSA Enforcement
Name Atlanta Gas Light Co
Operator Street Address 10 Peachtree Place Ne
Operator City Name Atlanta
Operator State Abbreviation GA
Operator Postal Code 30309
Local Datetime 2018-12-13 13:57:00
Location Street Address 100 General Mcintosh Blvd.
Location City Name Savannah
Location County Name Chatham
Location State Abbreviation GA
Location Postal Code 31401
Location Latitude 32.07746361 Google Maps OpenStreetMap
Location Longitude -81.080208 Google Maps OpenStreetMap
Nrc Rpt Datetime 2018-12-13 15:15:00
Nrc Rpt Num 1232909 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 175.8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2018-12-13 14:20:00
On Site Datetime 2018-12-13 14:00:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 840.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2007.0
Pipe Diameter 8.0
Pipe Specification Api 5l
Pipe Manufacturer Maverick Steel
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.219
Release Type Mechanical Puncture
Puncture Axial 0.1
Puncture Circum 2.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 1667000.0
Est Cost Emergency 5000.0
Est Cost Other 376500.0
Est Cost Other Details Cng Costs Related To Keeping Customers In Service.
Est Cost Unintentional Release 724.0
Prpty 2049224.0
Commercial Affected 2.0
Industrial Affected 0.0
Residences Affected 15.0
Accident Psig 110.0
Normal Psig 125.0
Mop Psig 125.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Easement
Excavator Type Contractor
Excavator Equipment Drilling
Work Performed Site Development
One Call Notified Ind No
Locator Type Contract Locator
Visible Marks No
Service Interruption Yes
Service Interruption Hours 9.0
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name R*** S*****
Preparer Title Director Compliance And Quality Assurance
Preparer Email R******@s*********.com
Preparer Telephone 404-584-4910
Authorizer Name R*** S*****
Authorizer Title Director Compliance And Quality Assurance
Authorizer Telephone 404-584-4910
Authorizer Email R******@s*********.com
Narrative At approximately 13:57 on december 13, 2018 atlanta gas light company (aglc) received telephonic notice from the savannah fire department indicating that damage had occurred to aglc natural gas facilities in the area of 100 general mcintosh blvd in savannah, ga. Shortly after arrival to the site, aglc crews determined damage had occurred to a 125 psig 8-inch steel main that crosses the savannah river supplying customers to hutchison island. The damaged was found to occur on the west land side of the river. To stop the flow of gas at the damage, a nearby valve was turned off which caused a total of seventeen customers to lose natural gas service for approximately 9 hours. The excavator responsible for the damage was drilling for pilings as part of a site development project in the area. There was no valid locate request at the time of excavation. The most recent locate request for the area of the damage by the excavator was received by aglc on august 23, 2018. As a normal locate request in georgia is valid for thirty (30) days, this request was valid until september 22, 2018. As the pipeline is still shut down pending repair or replacement, customers who lost natural gas service due to the damage, are being provided service by a compressed natural gas tanker that has been placed on the island. Pipeline that was damaged was replaced with a new 8-inch steel pipeline. Natural gas was restored to customers on the island on may 15, 2019. During the pipeline shutdown, customers were provided service by compressed natural gas facilities that were placed on the island. Additional nrc report number 1232992 was created for the same event after a 48-hour supplemental call was placed with the nrc.

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