HL incident on 2018-11-29 — TX

Operator
Energy Transfer Company
Cause
Excavation Issue
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$45,450
Incident datetime
2018-11-29 10:06
Report number
Location
TX
Narrative
On november 29, 2018 at approximately 10:00 am, energy transfer's 4inch ngl s315 jameson plant lateral pipeline experienced a discharge caused by third party damage. The line is located in nolan county in maryneal, tx. A contractor performing work for another operator was operating a track-hoe with a shaker bucket and struck the energy transfer line and caused a leak. The contractor stated that when using the shaker bucket on the track-hoe to backfill his excavation, the track-hoe began sliding toward the ditch. The contractor laid his shaker bucket down to stop the sliding of his equipment and struck the pipeline. Energy transfer personnel noticed the gas cloud while heading to the excavation location and notified additional energy transfer employees at 10:06 am. These company personnel immediately proceeded to shut in the pipeline by closing in the upstream mainline valve and downstream mainline valve at 10:22 am and 10:40 am respectively. The affected pipe segment was cut out and replaced with pre-tested pipe. The pipeline was brought back to service on december 1, 2018 at approximately 10:00 am. Energy transfer will continue to execute procedures outlined within our damage prevention procedures and spread public awareness through our public awareness program to help prevent reoccurrences. This pipeline is under the jurisdiction of the texas railroad commission the txrrc was notified on november 29, 2018 at 3:43 pm. Incident # 1889
Detailed record list
Report Received Date
2018-12-21 00:00:00
Iyear
2018
Report Number
20180407
Supplemental Number
31383
Report Type
Original Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2018-11-29 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
1150
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2018-11-29 10:06:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2018-11-29 10:00:00
Restart Datetime
2018-12-01 10:00:00
On Site Datetime
2018-11-29 10:22:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
S315 Tx Ngl Jameson Plnt Ltrl
Segment Name
S315 Tx Ngl Jameson Plnt Ltrl
Onshore State Abbreviation
Tx
Onshore Postal Code
79535
Onshore City Name
Maryneal
Onshore County Name
Nolan
Designated Location
Milepost/valve Station
Designated Name
19.59
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4
Pipe Wall Thickness
0.188
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1956
Manufactured Year
1956
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
2
Puncture Circum
0.5
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
24000
Est Cost Prop Damage
45450
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
69450
Accident Psig
560
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
56390
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Investigation identified no controller issues. Controller actions were consistent with company protocol.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Liquid Pipeline
One Call Notified Ind
Yes
One Call Ticket Num
1882519236
One Call Center Name
811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
48
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
C********** P******
Preparer Title
Regulatory Compliance Specialist
Preparer Email
C******************@e*************.com
Preparer Telephone
713-989-4464
Prepared Date
2018-12-21 00:00:00
Authorizer Name
C********** K*****
Authorizer Telephone
713-989-7077
Authorizer Title
Manager-Intrastate Regulatory Compliance
Authorizer Email
C***********@e*************.com
Narrative
On november 29, 2018 at approximately 10:00 am, energy transfer's 4inch ngl s315 jameson plant lateral pipeline experienced a discharge caused by third party damage. The line is located in nolan county in maryneal, tx. A contractor performing work for another operator was operating a track-hoe with a shaker bucket and struck the energy transfer line and caused a leak. The contractor stated that when using the shaker bucket on the track-hoe to backfill his excavation, the track-hoe began sliding toward the ditch. The contractor laid his shaker bucket down to stop the sliding of his equipment and struck the pipeline. Energy transfer personnel noticed the gas cloud while heading to the excavation location and notified additional energy transfer employees at 10:06 am. These company personnel immediately proceeded to shut in the pipeline by closing in the upstream mainline valve and downstream mainline valve at 10:22 am and 10:40 am respectively. The affected pipe segment was cut out and replaced with pre-tested pipe. The pipeline was brought back to service on december 1, 2018 at approximately 10:00 am. Energy transfer will continue to execute procedures outlined within our damage prevention procedures and spread public awareness through our public awareness program to help prevent reoccurrences. This pipeline is under the jurisdiction of the texas railroad commission the txrrc was notified on november 29, 2018 at 3:43 pm. Incident # 1889
Report Received Date 2018-12-21 00:00:00
Iyear 2018
Report Number 20180407
Supplemental Number 31383
Report Type Original Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2018-11-29 10:00:00
Location Latitude 32.20252 Google Maps OpenStreetMap
Location Longitude -100.55267 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 1150
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2018-11-29 10:06:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2018-11-29 10:00:00
Restart Datetime 2018-12-01 10:00:00
On Site Datetime 2018-11-29 10:22:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name S315 Tx Ngl Jameson Plnt Ltrl
Segment Name S315 Tx Ngl Jameson Plnt Ltrl
Onshore State Abbreviation Tx
Onshore Postal Code 79535
Onshore City Name Maryneal
Onshore County Name Nolan
Designated Location Milepost/valve Station
Designated Name 19.59
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4
Pipe Wall Thickness 0.188
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1956
Manufactured Year 1956
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 2
Puncture Circum 0.5
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 24000
Est Cost Prop Damage 45450
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 69450
Accident Psig 560
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 56390
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Investigation identified no controller issues. Controller actions were consistent with company protocol.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Liquid Pipeline
One Call Notified Ind Yes
One Call Ticket Num 1882519236
One Call Center Name 811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 48
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name C********** P******
Preparer Title Regulatory Compliance Specialist
Preparer Email C******************@e*************.com
Preparer Telephone 713-989-4464
Prepared Date 2018-12-21 00:00:00
Authorizer Name C********** K*****
Authorizer Telephone 713-989-7077
Authorizer Title Manager-Intrastate Regulatory Compliance
Authorizer Email C***********@e*************.com
Narrative On november 29, 2018 at approximately 10:00 am, energy transfer's 4inch ngl s315 jameson plant lateral pipeline experienced a discharge caused by third party damage. The line is located in nolan county in maryneal, tx. A contractor performing work for another operator was operating a track-hoe with a shaker bucket and struck the energy transfer line and caused a leak. The contractor stated that when using the shaker bucket on the track-hoe to backfill his excavation, the track-hoe began sliding toward the ditch. The contractor laid his shaker bucket down to stop the sliding of his equipment and struck the pipeline. Energy transfer personnel noticed the gas cloud while heading to the excavation location and notified additional energy transfer employees at 10:06 am. These company personnel immediately proceeded to shut in the pipeline by closing in the upstream mainline valve and downstream mainline valve at 10:22 am and 10:40 am respectively. The affected pipe segment was cut out and replaced with pre-tested pipe. The pipeline was brought back to service on december 1, 2018 at approximately 10:00 am. Energy transfer will continue to execute procedures outlined within our damage prevention procedures and spread public awareness through our public awareness program to help prevent reoccurrences. This pipeline is under the jurisdiction of the texas railroad commission the txrrc was notified on november 29, 2018 at 3:43 pm. Incident # 1889

All rights reserved. Copyright © by ClearPHMSA